Log of the 560 SEL's life with us.

Saturday–Sunday, March 21–29, 2009

I kept seeing this car on Craig's List. The advertised price was low: $2195. It looked like our SDL, but shinier. Interesting...

Monday, March 30, 2009

...I gave it plenty of time to go away on me: it didn't. I called and went to see the car. The price was interesting, compelling even, and this looked like a perhaps more expedient way to get a large 126 running for Jill again than fixing up the SDL right now, since she likes that kind of car. I offered $2000, and he grudgingly accepted, though it represented a 50% loss to him. We shook on it, and I was to come back after 3:30 PM when he was to be back home and we'd complete the deal. I then picked up the funds at the bank, and printed out the Washington Declaration of Buyer and Seller Regarding Value of Used Vehicle Sold (Dept. of Revenue) form to fill out. I did not want to be taxed as if it sold for high Blue Book value! According to the DMV trolls, a Bill of Sale is not good enough to establish the taxable value.

In the afternoon I went back and got the car. After work I left the Frankenheap there and drove this car home, bringing home a returned power tool in its (larger, and empty) trunk. It drove well, nice and strong. I did notice:

...I got the neighbors to run me back down to work after dinner, and we picked up the other car. (I rode in the back of the SEL on the way down, and he drove the Frankenheap back—he'd been wanting to see how it drove since he has a project car almost exactly like it.) Additional observations:

Tuesday, March 31, 2009

A hint from the mailing list:
Change the fuel filters first. On an SDL, when the fuel filters are partially plugged, the first symptom is that upshifts don't happen unless you let off the pedal.

I cleaned the failed Gorilla Glue off the torn red-dot keyhead and re-glued it back together with something more suited for the purpose: Shoe Goo.

At lunch I tried to get the car licensed, but they say I can't until I get a stink test. (She did say that the BoS, signed Nevada title, and SoV form [above] were all I'd need to make the transfer, in addition to the State-mandated prostate exam.) OK, perhaps tomorrow. So in consolation, and because I wasn't too far away, I swung by the U-Pull and went shopping. They had a 123 manny-tranny 240D, so I grabbed its special cruise control amplifier for the parts pile. The 126 300SD supplied a rear-view mirror and a dome light, and the 201 190E supplied a too-small but better than nothing trunk carpet, a SRS-equipped seat belt assembly, and an EHA valve to sit in reserve. (There were no intact brake lamp housings or shifter knobs to be had.) The mirror and the seat belt are the biggies this car needed. It was sunny and fairly warm when I hit the yard, I debated leaving my coat in the car with my hat, but I didn't. Good idea, but bad idea leaving the hat: as I was working out there a huge lightning and hail storm blew in; I got pretty wet, and working out in a sea of metal was a bit disturbing. On the way back to work I passed several wrecks on the freeway, the accumulation of slush on the road was pretty significant and I'm sure visibility had been bad. Jill reported that as she was coming through town at around that time she was seeing 1" hailstones! (I think that's an exaggeration, but I'm sure they were large. I was seeing 1/4" stones where I was. The sheeple were probably regretting taking off the snow tires as State law mandates be done by the end of today (if studded). But it was snowing here recently, and the half inch of slush today seems to be a snow tire worthy event. The Law, as has been so ably noted before, is [at times] an Ass.)

Jill called me shortly after my return to work to let me know that she was home, and she seemed excited to see the big white car out in the driveway. My ruse worked! She thinks it's the SDL coming back to life. I wonder how long I can pull that off?

Regarding the possibility of eventually making an SDL out of an SEL I hit the State's web site on the vehicle emissions testing program, and was unable to find out anything so I sent in a query:

I see no information here on the ramifications of converting a vehicle to a different fuel type. (Gas to diesel, or vice-versa, or to/from propane, or even hybridization.) What are the regulations on such conversions?
I got back this:
In order to legally replace an engine with another fuel type, the vehicle must have been certified by EPA for that fuel type and all emission system components are intact and operation[al]. If you are converting a vehicle to exclusively run on propane, you will need the state patrol to inspect the vehicle first before licensing the vehicle. If the vehicle is dual powered, then you will need to pass an emission test every other year as regulations mandate.

Tom Olsen, Unit Manager
NWRO Emission Check Program

When I got home I checked, and the new seat belt tongue latched into the buckle so it's looking pretty good as a replacement so far.

Wednesday, April 1, 2009

The repaired key seems nice and strong. Good. I replaced the rear-view mirror, that went well. I then removed the passenger-side B-pillar cover, and the belt assembly was indeed entirely missing. The proposed replacement bolted in neatly, though the mount at the shoulder end is a little different and can't be tightened down all the way if the adjuster is still to move. Still, I think it'll do until I can acquire a better match. The pillar cover's glue was failing, and that's why the skin looked so bad. I painted contact cement on the failed areas and let it dry, then pressed the skin back in place. It's a little lumpy, but much better looking than before. I found that the hump's bolt cover was also missing on that side.

Since I was back there I had a look at the reading lights. They both worked for me then, I think the one just had a dirty switch contact. They didn't fit right, though. I had a closer look, and removed them both and swapped them over to their correct sides. They fit much better that way!

Next was the wonky switch panel on the driver's-side rear door. It just wouldn't stay in. After removing it and playing around for awhile, I figured out that the problem is that it's a right-side panel jammed into the left side! (Part #126 766 08 91, should be #126 766 07 91.) I'll have to get a new one, that's probably going to be a dealership item. While I was there I corrected the switch positions on the left and right sides. The loose panel will just have to stay loose until I get a replacement, I'm not going to try gluing it back in place like one of the PO's did!

Still in the back, I replaced the missing cigar lighter element on the driver's side with one from the junkbox. Its illuminating bulb was burnt out, so I replaced it with the one I bought yesterday.

Moving up front I replaced the burnt-out 9004 passenger-side headlight with the one from my spares pile. (I'll try to get another one today.) I also replaced the passenger-side fog lamp rear hatch cover, which I found in the glovebox. I replaced a couple of burnt-out fuses, and restocked the spares in the fuse box. (I blew one this morning trying to run the wipers with them frozen to the glass.)

The ruse continues to work. Not only did Jill pass it this morning on her way out, with me in it and working on the seat belt, but when she came back I was still in it. I invited her to sit inside with me. It was even running. She still thinks it's the SDL. She: "Did you remember what was wrong with it?" Me: "Oh, I'm figuring it out." She even walked by the open garage, where the SDL was certainly visible. I'm a-gonna pay for this one! :-)

...At lunch I went and got the stink test done, which passed. I then went and got it licensed, $255 with tax and plates. (Ouch.) I then went back to the U-Pull. I grabbed the 126's non-SRS seat belt, which has the special mounting hardware at the shoulder point, I might be able to combine it with the one I put in today. I got its taillights too, to lay in as spares for the two 126's we now have. (That was $30, let's hope we never need them.) I got the hump's plastic bolt covers, but they're a different style. We'll see if they'll work or not. I also stopped at the liquidation outlet and got two 9004's and an H3. 70% off today.

...After work it was snowing again and I hit the wipers. Skreeeeeeech! Oops, one of the blades was working out of its socket. I put it back, it seems to stay now—I'm guessing it wasn't snapped in all the way last time it was replaced. I tested the fanfare horn (loud and soft horn settings), it works. The fourth seat warmer also works, I turned it on and felt the seat later.

As it was starting to snow harder I scraped around and found the extra new antenna grommet for the 190D that I'd somehow ended up with, and fit it into the hole in the fender. I then poked the antenna up through it. That'll keep out the worst of the moisture. I have some work to do to actually install this thing correctly.

Thursday, April 2, 2009

I woke up to 1–2" of snow this morning, 3–4" on the cars. I don't think I'll be driving this car to work! I gathered up the remaining pieces of the shattered center brake light, and the shards I gleaned from the junkyard yesterday, and started fitting them together. I used cutters and files to roughly shape pieces to make something resembling an intact housing, since many of the original pieces had been lost. Mostly this is just to contain the stray light from the bulb, and not look too bad while doing so. (I'd be happy to do without it altogether since I hate those stupid things, but it's not really legal and the mounting pedestal looks pretty weird there by its lone self. I'd also have to disable the lamp-out warning circuit for it, and that would probably be more work than this was.) I tacked it all together with cyanoacrylate glue, then put in a new bulb. The cover, naturally, won't stay on since its snap-ears are the first thing to go when something breaks, but I used weatherstrip cement to tack it to the housing, and a bit of duct tape to secure it 'til it dries. It worked when installed in the car, and the lamp-out warning was extinguished. This should hold until I can find a better one, and I think I could even open it up without too much damage if I ever do have to replace the bulb again.

...The SRS and ABS lights don't come on with the key, so after work I pulled the OVP relay to check out it and its fuses. There are two fuses on top of this vintage relay, it looks like a triple circuit: one pair (87E & 87L, two contacts each) relayed and another one (30a, two contacts) continuously powered. This is the 9-pole variation in the ETM. The relay is stamped with 091203, and has a Bosch (?) logo and a printed part number 89 7236 000 on one side, and printed legends of 10A, 12V, and "made in Hungary". There is a schematic on the other side, and a pin layout legend on the front. The back has two mounting ears spot-welded to it. I was unable to open it up to check its internal solder joints, but I did buff its contacts, and those of the (intact) fuses. The thin (think paper clip wire) rubber O-ring seal for the fuse hatch fell apart when the hatch was opened, we'll do without it I guess. There was something weird about the socket in the car, it seemed oddly attached to the car, but it was a little too dark for me to see what was going on. I'll know more in the morning, when I reinstall it.

I checked the online NADA blue book, and according to them I paid just about what the car was worth. That's a pleasant change.

Friday, April 3, 2009

Snowing again. Sigh. With any luck it won't be much.

I put back the OVP relay. With light I could see that this relay's electrical socket, unlike what I've seen before in this area, is loose on a pigtail and the relay's mounting ears snap into a retaining clip. I could also see that its two 87L contacts, and one of the 30a contacts, are not used in this car.

I pulled the driver's-side B-pillar cover and re-glued its skin using contact cement. Leaving it open for reference I then took apart the passenger-side B-pillar and swapped mounting hardware from the belt I got Wednesday. With the correct hollow bolt head and the metal spacer it is again possible to slide the belt shoulder height adjuster. Though it's still not quite right it'll do until (if ever) I run across the proper belt. I then put the pillar covers back. I replaced the missing driver's door courtesy light, but that was my last spare. I'll have to get more sometime.

I then swapped the plastic seat belt track bolt-head covers (that I got from that older donor 126) for the missing/broken ones in this car. Though they're black rather than color-matched, and more pokey/square than what belongs there, I think it looks better anyway. Again, at least until/unless I get a better match somewhere else.

On the way to work I thought the cold lockout on the HVAC was broken because the fan started up immediately, but after work I checked further and found that the LOW fan button also overrides the lockout. When on AUTO the HVAC was off until the engine warmed up. Interesting. The blower fan is a bit noisy, sounds like brush noise. On the way home I checked the ABS on the gravel road, it doesn't work. I also checked the ATF level after I got home, and decided that perhaps it was a bit low, so I put in 1/2 quart. We'll see if that makes any difference on its shifting.

...The ruse is over. Daniel threw up in the Chicken Wagon today, and we needed to go to a rehearsal at church. Since the CW's carpet was drying she asked if we could take the white car. "OK," sez I. (My preference would have been to hold off letting her travel in it for another week or so.)

So she gets in. "When did this shift knob get all messed up?" "I dunno," I reply. "Huh." We got all the way to the church, then she noticed the center console storage tray. "I don't remember this." "You wouldn't," I say. "Why not?"

I just couldn't hold off any longer. "Because this isn't the same car." It took a few seconds for that to sink in. I don't think she's entirely happy, imagine that. I'm sure that had I intended to I could have kept the ruse going much longer than this. But the danger is that she'd put diesel in it the first time she took it out.

Oh, and its shifting is unchanged.

Saturday, April 4, 2009

I checked the rear dome light, and the bulb was missing. Easily rectified, and it works as it should. I checked the dead driver's-side fog light and its bulb was there and intact. Turns out it was the ground wire that was unplugged from the socket. Also easily rectified, and it now works as it should.

I then threw all the tools and work clothes in the trunk and went off to the U-Pull to see if I could get a steering box for the Chicken Wagon.

...When I got back, and it had been parked for awhile, I noticed a green puddle of antifreeze under it. Oh-oh! (Probably the water pump, I'll have to check that.)

Costco no longer carries the good heavy rubber floor mats we like, so I stole the ones out of the SDL since we're not driving it.

Sunday, April 5, 2009

I like having a big car. We needed empty paper boxes to store some books in, so I went down to Kinko's and got 27 of them in the trunk and the back seat. I didn't even touch the front seat area, which was reserved for the pizzas I also picked up.

Monday, April 6, 2009

I checked the charging voltage, and it was a little over 14 V, good. It was frosty out so I checked the rear window defroster, and it all works but for one little stripe. Also good. While the car was running I could hear an odd scraping noise. I stopped the car and determined that it was the fan rubbing on the fan shroud. It was already adjusted all the way down (and one retaining ear is broken off and replaced with a bit of sheet metal to extend the reach of the clamp), perhaps the motor mounts are squashed? I fiddled with it until I got it to not scrape anymore, but it's very close.

No sign of antifreeze leaking.

...Cancel that! At lunch time there was a green puddle under the car, and I could see it dripping from the water pump. Time to order a new one!

Tuesday, April 7, 2009

Ordered (from Rusty) a water pump, the available seals for the suspension pump, some of its special oil, and the door switch panel. $170.

Tuesday, April 14, 2009

The pump, oil, and seals came today. Not the switch panel.

Tuesday, April 21, 2009

The switch panel came yesterday, so I installed it this morning. That took a while, there's really no way to get the panel to clip to the handle's bezel unless you remove the bezel too. I had to scrape off more glue to get it to fit properly. Now it looks right, though.

I popped the hood and started digging down in a bit in preparation for the water pump replacement and suspension pump re-sealing. I found torn-off rubber mounts on the air cleaner and the idle control solenoid, so I cleaned them with carburetor cleaner and glued them back on with Shoe Goo. The idle air hose was also cracking badly, so I cleaned and glued it too. It ended up nearly potted in the stuff, but I don't think it leaks now.

All the wires under the hood have hand-numbered masking-tape flags hanging off of them. This suggests that the engine was pulled at some time, presumably not at a dealership.

Wednesday, April 22, 2009

I started on the water pump by removing the fan and shroud, and loosening the power steering and alternator belts. The shroud has two broken-off plastic bits: a locating tab at the bottom and the grooved adjuster tab at the top, both on the same (passenger) side. (This should be repairable, but of course it would be a lot easier if I still had the broken-off pieces.) I was able to remove three of the water pump's bolts, the long one of which was very rusty indicating that it's leaked for awhile, and I got the upper 'thermostat' housing off. (Its gasket is ruined, if there isn't one in the water pump kit I'll need another one.) The two-pin connector shells at the top of this housing, one for the idle air solenoid and the other for a temperature sensor, are completely shattered. I need new ones. The grommet for the dipstick also fell apart.

Saturday, April 25, 2009

I took another stab at the water pump. In fact it does turn out that you must remove (at least partially) the distributor, else you can't get at one of the bolt heads. The last bolt, supposedly accessed through a slot in the harmonic balancer, eludes me. I did get the thermostat housing off easily enough, though.

Monday, April 27, 2009

Another half hour wasted on that water pump. I can't see how to get a wrench on that last stinkin' bolt.

Wednesday, April 29, 2009

Consensus from the mailing list is that it is probably necessary to remove the crank pulley and dampener from the harmonic balancer. (It appears that the water pump was designed to be removed via the slots, but the dampener was enlarged at some point in time which negated this provision. I expect this kind of crap from GM, not DBAG.) Rumor has it that this involves just six Allen bolts, not the big 27mm crank nut. Yesterday I bought a 1/4" 13mm socket, $0.25 at the pawn shop. Unfortunately, it didn't fit either. (And I lost it down behind the pulley and can't seem to fish it out, even with the magnet.) I'm now trying with the 13mm stubby wrench, but I ran out of time to resolve that issue. I did feel down inside the crank pulley, and I think it's hex-head bolts, not Allens, that hold it on.

Thursday, April 30, 2009

The stubby wrench didn't work. I then removed the 6 13mm bolts in the crank pulley. That didn't loosen it yet. So I removed the radiator, which didn't want to come out easily due to the transmission cooler lines. They eventually cracked loose without ripping out of the plastic radiator, but it seemed a close thing. I plugged these holes with four corks and set the radiator aside. I then removed the AC idler pulley, which turns out to be very stiff. The bearing is shot, it's likely that this was the source of the odd whining noise up front. I still can't get the 3-jaw puller in there because of the AC condenser, and the AC system still has some kind of charge in it, possibly R12, so I don't want to drain it. Out of time today.

There is a four-way vacuum splitter at the front firewall with one open leg and nothing nearby that looks like it came from it. Looks like it may be plugged, though, I'll have to look into that. Maybe somebody didn't have a three-way on hand?

Friday, May 1, 2009

Well, it's official: the harmonic balancer has to come off the crankshaft in order to remove the water pump. (I can't tell you how pissed such a design error makes me. I expected better from a top-of-the-line car.) Anyway, to the story: I used the brass hammer to tap on the crank pulley and it popped off fairly easily, it was just stuck a bit. With that out of there, along with all the belts and the water pump pulley, I could then reach through the slot in the balancer to the offending bolt head. By feel the centerline of the bolt is even with the edge of the notch, so there's no way a socket wrench of any sort would have gone on there. Once I bent the dipstick tube out of the way a bit I could then get the stubby 13mm box-end wrench on it. I cracked it loose, and then began a very tedious session of walking that bolt out: one 12-point notch at a time. It never did reach a point where it was loose enough to spin with fingertips. The bolt came free just about the time the bolt head contacted the rear of the balancer. While the water pump is now loose, there's no way to get it out of there, the bolt is too long and the pump is trapped there. (My wrench is trapped on the bolt, too.)

This sucks. I'm at 4.5 hours on this job and I haven't even got the bad pump out yet. A good idea from the mailing list:

Cut the bolt, and replace it with a narrow-head internal-hex (Allen) type that can be removed through the notch in the future?
That'd be good for next time!

Saturday, May 2, 2009

I had a few minutes, so I put the three-jaw puller on the harmonic balancer. It walked right off, releasing at last my lost 13mm socket, the water pump, the bolt, and my stubby 13mm wrench. I found that the offending bolt was 1/4" longer than the others, which might have made the difference between removing the balancer or not. At least with it out of there the suspension pump is going to be very easy to work on.

Monday, May 4, 2009

As a research measure I set the balancer back in place to see if any kind of small-headed Allen bolt is a better fit so that 'next time' the job could be less involved. Verdict? No way.

I then power-washed the area and flushed the engine block.

Saturday, May 9, 2009

Progress! I took a look at the nearly-frozen AC idler bearing, and removed it from the dogleg. I then cleaned it and carefully pried out the (hardened) rubber seal, exposing the dry bearing. A shot of brake cleaner loosened everything up, then I cleaned out the bearing and blew it dry with compressed air. I smeared in bearing grease, packing it down in, then I pushed the seal back into place. It won't seal too well anymore, but it'll extend the life of this considerably. (And I don't need to order anything or wait for it to get here.) It works pretty smoothly now.

I then removed the suspension pump from the engine. That takes a 17mm flare wrench to remove the low-pressure line, and a 17mm socket to remove the banjo bolt on the high. An Allen wrench removes the four long bolts from the face of the pump, liberating it. You need a 13mm socket to loosen the clamp on the low-pressure line, else you don't have enough slack to remove the pump. With the pump out you need to cork the low-pressure line else the suspension oil reservoir will empty onto the ground. I lost quite a bit of oil before I got this done.

With the pump out you can remove the remaining two Allen bolts (the short ones) and pry the lid off the pump. The shaft and cam can then be pushed out from behind with your thumb. I cleaned everything with brake cleaner, it was very grimy. I took pains to keep the four pistons from getting dirty during this. (The pump is a small radial design, similar in configuration to the R4 air conditioning pump that Mercedes [and GM] used to use.) The three old seals (of diverse sorts) can now be removed: scrape off the paper body seal (114 236 00 80), chisel out the large-diameter (but small cross-section) O-ring body seal (010 997 43 45) being careful not to damage the channel or the face, and pry out the shaft seal (004 997 01 47). The O-ring was very hard, I couldn't even tell that it had been an O-ring in the beginning, and was most likely the source of the leak.

I then cleaned everything again and tapped the new shaft seal in gently with a hammer. The shaft may then be lubed and twisted back into place. (You need to gently pry the piston drive ring into place to let the cam go into it while you do this. With the shaft in place you can then pry again to slip the brass bushing between the drive collar and the cam, it doesn't really work to try to install it all in one shot, tolerances are very tight.) Then I put the O-ring in the channel and bolted the cover back on with the two small bolts. The trickiest part is getting the body of the pump installed back on the engine with the drive ears mating with the distributor drive while keeping the new paper body seal in place. (You need to put the low-pressure line back on the pump first, though not tightened down yet, then twist and wiggle until it drops into place.) That's not too difficult, though. I then bolted everything back down and reinstalled and tightened the hoses and their braces, then sprayed everything off again with cleaner. Done.

The large-diameter O-ring keeps suspension oil from leaking out of the head of the pump. The shaft seal keeps it from leaking into the engine crankcase, and the paper seal keeps the engine oil (and any vagrant suspension oil) from leaking out behind the body of the pump.

...In another session in the evening I scraped off the gasket surfaces and installed the water pump. That took a long time, due to the tenacity of the old gasket. I tried to be careful with the razor blade not to damage the metal surfaces. Once done I transferred the thermostat to the new pump, but used the new O-ring seal that came with the pump. (I made sure to install the jiggle valve up.) The two slightly-longer pump mounting bolts must go in where they came out, at the bottom and bottom-right of the water pump where the thicker bosses on the pump are else they'll bottom out in the holes and not clamp. I wire-brushed the rust off of the one very long bolt that goes through the body before reinstalling it. The new gasket had a small tear most of the way through at one point, that was very distressing to find. At least it was at the top and not the bottom, so any leak will be very visible. I used Permatex anaerobic sealer to goop the torn area before reassembly, it should be fine. I got the pump and thermostat housings assembled, and the radiator feed fitting partially installed before I had to quit again.

This job is turning out to be very slow!

Sunday, May 10, 2009

I reinstalled the pulleys and belts. I just had to be careful to put it all back in the right order, else things get blocked. The balancer and main pulley went back on at the 90° mark where I took them off; there was also a pair of white marks on the balancer and the pulley to align. (All six bolts went in with no trouble, so obviously I got it right the first time. I used a mid-sized Allen bit to index the dampener and pulley to the holes.) I tensioned the belts and locked down all the adjusters. I bent the dipstick tube back into position, and cut a section out of a salvaged oil filter grommet in order to slip into the tube's clamp to replace the shattered original. It looks almost like it's the real thing, and should protect the tube equally well from wear due to vibration. I reinstalled the idle air valve, but my glue job on the mount didn't hold so I pulled it off and potted it again, more heavily. The rubber lining of the clamp was hard and shattered away, so I cut some bicycle inner tube to serve as a replacement. Since I had the glue out I cut a piece of black plastic to serve as a new bottom locating tab for the fan shroud, which I then glued on. About all that's left is to reinstall the radiator, but the glue needs to dry first and it was time for breakfast anyway.

...Later I went back to it, and got the radiator installed. I washed out the fins on both it and the condenser with the hose, they were both pretty clean (not like some I've seen). I left off the fan and shroud, since the glue was still drying. I bolted the fan pulley on and started the car. It started right up. I moved it just to show Jill that progress was being made. (Sort of a Mother's Day present.)

Monday, May 11, 2009

I tried to install the now-dried fan shroud, but found that the fan now rubs on the bottom if I do. (Extra fun is that you have to unhook the upper radiator hose to slip in the shroud, but all I lost was water since I'm still at the flush stage.) Great, it's probably collapsed motor mounts, though there is no sign of that on-the-rails sound I've heard before. I put the fan back without the shroud for now. I then started the car, the little knock was still there. Not sure whether it was water pump or suspension pump, I then poured my quart of fresh suspension fluid into the reservoir, which brought it back up to within the marks on its dipstick, and took the car for a test drive. It acted just as it had before (good, I guess), and when I got back the little knock was gone. I installed the air cleaner and dropped the hood. Sometime I'll check the timing, but it seems to be running good enough for now. The rough idle is reduced, that was probably at least partially the leaking air pipes on the idle air solenoid.

...I drove the car to work, etc. It worked fine. No sign of leaks, though the new water-clear suspension oil turned all dark. Needed more flushing, I guess! I stopped and bought a jug of Zerex G-05 antifreeze. I'll put that in after another flush cycle or two over the next few days to get out all the green.

Tuesday, May 12, 2009

I drained the coolant, it had gotten pretty green yesterday. (From the heater core, no doubt. Unfortunately the connections to it are not particularly accessible, so I wasn't able to flush it properly with the hose while I was doing the rest of the system.) I flushed it out with water, then refilled it—also with water.

...In the evening we took the car to a concert. The low-oil light started coming on, and we could smell burning oil when we got out. Some kind of leak thing going on?

Wednesday, May 13, 2009

I drained the radiator again, still a bit green. One or two more, I think. I then jacked up the car and drained the ATF, which looked a little cloudy, though not much. That took a long time to do, especially through the torque converter drain plug, and the pesky wind blew oil all over the place. (I finally got a scrap piece of plywood to shield the area, which helped.) I then refilled the transmission and the radiator with their vital fluids. I also vacuumed out the leaves and such from the firewall corners. That is easiest done with the hood all the way up and the springs removed.

I checked, and the engine oil level was fine. The level sensor must be lying, I may well need a new one.

...While driving to work today the brake boost failed suddenly. When I got to work I popped the hood, and found that the fitting on the check valve had snapped off, making for a rather large vacuum leak!

The ATF change made no difference in the car's shifting characteristics.

...When I got home after work I dumped the coolant, it looked pretty clear so it's time to use the Zerex. I removed the brake vacuum line and cleaned it with brake cleaner. I tacked the fitting back on with cyanoacrylate glue, then potted the whole thing in Shoe Goo. It should be ready to use by morning. The rubber boot through the mid firewall is torn, I'll glue that too once the potting sets up a bit.

...After a couple of hours I turned it over, cleaned, and potted the tear in the rubber boot.

Thursday, May 14, 2009

I reinstalled the vacuum hose. Unfortunately, in spite of my best guess last night I'd managed to glue it on backwards, with the slight curve pointing the wrong way so the fittings didn't line up. I pulled on it and the Shoe Goo stretched and bent, so I installed it that way, but there's a big gap in the joint that's webbed over with glue, we'll see if that holds.

While in the area, at the suggestion of a lister, I loosened the pull of the shift cable by about 1/8". We'll see if that makes any positive difference. The thing looked unmolested and otherwise as it should, so I don't hold out much hope for this. I thought that a maladjusted shift cable resulted in skewed shifts across the board, not just a problem with 1→2.

I also put in the Zerex G-05 and topped it off with water. So's not to wash away any coolant I was gentle with the refill, I may have not gotten it all the way full. So I filled the empty jug with water and put it in the trunk for topping off purposes.

...No, I lost the brake boost again on the way to work. The webbed glue holed, I'll have to re-do the job properly when I get home. I also note that the tranny cable adjustment has made it a little more palatable for regular driving, but if you romp on it at all it'll still go up and bounce off the rev limiter unless you back off the throttle to let it shift.

...When I got home I loosened the engine-side fitting and spun the hose around to match the bend of the other hose, thus closing up the crack, then I put a wad of glue over it. After it set up some I smeared a wad around the bottom too, and connected the hose to hold it in its final position, but loosely so as to minimize stress on the glue joint.

Friday, May 15, 2009

I connected up the vacuum hose, and topped off the coolant supply. Jill needed to drive it today, because the 190D lost its clutch hydraulics. She reported that the brakes only worked for a short while before they lost boost again. Nuts.

The Shoe Goo is just too soft for underhood use like this, plus I wasn't ever waiting for a full cure. Today at the U-Pull I nabbed some items from their latest 126 organ donor: a good shifter knob, a stiffer rear-view mirror, a trunk carpet, a clip to replace the missing fan shroud clip, a warning triangle, and a brake vacuum hose. I also got some dirty and bent grille trim strips from the car's broken grille. When I got home I tried out the new hose, but it was about 1" too short! Nuts. I pulled the failing glue off the original and tacked it back together with cyanoacrylate glue, this time making sure it was oriented the right way. I mixed up some 5-minute epoxy and coated it with that instead of the Shoe Goo. It wanted to run, so I kept it spinning slowly by hand until it started to firm up, then set it aside to dry.

I also got a factory sparkplug wrench (that'll probably go into Ethelred since it unfortunately has need), and a factory lug wrench which I can use in this car. I got the spark wires too, which I'll probably try in place of the existing ones to try to see if there's a problem there that is responsible for the intermittently rough idle.

Saturday, May 16, 2009

I reinstalled the now-dry brake vacuum line, it looks good. And the epoxy is nice and strong. Finally done with that?

I got out the warning triangle I got yesterday and wire-brushed off the rust. Then I painted the metal again, mostly I used a brush since I had to avoid messing up the 'printing' on the face or the plastic reflector surfaces. While that dried I glued the retaining tab on the triangle's mounting clamp that I had to break yesterday in order to get it out of the car. These were set aside to dry. I then removed the console surround, switches, etc., and removed the shifter knob. That's when I found that the new one was subtly different, and not likely to end up pointing right if I were to install it. I tried hand-sanding the scabrous top of the old one in order to clean it up for painting, that's when I found that it was actually leather-wrapped. (I think the original leather surface was ruined by hand lotion and/or DEET insect repellant.) I ended up pulling the top cap of leather completely off, exposing a pretty nice plastic surface. I lightly sanded it and then painted it (and the remaining leather) with black vinyl paint. It doesn't look too bad now. I cleaned up the PRNDS2 window and the rubber boot, then reassembled the shifter once it was all dry. That took a bit of fiddling.

The coin tray was really chewed at the bottom, through the color and into the substrate, so I mixed up a little paint to get a vaguely close color (that didn't really work) and brush painted the bottom. I then put the console back together, replacing the one missing ashtray screw. I left the Becker BE 1480, serial A 9532117, out as I need to get its security code input in order for it to work again. I then attached the now-dry (enough) warning triangle to the trunk lid.

I also replaced the passenger-side courtesy light fixture, since its mounting ear was broken off and it wouldn't stay in place. And I installed the new trunk carpet, and threw the lug wrench I got yesterday into the trunk after I wire-brushed off the rust. Then I replaced the rear-view mirror (again) with the better (stiffer) one I got yesterday. Even at 2× the price ($4) it is a good deal.

Not quite done for the day, I tried to install the $2 worth of spark plug wires I got yesterday, and found that they didn't fit. The distributor end sockets were too small. (This discovered only after I reworked one pulled-off socket to get it back together again.) Too bad, I had been hoping to diagnose the rough idle as being due to old spark plug wiring. There is a mess of glue on the driver's side valve cover where the wires are, not sure just why this would have been done but it's highly suspicious.

I then got out the salvaged grille trim strips from yesterday and had a look. Two were the right length for the missing pieces, and in about the same condition except for some mild bends, but most of the mounting tabs molded into the grille itself were broken off. So I used screwdrivers and my hands to straighten the strips, then glued them into place. Twist-ties served to hold them in place until the glue dried. They look pretty good now. Consistent with the rest, anyway.

Sunday, May 17, 2009

Jill got home today and said the brakes had again gone out. I opened the hood, and the epoxy joint had cracked. (The engine heat back there is something fierce.) While I could try again with JB Weld, a much tougher epoxy, I'd had enough. I got out the heat gun and removed the valve-bearing tecalan hose from the 'new' too-short assembly and put it on in place of the broken one. (Thus keeping the longer booster-side end so that the hybrid would fit.) I also swapped firewall grommets, since the replacement one was better. That only took a few minutes to do, but I was hesitant to do this before because it's really easy to ruin the tecalan if you're not careful with the heating. (If the glue route wasn't going to work, however, that removed the disincentive.) That should cure the problem, let's hope.

Monday, May 18, 2009

Jill reported that the LR window won't go back up. And also that she's unhappy with the lack of AC. (Probably needs a charge. However the brakes were still working fine.) Crap, this was supposed to be the nice car. She switched to driving the truck. Wimp.

Tuesday, May 19, 2009

Jill lost the only key, claiming that she put it in the proverbial 'safe place' for me. (We both suspect Daniel's influence here.) That slowed down repairs more than a little. I pulled the switch panel out of the door again (so easy to take out, so hard to put back in) and used the battery charger to apply power to the motor leads. (Black and green solid colors.) I could hear the motor running freely. I ran it back and forth, and finally got the window to pop up a bit. I could hear the gear slipping on its sector. The glass was also freely movable once I could grab it. I'm guessing the slider has broken off, but from the sound of it the gear's also chewed. I'll see if the junkyard car has one of these left in it. I got the window all the way up, which was good since it was then raining.

She'd also left another window down some, a front one, so I pulled open the console and used the battery charger to run that one up too.

I checked, and I have enough juice to charge the AC. Can't, of course, without the key.

...At lunch I bought a window motor/regulator at the U-Pull. $17, that's a profit center piece obviously. The 'new' regulator is bent, as nearly all are. Junk pot-metal design. The nylon slider is also broken, though it's all there. That's not so good. Maybe with this I'll have enough pieces to throw together something that will work. I should order a new slider, but that'll take time.

Wednesday, May 20, 2009

I opened up the offending door panel. Surprisingly, the vapor barrier was still there. I pulled out the window regulator, and found to my surprise that it's in very good shape. Only the slider has broken. I think I need to just order a new slider, and return the window regulator I don't need.

So I called Rusty and ordered two sliders, so that I'd have a spare for next time one of those POS's breaks.

...At lunch I returned the unneeded window motor/regulator to the U-Pull and got my $17 back. (But not the $2 entrance fee, of course, nor my lunch break.) My fault for jumping the gun and buying parts in advance of diagnosis.

Saturday, May 23, 2009

It was warm today, so I checked out the AC. Cold pressures were reasonable for a charged system, and the compressor engaged when told. Low-side pressures dropped too low while operating, which would indicate an undercharged situation, so I began to put in some secret sauce. Low-side pressure rose and stayed high, and wouldn't act normally, so I bailed out. Later I started to wonder if the low-side fitting self-closed due to a poor mate to the service fitting? I had that happen once on the Chicken Wagon. I'll need to look into that.

Sunday, May 24, 2009

I measured the diameter of the car's low-side fitting's barrel: 0.358", which is even larger than the 0.350" one that was a problem on the Chicken Wagon! Time to get out the file, I guess. (This is making me start to wonder about the 'quality' of the Robinair hose set on my Snap-On gauges. They're obviously not cheapies, yet sometimes they don't fit.) I measured the parking spot on the gauge set, and it's 0.335", which is what I expected. Before filing I checked my toolbox and found a (new, unopened) spare Imperial Eastman high-side hose, but it worked as a low-side hose and allowed the system to be charged. I put in one can of test refrigerant, and topped it off with R290 until the system started cycling even with water slopped on the condensor. I took it for a test drive, and vent temperatures were about 48 °F—not great, but not bad either. About what I usually get unless I'm particularly lucky. (It was about 80 °F outside, hardly a stressful situation.). During the charging the center vents lost most airflow, and the defroster flaps opened. Vacuum problem? More fun I guess, we'll just have to see how it behaves in time. When I removed the gauge set I found what appeared to be red dye in the system, so obviously somebody has been chasing a suspected leak.

The center brake light fell apart on the test drive, the glue let loose in the oven heat of the closed car. The weatherstrip cement I used is apparently not that good in high temperature environments, or perhaps I didn't use enough. Anyway, I had recently found that I had another, mostly intact brake light assembly in a parts box, so I used that instead of frankenstein's monster that I'd pieced together earlier. (The rear cap retaining snaps were gone, of course, but otherwise it was in good shape.) I used more weatherstrip glue this time to hold the end cap on, and set it aside to dry.

Wednesday, May 27, 2009

The new window slider(s) came yesterday, PN 126 720 01 42, so today I installed one: grind off the old retaining rivet, and hammer a new one on with the BFH and an anvil. I used the old rivet as a spacer to the anvil so that I wouldn't break the new plastic. That part was fun, but putting it all back together thereafter was tedious. Tedious enough that I didn't quite get it all done in the time I had. I did get the door panel hooked on, which is the difficult part. (I hate trying to get all six plastic clips lined up at the same time as you catch the upper part in the window opening's rubber wiper, and without breaking anything.) The window is working again, and I greased the track too. I just have to install the handle, and the switches and trim.

I looked at the radio's wiring harness and labeled the radio's contacts with a Sharpie. (This so I can connect power to it on the bench. It needs 24 hours of power to snap out of its code-wait state.) I found a spare Becker plug in the parts pile, so it was even easy to hook up on the bench, which I did. Now it says to WAIT. Well OK then, see you tomorrow perhaps.

...Today I surfed and got some radio serial number decoder applications, and after work I threw them at Virtual PC. The Becker 4-digit decoder becker4digit.exe suggested the code was 4140. The becker.exe program suggested 34141, as did becker2.exe. All of these crapplications only accepted the last four digits of the radio's serial number: 2117. The becker9preset.exe suggested 24141, and also would only accept four digits of the serial number. (The most likely code is the first one.) Our office computer cluster[f**k] claimed there were viruses in becker.exe and becker4digit.exe, but I ran them anyway since they're locked in a VPC box that I don't care much about.

I also finished putting the car back together except, of course, for the radio. That didn't take too long.

Thursday, May 28, 2009

Today what should greet me on the bench but CODE! No more WAIT. Feeling brave I then tried my best guess from yesterday's foray into PC-hell: 4140. It worked, the radio then switched to an FM station. I wonder if it'll work in the car now? I used a Sharpie to write the code on the case for next time. (I'm not really worried about the theft-ability of a pushing-20-year-old factory cassette deck.)

I then put the radio in the car, which was a lot of fun since there are so many wires to hook up and wad behind it. It CODE-ed again, but that's no longer a problem. The radio worked, even without an operable antenna. The front/rear fader is scratchy and noisy, and cuts out the right channel at the least excuse. Obviously it needs a good cleaning. The rear speakers make almost no noise at all except for a scratchy little whine, they're probably sun-rotted and blown. The door speakers work, as do the dash speakers. Success! I programmed the local FM stations into the presets.

...This evening we drove the car to an event. It worked well, and the radio was nice, as was the AC. Coming home at night I shut off the AC and radio and opened the sunroof. Nice.

Friday, May 29, 2009

We took the car to another event. AC worked well going in, and sunroof coming back. When we got home it was full dark, so I popped the hood while it idled and tried to look for arcs. I didn't see anything but that's not definitive. I'd really need to take off the air cleaner for better visibility. The rough running, mostly when idling, is still intermittently there. As is the oil burning off the exhaust.

Monday, June 1, 2009

I plugged in the antenna that I'd had hanging in the hole, and it whirred. Unfortunately, because it wasn't mechanically secured the antenna's swinging weight had ruined the grommet, although it hadn't been in perfect condition when I put it in. I'll need to get a new one. Anyway, I bent the bracket that was on the antenna so that it went over to the mounting hole and screwed it down. Good enough, I'd say. The antenna would extend a bit, but the end segment of the mast was strangely bent, sort of corkscrew-y. I used the BFH and the anvil to gently tap the bends out of it, then I used Kroil to loosen the very sticky mast sections, especially the bottom one that wouldn't move at all originally. A lot of sluicing and working later it was all fairly free, then I used teflon spray lube on it and installed it back into the body. It works, at least good enough for now. (It really needs a new mast, but this'll do for awhile.) AM reception was good.

In celebration I got out the touch-up paint and covered the worst spots I could find on a quick walkaround.

Saturday, June 6, 2009

Jill complained that she couldn't find the center rear seat belt, and so had to take the truck to ferry schoolchildren around. I pulled out the rear seat bottom and found the belts wadded well underneath, so I brought them out. (I also found business cards and receipts from Reno, Nevada under there. No money, though.)

Tuesday, June 9, 2009

I checked the fluids today, and found the oil just fine but the coolant a bit low. I'm hoping it's still just air burping out from the water pump change. I topped it off with water, regardless. One sad thing: one of the air feed ducts had popped out of place and was caught up in the belts and half chewed away! I'm a little surprised that Jill didn't notice the noise...

Wednesday, June 10, 2009

I removed the damaged air intake duct (P/N 117 094 19 82) and patched it with pop cans and duct tape. Black paint masked its essential patchiness. Quality! I also made another trip around the car with the touch-up paint, it's amazing how much you miss in any given pass. The coolant, now that it was cold, was still a bit low so I added some more water. At this point the level should be stable, when checked cold. I see no signs of leaks.

Thursday, June 11, 2009

The coolant is down a little again. There must be a leak somewhere, yet I can't see one.

Tuesday, June 16, 2009

I found an extra 560 SEL owner's manual this morning that I wedged into the console box. 1987 is a bit old, but it's better than nothing.

Saturday, June 20, 2009

On the way to a party this evening the cover fell off of the third brake light again. That unshielded light is bright at night! I'm trying to tread a fine line between gluing it together securely and yet not permanently. Not easy.

Sunday, June 21, 2009

Screw glue. I took the light out and screwed it together with some small wooden strips as brackets. (They were the broken pieces of the Holton trombone case slide retaining bar, so the wood's nearly 100 years old. I spotted them on the bench and they were blonde enough to not clash horribly with the beige plastic, and easier to work than metal.) I pre-drilled the holes first, the very brittle plastic will not take much abuse. I then used Vaseline to tackle some of the creaking door edge areas, I had pretty good luck with that in the SDL, un-doing the effects of a bad detailing. (Vaseline: the anti-Armor-All.) We'll see if it helps.

The ashtray in the LR door rattles horribly on the road, so I took it out and tacked its loose metal trim piece down with cyanoacrylate glue. We'll see if that improves anything too.

Wednesday, June 24, 2009

I checked the coolant level and it was down a touch, so I topped it off again. It seems to me that the suspension oil level is dropping too, and that the engine oil level might be rising. How nice. I may have damaged the shaft seal of the suspension pump on installation.

I pulled out the driver's under-dash panel, which was difficult as the plastic trims covering the screw heads were very sticky, they were close to breaking when they finally popped out. (These pry out starting from the outsides! That is, the extreme left and right edges when seated. If you pry from the wrong edge you'll break off the piece's retaining hook.) I'll need to lube those with teflon spray before reinstallation so that they don't break in future. The ABS plastic footrest, 126 688 11 06, was all broken up so I pulled it out (it's part of the outside carpet side panel) for gluing. (There's a hook on the side panel part, it pulls toward the rear of the car, and then away from the side wall and out. I broke it further figuring that out.) With the carpets out I vacuumed, there was a lot of dirt under there. Anyway, with that all out of the way I could then pull the cruise control amplifier, which shares a bracket with the Hella 004 545 07 32 8-pin warning module, also removed. (Disabling the interior courtesy lights as well.) It's all held in with only one 10mm nut.

It's your typical VDO 14-pin servo amplifier package, with customization plug. The ink-stamped (date?) code of 518 20/90 implies that it's the original unit. Scrawled on it in red grease pencil is a big 218 (maybe). Stamped into the case metal is:

20/90
      12V
  412 212/1/1
* Mercedes-Benz
005 545 05 32
The customization plug is labeled 19 90, a date code, along with 005 545 07 32 and VDO 519201/1/01.

I opened up the amplifier and found a change: instead of the usual digital or analog discrete circuitry there was a 40-pin DIP, possibly a microprocessor of some sort. (It could also be an ASIC. There's still plenty of discrete circuitry to go wrong though, including an LM2901 quad comparitor and several transistors, including an H-bridge for the servomotor.) The big DIP was labeled:

ITT
V 8001-501
Germany
It also had 32 and 0045: labels on it, sideways to the main markings. The board was (as is usual) conformally coated. It was hard to tell for sure through the coating, but many of the solder joints looked suspect. The board, while double-sided, has traces only on one side; the component side is a shielding ground plane. Zero-ohm resistors are used where necessary to route signals on the component side, I counted eleven. I ran out of time to proceed further today.

...This evening we drove to dinner in this car, my first time in it since the noise treatment, and I could tell that all the odd creaking was gone. Yay, Vaseline! The noisy ashtray handle was also quiet. Makes quite a difference in driving enjoyment.

Thursday, June 25, 2009

Paint stripper time. (The secret to resoldering cruise control amplifiers.) That went well enough, then I resoldered the board. There are less components in this variation so it actually went fairly quickly. I didn't really see any connections that I'd call very bad, but some did look marginal. I then plugged it in the car and tried it out.

Oops. There was a surge when I turned it on, then it seemed to act weird. Then I smelled magic smoke. I stopped the car and opened up the case, and smoke poured out. One of the motor drive transistors fried, ruining one of the PCB mounting pads. That's not good. I pulled out the coupled TO-126 pair, and found both transistors completely shorted. One is a BD-438, the other (unknown) was cooked into slag. The other similar physically-coupled pair on the board are an NPN-PNP complementary pair, I didn't pull them out to check the markings but I expect them to be the other leg of the H-bridge and exactly the same. The BD-438 is a PNP 4 A 45 V power transistor. The slagger is probably the complementary NPN device, BD-437. I replaced the BD-438 with a 2N4918, and the other one with a 2N5190, both from the junk box. These are not exact matches, but perhaps they will work. I had them on hand, anyway. I used heat-sink grease on them to help couple heat to the little metal clip. The PCB pad, though fried, still made enough contact to the Emitter of the NPN that I didn't have to use a jumper wire. The Fluke's diode test range showed the two devices acting appropriately in-circuit.

Obviously, however, a bit more care is called for in testing this. I need to resurrect the bench test harness, and fire it up with a current limiter first. These H-drive circuits are highly susceptible to frying if anything bad happens to the inverting base drives. Bad solder could certainly do this, so I resoldered this circuitry again.

Friday, June 26, 2009

I dug out the bench rig and decided that it was long past time that I hook up a 'brake switch', so I got a NC microswitch from the junk box and screwed it to the stalk switch assembly, then wired it into the harness. Much easier to 'apply the brakes' during testing that way rather than messing with alligator clips, etc. (The brake switch removes a virtual ground from the correct line to the amplifier, hence the use of a NC momentary switch to ground.)

On the bench the amplifier drew approximately 400 mA on average while driving the motor, and seemed to work correctly. No smoke, no excess heat. I'll need to check that there isn't anything in the car's wiring harness that'll cause a problem, but so far it's looking good.

The 'processor' takes a 4.19430 MHz (222 Hz) crystal, driven by pin 29 of the part and fed back in on pin 28. Probing around shows that the processor uses a 5 V supply, I think via a Zener diode somewhere on the board; there is no sign of a regulator. A strategically-located bypass capacitor implies that it takes 5 V power on pin 1, and ground on pin 21. Perhaps this can be of aid sometime in identifying the part, not that this would be of any use in finding a replacement since it's probably a masked ROM device. (If it's actually an ASIC there's equally little chance of ever getting a replacement.) With that pinout it's not an 8051 processor, I know that. While poking around on the board I did find a case-split 1N4005 diode, which I replaced with a brand-new identical part from my parts bin. (That's kind of unusual for me. The really odd thing was that the split part seemed to still be working.) The diode was probably ruined by excess current going through the H-bridge.

I opened up the customization module and found five resistors inside, one of them a zero-ohm job. Roughly what I would have expected.

I checked the wiring harness connections to the servomotor to make sure there was no power or ground fault, and it passed so I took it for a test drive. It worked perfectly, and held my 35 MPH set speed up hill and down. (Downhill it sped up some, but that's because of the sloppiness inherent in the torque converter.) I then hammered the aluminum case ears back down and reinstalled it in the car. I was short on time so I left the panel work for later. (Plus I have some gluing to do on the footrest.)

To get the gluing started I cleaned off a couple of the breaks and then tacked them together with cyanoacrylate glue, then bolstered one of the more fragile breaks (the floor mounting ear) with a piece of sheet metal and Shoe Goo.

...When I got home from work I did some more cleaning and gluing. I got the panel/footrest all glued together with cyanoacrylate glue, and I got some more Shoe Goo laid over some of the non-critical cracks. I'll use sheet-metal backing plates for the higher-stressed areas.

...After dinner I did some more cleaning and Shoe-Gooing. Two more sheet-metal backing plates across some stress breaks.

...And before bed I did one last cleaning and Shoe-Gooing. I found some more sheet metal (leftovers from one of the Frankenheap's preheater attempts) and made backing plates for the rest of the stress breaks. That used up just about all of that tube of Shoe Goo, so I guess I'd better be done. Tomorrow (or better yet, the next day) I could reinstall this thing.

Saturday, June 27, 2009

The footrest panel is shaping up well, but I wanted to do just a bit more to clean it up. I hammered the sharp edges of the one big backing plate down around the part's profile and glued all around it. I also touched up a few of the other places that looked like they could use some more strength. Now I really am out of Goo!

Then I went out and removed the passenger-side under-dash panel, it was time to take a stab at the noisy aspirator motor. (The screw-hiding trim panel pries out from the outside edge [extreme right] first! If you pry from the wrong edge you'll break off the piece's retaining hook.) The panel came off easily enough, but the knee bolster was a bit recalcitrant. Eventually I figured out the problem, it was just caught on something. The passenger airbag is held in with one long bolt through a plastic-lined recess in the bolster, and comes out very easily. I didn't really need to take it out, however, but I didn't know that until I'd already done it. (The airbag bolt can be removed even with all the trim and panels in place.) One of the plastic ears on the air outlet that goes to the door was broken off so I cleaned it off and tacked it back on with cyanoacrylate glue, then I used pliers and a small screwdriver to dig enough Shoe Goo out of the 'empty' tube to glue it back, along with a small piece of reinforcing metal. I also used weatherstrip cement to reattach the foam collar (for the air outlet) to the knee bolster.

The aspirator motor (000 830 96 08) didn't want to come out very easily, it was wedged into a soft foam block. Eventually I got it out and lubricated it. (It wasn't easy to get open, and I don't know how successful the lubrication attempt really was.) The cover for the main blower was loose, one of the screws had fallen out. (It seemed to be the wrong size anyway.) I dumped the leaves and dirt out of the porcupine (blower speed regulator) that's in the air path, then I removed the blower motor to see if it could be serviced.

It looked OK, so I dripped a little oil into the bearings. Putting it back was interesting, it seems that it had been taken apart before and not put together correctly: the plastic was a little deformed and things didn't want to slot into their correct channels. (The blower housing fits very snugly, there are a lot of tongue and lip joints to mate.) Perhaps this is a replacement motor, installed carelessly? With a bit of fiddling I got the motor and the cover back on correctly and found that part of its problem was that a retaining clip for the rear corner was missing. I fabricated a new one out of some springy metal banding. That took awhile, but should help keep the housing airtight and quiet. I put the aspirator motor back in. When I fired everything up the aspirator was noisier than it should be, but I hope that the intermittent shrieking is gone. I really should get a new aspirator, but I hate to if it's not completely necessary. We'll see how it goes, now that I've R&R'd it once it would be easy to do again: you only have to remove the underneath panel and the knee bolster.

I checked under the floorboard and the airbag system is plugged in, so if it's non-functional that's not the reason. While I was there I vacuumed. I then put back the knee bolster, but I left out the rest until the glue can dry on the air outlet.

...In the afternoon I got impatient and put the car back together. I could have waited longer for the glue to dry but I think it'll be OK. We won't be driving it today so that'll keep most of the worst stress off of it anyway. I used spray teflon lube on the clips for the plastic trim strips that cover the screw heads. That should help them to come out next time. (Half of one center clip on the long passenger-side piece is missing, but so far hasn't seemed to cause any bowing.)

I made a small mistake and overtightened one of the hood release screws and cracked the tip off of the plastic body. Oops. I glued it back on with cyanoacrylate glue, we'll see if it stays together. (It's only cosmetic.)

While looking in the trunk for the panel mounting screws what should I find but two radio code cards! That would certainly have simplified things last month...

I checked again, and the coolant level is down a little more as is the suspension oil level. Engine oil level is up. No sign of any external leaks, however. Not good. I can blame the oil levels on a botched shaft seal on the suspension pump, but where's the coolant going?

Sunday, June 28, 2009

I jacked up the front of the car and tried to have a look at the oil level sender. I couldn't find it! Since I had the car up I cleaned and tightened up the transmission oil cooler line mount that was loose. I used some inner-tube rubber to cushion the clamp again, it was wearing into the line. The bolt was nearly all the way out. I then put the front license plate on, and then pulled out the ABS sensors and cleaned them. They were pretty dirty, let's see if this helps anything. There is a pretty significant oil leak at the input shaft of the steering box, that's making a mess. Something at the rear of the transmission is leaking pretty well too, that's the source of the oil that's smoking on the exhaust system.

After breakfast the sun was up enough to shine down into the engine compartment, and then I could see the sender: It's to the rear of the oil filter housing, and hard to reach behind an engine shock absorber. I pulled the connector off the sender with pliers and it popped right off the wire when I did so. It might have been that the wire was merely broken, so I took it apart to fix it. Unfortunately the connector shell (014 545 07 28) broke apart too, and its rubber boot (008 997 07 81) tore. Criminy. I checked the sender itself and it was grounded, which is as it should be. (The light comes on when it's open-circuited.)

I scraped and cleaned the area, then resoldered the connector back on. I did a pretty crappy job, but it's hard to do on your back underneath a car! I used some cyanoacrylate glue to patch the shell, and dregs of Shoe Goo dug out of the tube to patch the rubber cover. It'll have to do, and it did seem to seat securely back on the sender. When I tried the key the low-oil light was out, so perhaps this has cured the problem.

Monday, June 29, 2009

In light of the power steering leak I checked the level. Not bad, but room for some topping off.

Tuesday, June 30, 2009

I bought more Shoe Goo today and wiped off and potted the cracks in the lower ball joint boots. That should help extend their life.

Thursday, July 2, 2009

I prepped the car for our cross-State road trip. Tires aired, including spare, fluids and belts checked, etc. I'm carrying a gallon of water and a quart of ATF in the trunk, just in case, along with some tools. (The toolkit I've been carrying in the 380 SL, in fact.) The travel cooler is in the back seat and plugged into one of the door ashtrays. (One of the nicer convenience features of the 126.)

Sunday, July 5, 2009

Just got back after putting on around 1000 miles, and the car acquitted itself well. The AC worked great the whole trip, which at times touched triple digits and was usually well over 80 °F. It was very nice down at the beach where we beat the heat. The car did burn off a bunch of ATF on the exhaust pipe, but I think I had it overfilled. (Very smoky after long freeway runs, scarily so a time or two.) I kept an eye on the fluids and all levels were otherwise fine. Fuel economy was above what we'd been getting around town, and about what was expected for this car. Not great, but we still had a comfortable 400 mile range.

The cruise control worked flawlessly. The radio was fine, but at times would emit an intermittent very loud BRRRRR-AAAPPPPP sound that wasn't source-related, nor did it respond to the volume control. Post-preamp problem in the head unit? Rear-mounted amplifiers? Regardless, Jill wants a CD player so it'll get swapped out sometime.

Saturday, July 18, 2009

Jill's been complaining of the sporadic AC venting, so today I tore into the console. I followed my electrical checklist and determineed that at least three of the seven electro-pneumatic valves in the integrated switchover valve block were electrically open. Great. A new valve block (126 800 09 78) is some $160, but there was a 1990 300 SEL at the U-Pull today so off I went to see if I could get lucky. I met with marginal success: while I did get the valve block it also was broken! I bought it anyway because I think there's room in there to be able to mix-and-match, using both valve blocks to get seven good valves. More work, but much cheaper considering the valve block (and its mating connector 201 545 39 28) only cost $3. ($5 with admission.) I also bought a proper passenger seat belt ($3) and a blower motor/porcupine ($4, for the spares pile), and some other items, mostly not for this car. (The total bill was $34.)

I wonder if the single molded valve block traps too much heat around the coils for reliable long-term service? I've never seen a bad individual switchover valve. Also possible are internal soldering problems, since it looks as if the thing is built with a PCB inside, and banging on one can open/close some of the bad connections. If I had a third broken unit I'd cut into one to see what was up, but as I'll need two in order to accomplish my plan I'd better not risk damaging one of these further.

While I was at it I disconnected the amplifier connection to the radio. I told Jill to drive with it on (but of course non-functional) for sufficient time to prove whether or not the intermittent nasty noise was coming from the head unit (now isolated) or the amplifiers.

Sunday, July 19, 2009

I traced out the switchover valve block's connections (facing the little pins on the valve block):
Valve block
o8 7o
o6 5o]
o4 3o]
o2 1o
      
Valve
8Common 7Short DEF Flap
6Diverter Flap 5Long DEF Flap
4Center Flap 3Leg Flap
2Long Fresh Flap 1Short Fresh Flap
      
Wire Color/Tracer
8Red/Black 7White/Black
6White/Violet 5White/Red
4White/Green 3White/Yellow
2White/Gray 1White/Blue
      
Hose Color/Tracer
8Red/Green; 7Red/Blue
6Green 5Red/White
4Red/Black 3Red/Yellow
2Green/Blue 1Brown

Pins 4, 5, 6 & 7 (Center, Diverter and both Defrosts) were open and/or intermittent on the original valve block. Pins 1 & 5 (Short Fresh and Long Defrost) were open on the junkyard unit. If I install the junkyard unit, and flange up valves 2 & 3 from the original in place of 1 & 5, that should get it functioning again with the minimum amount of work. (I picked 2 & 3 specifically because they were both good in both valve blocks, possibly indicative of light use and thus the most likely to last.)

So that's what I did. There was plenty of room to lay the second valve block near the first one so that I didn't need to extend any lines. Careful reassignment of rubber bits from both valve blocks is all that was necessary. That, and a large rubber 'Y' fitting that I also grabbed from the donor car. I teed into the electrical lines and soldered the extra connector onto the required lines going to the original connector, and I corked off the now-unused valves in case they should try to actuate due to vibration, or general cussedness. I got sidetracked at about that time and didn't get a chance to test it, or to button things back up.

Monday, July 20, 2009

I put the control panel back in place and started the car. I could hear a vacuum leak, which turned out to be the Y connector, it just didn't fit tightly enough given the contortions it needed to make. I re-plumbed using some short pieces of hard pipe to get a deeper fit into it, there were enough of the original rubber fittings to go around. Once that was taken care of I cycled through the settings. I still wasn't getting good center vent air, but I could feel that the Center flap control was working. (It's right on the front.) I found that the Diverter flap wasn't doing its job, and when I pulled its hose off the valve block and sucked on it I got a blast of air in the face. I teed a vacuum gauge into that line and removed the X1 connector from the ACC panel. When pin 6 was grounded the gauge registered, so that part is fine. The ACC system either chose not to actuate it, or else the driver was broken. I opened the ACC panel back up and resoldered the circuitry in the area of the drivers, paying particular attention to things connected to pin 6. Since I had the thing all the way open I noted that it only had one PCB inside, rather than the two I've seen before (more integration?), and it used some kind of Motorola 40-pin processor. There were a pair of 74HC373 8-bit latches that are probably the driver outputs for the processor, and a bank of four SGS-Thompson L9309 (88944) SIP's that are the drivers themselves. (Dual high-current low side current-limited drivers.) There are also clamping diode arrays on the outputs to the valves. Other 'interesting' devices are, of course, the Motorola processor, labeled:
ZC93769CP
MKCS0006DH
JH8
QLDR9006
a LM2904 dual op-amp, and a heat-sunk L9307 dual driver (the L9309's big brother), probably for the monovalve and the auxiliary coolant pump motor. On the X2 (input) side of the panel there are two 74HC4051 8-input analog multiplexers and another L9309. Three transistors and a LM2940T 5 V regulator complete the complement of active devices. There are two thermistors on the board, one near the heat sink and one at the other side. These are probably used differentially to keep tabs on the high-current driver's state. All in all, it looks like a nice little design.

Anyway, I put it back in the car and tried it out again. This time I got normal center vent behavior. I'm not a-gonna look too closely at this, just call it fixed. The car went back together pretty easily after that, even the side carpet. We'll see if this makes Jill happy.

Tuesday, July 21, 2009

This evening we (including Dad) went to dinner in the car, and on the freeway on-ramp it refused to shift up. We ended up driving for a mile, flashers on and on the shoulder, before it relented and up-shifted. Not nice.

At least the AC was working correctly.

Tuesday, August 11, 2009

We were at the coast on vacation and fired it up to go home. It'd been parked nose-down for days, and wouldn't move. Low on transmission fluid, nose down, and cooled off it no longer had pressure, presumably because the oil no longer reached the pump pickup. I put in the quart I'd thrown in the trunk for just such an eventuality and off we went. Going to have to deal with that leak.

Friday, August 21, 2009

Becker makes the 4602 as a modern CD-capable replacement for the radio. Don't know if it'll do CD-R, and that's critical for us. Their 788X series (X=2: White display, 5: Blue, 6: Yellow, 7: Red, 9: Green) also looks interesting, this also does MP3, CR-R/-RW, etc. I've heard mention of a 4337, but it might be European. (AM incompatibility, etc. Wouldn't be good, Jill listens to a lot of AM too.)

Tuesday, August 25, 2009

I ordered another suspension pump shaft seal, two liters of fluid, and a transmission filter/seal kit.

Tuesday, September 1, 2009

Replaced the burnt-out LR turn signal lamp.

Saturday, September 5, 2009

The Harman/Becker BE 7881 Traffic Pro I bought through eBay ($160) came today. (Seller says it was a take-out from a Mercedes, but as Harman is what's printed on the front it couldn't have been an OEM installation in the beginning.) It looks good, but even the antenna connector is different than before. Will definitely need some adapter cables.

Tuesday, September 15, 2009

Jill complained that the turn signal was out again, so I had another look. Stupid PO actually had parking lamp bulbs in those sockets, which I'd faithfully replaced last time two weeks ago, so I replaced them with the correct bulbs. I'd thought they seemed a little dim the last time I followed the car! I also ran around the car again with touch-up paint. It's amazing how many sessions of that you need before you stop finding chips and scratches.

Thursday, September 17, 2009

A guy on Craig's List was selling 5 quart cans of Royco 756 aircraft hydraulic fluid at $2/quart, $10 total. This stuff is MIL-PRF-5606H rated, which is the same stuff (more or less) as the suspension system needs. Red-dyed, though, but otherwise should be compatible. Much cheaper than the official stuff! I bought all five quarts.

Thursday, September 24, 2009

Jill left the seat belt hanging out of the car door again, but this time the stinking dogs found it. Ruined, and there's no donor in the junkyard right now. (Somehow, this is all my fault.)

Friday, September 25, 2009

The order from Rusty finally came after a month of waiting (I'd had to call again, and he re-submitted it to his vendors), but it contained the wrong seal for the suspension pump! I'd ordered the shaft seal, but what I got was the body seal. All that waiting, and still I can't proceed. Can't do anything about it 'til Monday, however.

Tuesday, September 29, 2009

It finally occurred to me that I already had a replacement seat belt: one that was earmarked for the passenger side to replace the cobbled-up arrangement I had made. Well, that belt's working well enough, it doesn't really need replacing, unlike the now-ruined driver's-side belt. I washed the 'new' belt webbing with warm soapy water and dried it. I used vise-grips to hold it unrolled to dry while I removed the old belt. The switch was uneventful.

I then jacked up the car and had a look underneath. The rear suspension components are dry, and look like they're hooked up. The valve is in good shape, visibly. That's good. There was a missing rubber exhaust hanger on one of the resonators, so I replaced that. I checked and topped off the transmission fluid, I can see that its leak could well be from the pan so I should have what I need for that. Since I was underneath I used the MityVac on the shift modulator. It leaks down, so I'll need a new one of those too. The input shaft of the steering box is really messy, I need a new seal kit for it, too. I saw no significant signs of any other fluid leakage. I put one of the quarts of Royco oil in the suspension tank, it was long past time to get some more oil into the system.

Wednesday, September 30, 2009

I ordered a spare key (from the dealer) today: P/N 126 760 10 06, $25. When I got home I found a wayward Fed-Ex package containing the suspension pump shaft seal, P/N 004 997 01 47! This must have been trickle-in from the original parts order, the remaining parts of which never showed up. Well, at least I don't have to order another one!

Thursday, October 1, 2009

The 'new' seat belt is difficult to pull out. I had a closer look at the old one, and the belts are not interchangeable! There is a little 'ear' that prevents the upper belt guide, when installed on the correct side of the car, from rocking too far backwards. With this incorrect belt it won't rock for-wards, causing binding when pulling out the belt. (If you pull straight down it comes out easily.) Will definitely have to keep my eyes open for a new, correct belt for the driver's side. (Then this one can migrate across to where it belongs.)

Saturday, October 10, 2009

On a family outing today it appeared that the car was unable to heat, even when set on MAX. Monovalve? Will need to check into that!

Monday, October 12, 2009

Started driving this car myself, with the departure of the 380 SL. I disconnected the monovalve cable to see if it would heat that way. It does.

Tuesday, October 20, 2009

Reconnected the monovalve cable again, as I'm now driving the 380 SL again. The car reliably heated at all times, so either the control panel is screwed up, or the monovalve doesn't respond correctly to PWM attempts.

Wednesday, October 28, 2009

Jill complains that there is no heat again, so I disconnected the monovalve cable again. Heated just fine for her then. Need to hook up a test light to the monovalve cable in order to see if it's trying to modulate the heat or not.

Wednesday, November 18, 2009

Jill complains that the windshield wiper blade is coming apart... Yep, sure is! The plastic retaining clip also broke on the driver's-side wiper, just like the other one. And, just like the other one, I used a screw to hold it in place. We stopped at Schucks to get a new Trico wiper insert, and I found they'd only just discontinued carrying them. The counter jockey said the other nearby store was still in the process of pulling them from the shelves, so we went there and bought all three 22" inserts he had left, he had to dig them out of a pile in back.

Thursday, November 19, 2009

I installed the new wiper blade. It fit perfectly. Works well, too.

Tuesday, November 24, 2009

I swapped out the 'weak' driver's-side brake light, which turns out to have been a red-painted bulb. No wonder it didn't look right. I also filled the wiper fluid.

Thursday, December 3, 2009

The other side's brake light was out, so I replaced it. The filament broke off the post, it's possible that the intermittent brake lamp out warning we've been getting for some time was due to this all along. No fun replacing bulbs when it's 16 °F outside!

Monday, December 14, 2009

Snow today, finally. I swapped the Hakkapeliitta 1 snow tires from the SDL. Twice as much work that way! We'll see if they've got any life left in them.

The rear suspension looks 'down'. I really need to address this.

...Jill reported that the car was shimmying quite a bit. I drove it today, and she's right. The tires took quite a 'set' during the two years (or so) that they'd been sitting on the other car. We'll see if they straighten out, or whether they're ruined.

When she got home I checked the air, and the two rears were low. (Didn't get to them this morning, but they looked OK.) I also noticed that the rear was sagging, we left some bags of dog food in the back for weight, and the suspension fluid was all gone. I put in another quart of the Royco, then I went for a test drive. No real change. I did notice sounds of tire rubbing from the RR on left-hand turns, and when I jacked up that side I could see where it had been rubbing on the interior of the wheelwell, trunk side, but it seemed to me that it looked like it was protruding a bit much there. Yanking on the wheel didn't show any obvious looseness. The rear end was raised again, anyhow.

Tuesday, December 15, 2009

Just in time, we had about 4" of snow overnight.

Saturday, December 19, 2009

The tires are lumpy, they're not getting better. Jill also reports some intermittent scraping noises, and I actually heard it from the house when she last took it out. I jacked up the rear and ran the car with it in gear. (If the car ever had a limited slip differential it's no longer working as such.) The RR had a little bump. The LR had a big bump, and had worn through to the steel belt. Worse, however, is that the RR appears to have a bad wheel bearing. (This time I jacked it up under the axle carrier, so the car suspension was in a closer to normal configuration.) I could wobble the wheel by hand, and see the motion telegraphed to the axle. This job is not very DIY-friendly, by all accounts, so I'll probably have to take it in. And I won't do anything with the tires until the bearing's taken care of, which will be soon.

Monday, December 21, 2009

I took the car to see Fernando at Motortech. $343 later it had a new wheel bearing, and he noted the transmission was 3 quarts low (he topped it off). He didn't think much of the transmission, or the bad tires! (He also noted that the wheel bearing job is a real SOB, which is of course why I brought it for him to do!) When I picked it up (two days later) he took me in back and showed me the 280 SE convertible he's got for $ale (well into the six figures). Very very nice car, and immaculate. Our poor Ebola Fishtank is a pale imitation indeed.

Tuesday, January 12, 2010

I ordered the cables (from Becker Autosound, parts@beckerautosound.com, (201)-773-0978) to put the Becker 7881 Traffic Pro in this car.
Qty Item Cost
1BAS-1253
Harness
$18.99
11319-108
Preout cable ( TP )
$24.99
Subtotal:$43.98
Shipping and handling:$12.00
Total:$55.98

Friday, January 15, 2010

I bought three used 205/65R15 Hakkapeliitta 1 studded snow tires from a guy on Craig's List. He'd had tire damage and lost one on the right, I think I can salvage one of mine on that side. (I know both lefts are really bad.) They're of unknown vintage (he'd bought them used himself), but they're certainly better than what's there now, even without counting the lumps. $75

I also stopped at the U-Pull and got two wiper blade assemblies from a 126. Sadly, it didn't have the right kind of seat belt.

Monday, January 18, 2010

I jacked up the left side of the car and put its two wheels into my car to take to Les Schwab. When I went to get the matching two replacement tires I found that once off the wheels they're no longer 'handed' (as they can be mounted either way 'round), so I need not fear running short of tires provided that I can find one keeper from the original set. I also found that the replacement tires are in poorer shape than I'd thought. The sealing surfaces are all rusty and gunky, and one of the tires had chunks out of the sealing surfaces. (Looks like they didn't lubricate the tires before running them through the machine.) Not good. I used Toluene to clean the tears and Shoe Goo to repair them. The tears don't quite look deadly, provided that great care is used when installing the tire. The tears don't quite go to the sealing surface itself, which would be fatal. However, it's quite likely that this tire may not be usable anyway. I think these tires may be fully as old as the ones I'm replacing. I decided to back off on my plan a bit, and do only the one really bad tire to start. I used 50 grit sandpaper around my thumb to clean the rusty sealer off the sealing surface of one of the tires. I will get this one wheel taken care of and then drive the car to determine what next gets done.

Schwab was deserted, they swapped my tire immediately, no waiting. No charge either, since I didn't bother getting it balanced. (Not yet, anyway.)

Tuesday, January 19, 2010

I put the two wheels back on the car and drove it to work to see how it behaved. It was much improved, but there's still some wobble up front. It's somewhat variable, too. I'm going to try swapping out wheels one at a time to see if I can identify the problem child, it's not particularly icy right now. (I have a spare or three lying around, of the summer tire variety.)

Wednesday, January 20, 2010

I took off the LF wheel and replaced it with one of the SDL's old summer wheels. We'll see if that cures the wobble or not.

...Still a bit wobbly up front, but I think it's better. Will try another wheel swap tomorrow.

The cables for the Becker came today. One connector block looks fine, but the other I don't quite see how it hooks up. The antenna connector is still wrong, too. I had a closer look behind the faceplate, it appears that there's a CD in it. The navigation maps? Let's hope so!

Thursday, January 21, 2010

I took off the RF wheel and replaced it with another summer tire.

...Better yet, though not quite perfect. The LF tire was low on air, however, and I stopped at Schwab's for a quick shot of air. I'm going to try swapping it back tomorrow in order to get an A/B/A+B set of wobble data. Then I'll decide what to do, exactly.

I got both new connectors plugged into the Becker. The preamp-out connector was very odd: it's a small connector that plugs into a large sea of pins, but it really can only go in one way. Not something to try to do in the dark!

Friday, January 22, 2010

I put the LF snow tire back on.

...Still fine. That fingers the RF tire.

Saturday, January 23, 2010

I took the RF wheel into Schwab's and had a (freshly-sanded) tire put on. It was pretty busy, I got dinged this time. $8.15, but I suppose I can't really complain.

I then got out the Becker 7881 and took it to the car. Just as I thought, the connectors don't match up with what's in the car. That'll be fun.

Monday, January 25, 2010

10-gauge solid copper wire is a snug fit into the car's female radio connector blocks. I cut some 1-inch pieces and got a small block of Mpingo (a.k.a. grenadilla, African blackwood, clarinet wood) to make keepers for them. I used a power connector from an older Becker as a pattern, and drilled four holes in the wood strip, then made little 'canes' out of the wire and twisted them into the tight-fitting holes in the wood. This ersatz connector mated well with the car's connector, and I soldered the new Becker's harness wires to the loops. I tried it out, and was greeted with "ENTER CODE KEY". Oh. I was able to eject the CD, and it's an East coast USA navigation disc. East coast, huh? That'll be a lot of use! Anyway, I potted the back side of my homemade connector in Shoe Goo to prevent shorts.

Tuesday, January 26, 2010

I tried the Becker code applications I have, and got either [8]2544 or 42144 from the serial number 7881A6025000224, only the last four digits of which were accepted by any of these apps. None of these codes worked, the radio wants five digits and has no buttons for 8 or 9 so the first codes are out. The only correctly-formatted code was 42144, which didn't work. I only tried once, carefully, I know that game! I contacted the seller, and he had nothing to offer.

Regarding the connector mismatch on the pre-out cable, Becker is checking the invoice. The ordered/invoiced part number 1319-108, which matches (partially) the tag on the cable. Its full number is 1319.108-276, and also has Zeichnungsstand 20.10.98, Fertigungsdatum 31/05, and Prüfnummer 973/108 on it. I've also asked for the security code.

...Becker says that the wrong pre-out cable was ordered or shipped, and to send it back and they'll substitute the correct one, part number BAS-1185.640, which has the three-pin plug on it. They also state that the decoding will be $20. Great. I mailed back the incorrect cable today. $1.56 that cost me. I asked them to bill me for the code. The costs (in pain and dollars) are mounting up!

Sunday, February 7, 2010

Jill said there was some scratching/scraping noises coming from the back of the car, so I jacked up the right rear to take a look. Nothing wrong that I could see, I believe the noises are rocks and mud caught against the splash shield. I did find that the tire (one of the originals) has worn down to the belts, so that's where I'll put the last replacement. I sanded the gunk off of its sealing surfaces.

Monday, February 8, 2010

I drove the car today, OMFG the noise! Horrid metal-on-metal scraping noises, heads turning whenever we drove by; it was awful. And, naturally, all on the driver's side which Jill had neglected to mention. (All weird noises had hitherto been on the other side, so that's where I looked yesterday.) I'll have to jack it up and dig into it, it probably needs new pads, and perhaps a caliper rebuild. I hope it hasn't ruined the brake rotor. As of now the car's officially on the bench.

Tuesday, February 9, 2010

I jacked up the car, and the pads are indeed shot. I dug around in the garage and found a decent set of used rear pads that I can put on. The rotor surface looked OK. No time to proceed further, however.

The stereo cable came today, and looks to be the correct one. The paperwork had BAS-1185-640 scrawled on it, and the part itself reads: 5000-469, and also has Zeichnungsstand 15.01.96, Fertigungsdatum 39/06, and Prüfnummer 5000-469c on it. "Made in Tschechische Republik". There was no sign of the asked-for security code.

Saturday, February 13, 2010

I got to tackle the brakes today. The pads were almost shot, the vile noise was a small (but obviously strong) rock pinned between the caliper body and the disk. I pried it out of there and gave it to Daniel to show Jill. One of the pads was OK, but the other was paper-thin, so I replaced it with a better one. It got the usual scrape-out and greasing job on the pad edges and backs. Both pucks in the caliper moved easily enough, there was no need to take it apart for rebuilding yet.

I moved to the other side and took off the bad wheel and put it (and the last replacement) in the Frankenheap to take in for the swap. I grabbed Daniel and we went in, they were able to do it right away. No charge for this one, either. When we returned home I put it on the car and let it down. Ready for action again!

Monday, February 15, 2010

I started installing the Traffic Pro. The new cable worked well, the thing is half in the dash and pleading for the Code. The antenna plug is going to be fun.

Tuesday, February 16, 2010

The bill for the code came, and I paid it. An hour later the code showed up: 225XX. I put it in the radio, and its normal display came up. It's interesting that the last four digits are what I got out of one of the old decoder applications, it almost saved me $20. (But didn't.)

Wednesday, February 17, 2010

I planned the fabrication of an antenna jack converter. More mpingo, and some 14-gauge solid copper wire. The plan is to take one of the irregular chunks that is large enough to drill a socket for the shell of the connector on the back of the radio to slip into, and mark the circle on it. (The wood oriented for the L-shaped drilling's benefit, the short leg is for the radio side socket, the long for the antenna plug in the car.) I'll drill a hole along the periphery for the wire to go into, then drill out the center. At 90° to this hole I will do the same thing (to make the long leg of the 'L'), twice, for the center pin and outer body of the antenna plug in the car. The shield wire is to meet at the inside corner of the 'L', the signal wire is diametrically opposed to this and will bend 90° inside the free space inside the big socket in order to plunge into the center contact of the radio's jack. Bad ASCII art:

       MMMMMMMMMMMMMMMMMMMMMMM
       MMMMMMMMMMMMMMMMMMMMMMM ← Mpingo (wood) body
= = ========____MM      +   MM
= = ========    MM___,  |   MM
    ↑  MMMMMMMMMMMMMM|  |   MM
    |  MMMMMMMMMMMMMM|  |   MM
    |            .
    | Antenna    .   ,_____,
      Plug       .   |  V  | ← Protruding antenna jack
                 .   |  |  |
            - - ---------------- - -
                   7881 Radio                                
The two 14-gauge wires are pinched against the antenna plug by the holes in the wood; the shield wire is similarly pinched against the antenna jack shell. The signal wire plunges freely into the antenna jack, some glue in the open space helps keep it oriented.

Sounds like a plan, I wonder if it would work? Six precision holes using what are essentially hand tools is not really a recipe for success. This'd sure be a lot easier if I just had a female Motorola antenna socket that I could use, I wonder if the junkpile has one? I should look harder.

Thursday, February 18, 2010

Yes, further digging revealed several donor candidates: a $6 thrift-shop Becker 780, an old Jet 8-track that came in the Albatross, and a $1.50 thrift-shop Delco AM/FM I bought long ago for the knobs, for the Chevy pickup. The Delco is the least likely to ever get used again, I think I'll cannibalize that one even though its socket is spot-welded to a metal piece that's screwed to the chassis.

The metal piece unscrewed easily from the Delco, and I cut the wires going to the socket. I ground off the metal bracket, the socket that remained snapped easily into the plastic clip on the back of the Traffic Pro. I cut a piece of 10-gauge copper wire to serve as the center plug, and a piece of 14-gauge copper to wrap around the outer shell. (10-gauge is what fit snugly into the center socket.) I soldered both to the antenna socket and attached the assembly to the radio. Looks cruddy, but is secure enough.

I slipped the unit into the car and hooked up the blue antenna control lead, which needed a crimp-on spade lug and some electrical tape, and turned it on. Re-entering the code I could then run the radio, which identified the stations by call sign and started playing. I'm only getting sound out on the left front speaker, but I'll dig into that later. I tried a CD and it seemed OK, and a whack at the navigation system showed it reading the CD and then asking me to select a destination. I removed the original Becker retaining clips and put them in the radio box in the trunk, and pushed the unit most of the way home in the dash. I think it's going to work.

Friday, February 19, 2010

I pulled out the Traffic Pro and (temporarily) replaced the Becker, but the right channel was still out. I then fiddled with the front/rear fader in the console and the right channel came back. (I could have saved some time there by trying that first...) I then reinstalled the Traffic Pro and got the wiring tucked behind and below the radio so that it would go (almost!) all the way in. (It looks like it's all the way in, though I think it's still protruding 1/8" or so.) I replaced the ashtray, and called it done. I put the East Coast navigation CD in the console storage box, for lack of a better place to keep it. I spent some time fiddling with the controls, it's not obvious how to get some things done. I'm not sure how much I like this thing. I boxed up the original Becker, with mounting clips, and labeled and stowed the box in the garage. (Never to be seen again?)

Let's hope Jill likes this thing, it was certainly enough expense and trouble!

Wednesday, March 3, 2010

The RR door had been 'crunching' lately when opened, so I popped off the door panel and examined the door check. It was fairly dry, and some rust was starting to set up shop in the track, and presumably on at least one of the large ball bearings. I used WD-40 on it, then re-greased the track. It went fairly well, clamping the arm in a vise and pounding on the body with a BFH was necessary to move the slider out of the first detent. Reassembly was the usual problem, getting the two hinge-side screws started again can be surprisingly difficult. All the glued-on plastic and foam fell off the door, so more Spray 77 glue was required. The connector to the ashtray was falling apart, and partly not there, and the styrene light fixture fell apart too. (A little cyanoacrylate glue took care of that.) All but one of the hooks on the top of the door panel were already broken off. With perseverence, however, it all went back together, well enough at least when considering that there aren't any top hooks. The door seems to work much better now, anyway.

Saturday, March 6, 2010

Summer tire time! I swapped the new tires back from the SDL, twice as much work that way! I put the Hakkapeliitta 1's into the shed, and put the nearly-worn-out Toyos (the SDL's summer tires) back onto the SDL. One of the new tires (RR) was flat. I didn't see any nails or anything, perhaps the bead has just lost its seal. We'll see.

Tuesday, March 9, 2010

Jill noticed that the RR tire was low again, and took it to Schwab. They said the wheel was corroding and losing its seal. They cleaned it up as best they could, and remounted the tire. We'll see if it holds up.

Monday, March 22, 2010

Spilled barbecue sauce all over the trunk, so the trunk carpet got a bath. Lots of dirt besides red sauce came out!

Wednesday, March 24, 2010

The low oil light's been flashing lately, so I checked it: low oil. I put in two quarts this morning.

Monday, March 29, 2010

Car passed its required biannual emissions test. Easily, it looks like.

HC
(PPM)
COCO+
CO2
O2RPM
Cruise Limit:1501%6%N/AN/A
Cruise Emissions:510.1%15.3%0.09%N/A
Cruise Result:PASSPASSN/AN/AN/A
Idle Limit:2201.2%6%N/AN/A
Idle Emissions:200%12.2%3.62%780
Idle Result:PASSPASSN/AN/AN/A

I have no idea what the CO+CO2 'limit' is supposed to mean given that CO2 (along with H2O) is the ideal engine exhaust. Engine too big? Lame.

Thursday, April 8, 2010

Jill's been concerned about the apparent malfunctioning of the ABS system: it seems to engage when it shouldn't (and oddly, at that). I've noticed this myself. I think I need to disconnect the controller, but first I need to find it. (ABS is a luxury, but brakes that you can trust is not.) According to the ETM (page 209), it (N30) should be near the battery and the hood switch, behind the first firewall. I had a look, but it wasn't immediately obvious which thing there might be the ABS controller. The biggest item right there looked a lot like the engine management computer, and we do need that!

Friday, April 9, 2010

According to the ETM (page 207), the CIS-E control unit (N3) is "Front passenger footwell, behind right kick panel." OK, good enough for me.

I removed the N30 (?) from the car. Two spring clips held the unit into its nest, and one rather strong spring clip held the connector onto the unit. (The connector does look just like the CIS-E controller I found in the 380 SL.) I took a plastic bag and tied the connector in it, for protection, as this may well be a 'permanent' condition.

The controller bears the following labels on a blue sticker:

(B)BOSCH0 265 101 018 (085)
Made in Germany
(MB)005 545 21 32  06424473

The plastic cover shell was held on with four self-tapping coarse thread Philips-head screws, and had a rubber gasket between it and the pot-metal casting that carries the 35-pin connector and the circuit board. The circuit board had been dipped in a very soft clear conformal coating, much like RTV. It seems like it might scrub off mechanically, if necessary. There were two big 40-pin DIP AMS-brand (?) IC's on it, they looked identical and were labeled:

8950GAL
BB 33 208
C14445
AUSTRIA

There was also a 16-pin DIP: Siemens 30008, 9002, and a 21-pin ZIP IC clamped to the casting. (Markings hidden by the clamp.) There were two hybrid modules mounted at right angles to the main board, and three large inductor-fed power transistors clamped to the casting, markings also obscured by the clamps. There were two aluminum electrolytic capacitors and a tantalum, and a 4.194304 MHz crystal. There were seven diodes of various sorts, and the usual crowd of resistors and capacitors filling out the complement. All date codes are '89 or '90.

The solder joints didn't look all that bad, but as I've found out plenty of times already that doesn't necessarily mean much. However, today I'm not trying to repair it, only disable it. I put the cover back on and bagged the controller (for protection of the now-exposed connector) and put it back in its nest for safekeeping.

Thursday, May 6, 2010

It's been shifting out of Park a bit slowly, so I put in another quart of ATF. Stupid leak!

Sunday, May 16, 2010

It was past due, and I finally changed the oil, but didn't change the filter. I used the vacuum sucker, it took quite awhile because I was only able to warm the engine for a few minutes before I began. I also put another quart of the Royco 756 in the suspension tank, it was empty.

I topped off the windshield washer fluid with water and checked the brake fluid level, which was OK.

Friday, May 21, 2010

Jill asked me to dig out the center seat belt in back, she wants to taxi the schoolkids in it rather than the truck. I did so, but I first had to remove the seat bottom to do it. (Two 10mm bolts, not the spring clips of the non-reclinable rear seat. Uncovering a disgusting and vast array of my child's 'droppings'. Ugh.) While I was there I took another look at the recalcitrant buckle on the driver's side. (It has always taken an excessive amount of force to get it to latch.) I removed it from the car in order to dump out anything that might have gotten into it, but that was ineffective. A closer look showed that the latch can be taken entirely apart, starting by grasping the flat plastic side cover with vise-grips and pulling it out. (There are six plastic hooks that tie the flat piece to the shell.) Once the cover was off I could see that one of the two main springs had gotten out of its channel and was bent under the guide for the buckle's tongue. I don't see any way that this could have happened except by being mis-assembled at the factory. I gently removed the red plastic release which let me fully take apart the spring mechanism, straightened the bent spring, and put it all back together. The belt now works properly, Jill will be pleased.

Saturday, May 22, 2010

Jill complained that the heater wasn't coming on and requested that I unhook the monovalve again, so I did.

Sunday, May 23, 2010

Jill complained that the heater wasn't shutting off enough even with the OFF button, that being baked was worse than being a little too cold, and requested that I re-connect the monovalve again, so I did.

I really need to look into that.

Jill's been noting that the engine temperature is too high, and that the power steering is groaning again. I checked the steering fluid, and it was low. That was easy to correct. When she got back from an errand I checked the radiator, and it was pretty cool behind the cooling fan, yet fairly hot along the sides. Not a good sign. I used the hose to spray it out, hoping to remove any gunk that was cutting the airflow. (There was a lot of mud along the bottom.) Better that than reduced fluid flow, which is what I most suspect. We'll see if it's any better after this. I may need to do an acid flush.

Tuesday, May 25, 2010

Too many things wrong to trust the car as-is for another trip to Seattle this coming weekend. Time to dive in. On the list: It all starts with jacking up the car.

I did this, but I first had to replenish the hydraulic fluid in the jack in order to get the full height out of it. (I used power steering fluid.) Once up and on jack stands I removed the fan and drained the coolant. I was only able to get a gallon out of it. That doesn't bode well for reusing it, there's at least another gallon trapped in there. I dug out the bag of flushing thermostats and swapped in the correct one.

I also had a look at the transmission leak. It really looks like it could be the pan that's leaking, so I should be able to fix it. I already have a new filter and gasket kit, I just need to check the pan's flatness. Overtightening the bolts bends the pan, but it can be bent back. I'll use the saw table (ground cast-iron) as a flatness gauge.

I tested the thermostat in a Pyrex cup using boiling water and a meat thermometer. I filled the cup with hot water and then added boiling water to bring the temperature up. I'd spill out water to cut the thermal mass, raising the proportion of boiling water to not as I went. The thermostat started to crack open at around 77 °C (the thermostat was marked 80 °C), by about 90 °C it looked pretty far open: maybe 1/4" or so. When left to cool on its own it was pretty much closed again by 77 °C.

Wednesday, May 26, 2010

I flushed the cooling system with a continuous flow of water. I put the garden hose (on low) into the filler neck, and replaced the upper radiator hose with one that has a flushing fitting in it. The garden hose filled the system, and it ran out the upper radiator hose fitting. I set the car to idling the whole time once it was full, and nearly-hot water ran out of it after a time. It took about a half hour until the emitted water looked (and tasted) clear of coolant. It was interesting that the bulk of the radiator remained cold during this operation, only warm over on the side where the two fittings were. When drained, the radiator water was cold. This flushing will insure that there will be nothing in the cooling system but acid and water—and corrosion! It should work best that way.

I dug in the garage until I found the 38-oz (2.5#) bags of powdered citric acid that I'd bought with a neighbor. (We'd split an order.) I don't remember what I paid, but I think it was about $5 a bag. I ran out of time to perform the acid flush today, but I gathered everything I'll need for tomorrow. (Or perhaps even tonight.)

...Yes, tonight. I followed the procedure I used before on the SDL. (This is essentially Job 20-015 in the service manual.) I let it idle about a half an hour with the acid sealed inside, that gave it about 15 minutes at operating temperature. While it was idling (with the heater on full) I kept feeling the back of the radiator. Eventually it got to a more-or-less even temperature, which was not the case initially. Hard to say whether or not that's a significant test, what with no airflow through it. While it was hot I started putting PB Blaster on the transmission cooler fittings.

I also let the car idle during the water flush to remove the hot acid. I pushed water into the filler neck and let it perk out of the special upper radiator flushing hose's fitting. When the hot water coming out no longer tasted sour I shut off the engine, then let it flush more until the water coming out was cool. The whole procedure took about half an hour. That should have gotten most of it. While I waited I dug out the spare monovalve I'd gotten at the junkyard some time ago and checked its rubber bits. It looked good. Next session I'll pull the car's monovalve insert and see how it looks, and swap inserts if the junkyard one looks better.

Thursday, May 27, 2010

I removed the radiator and gave it a good physical cleaning. While I was there I also washed out the AC condenser's fins. I used small rubber stoppers (from the clarinet rebuild) to cork off the transmission cooler lines in order to keep out dirt and water. I was unable to remove the lines from the radiator, but the flexible lines are only about 6" long and I was able to remove the other ends from the hard lines, then lift out the works. (I had to use the propane torch to heat the nuts to the hard lines. That same trick didn't work on the radiator end, I was unwilling to use too much heat or force there or I'd ruin the radiator. Then I would be unhappy.) The radiator fins looked pretty good, not all clogged. I then pulled out the monovalve insert, and it was definitely bad. I replaced it with the good used one from the junkyard. The monovalve is less accessible on this car than it ought to be, the new-style rectangular engine diagnostic connector (with snap-on cover, LED, and readout pushbutton) is in the way.

I tried to remove the suspension pump, but two of the 5mm Allen bolt heads stripped out. (Fucking things, whomever thought that those pieces of shit would be better than regular 10mm hex bolt heads needs a blanket party.) One of the bolts is a short one (of two) that only holds the head to the pump body, the other is a long one (of four) that's holding the pump (head and all) to the block. I'm not sure what I'm going to do there. When I do get those bolts out, all of them will need replacing.

...After I got home from work I tried again, this time using some hammer-in left-hand twist bolt extracters. One of them was just the right size to hammer tightly into the dead Allen sockets, and they cracked loose and came right out when I turned the wrench. So I'm back on track again, I'll just need new bolts for sure. (I knew this already!) I'll get those tomorrow.

Friday, May 28, 2010

I removed the suspension pump and replaced the shaft seal (P/N 004 997 01 47) again, more carefully this time. (I plugged the oil lines with more rubber stoppers while it was apart.) I used ATF to lubricate things on reassembly, that made it much easier than last time. I put the pump back loosely with a couple of the best of the old bolts, just to hold it in place until I get new bolts. The seal I removed didn't really look bad, but it's possible I didn't have it hammered into its socket quite far enough. It has a microscopic nick or two in it, but given that I had to pry it out with a screwdriver that could be recent. I still believe the wayward suspension oil was getting into the engine, and this is the only place it can do so. I guess we'll see. In spite of my efforts to save it the suspension oil in the tank drained away. There went another $2! (Most of it was already gone due to the leak I'm chasing.)

I then reinstalled the thermostat, there was a lot of gray sludge behind the flushing thermostat. Not sure what's up with that, but I wiped it out. I then drained the transmission pan. I loosened its six retaining bolts, and some of them were very tight. No wonder it leaks. I'll tackle this next. So far things are on schedule, which means I have all of tomorrow to finish it!

...At lunch I bought the new M6-1×60 and M6-1×20 bolts at the hardware store. They only had lengths that were a bit too short or a bit too long, so I went with long. About $6 for all six bolts, highway robbery!

...When I got home I installed them, using some flat washers from my Harbor Freight hardware assortment. They all fit well in spite of being a bit longer than before. The suspension pump's back in place now, let's hope it worked.

Saturday, May 29, 2010

Finishing day! (Not real nice out: gray, windy, and intermittent rain. What my family has always called 'beach weather'.) I checked the (rebuilt) AC idler bearing, it was still OK. (You have to remove it in order to get at the suspension pump.) I then reinstalled the radiator and fan, and finished buttoning up things in front. (Except for fluids.) That actually went pretty smoothly. I checked the radiator shroud, no way that'll fit now, the fan interferes solidly with it at the bottom. Probably motor mounts letting it sag down, more now than ever before. Regardless, I left the shroud off again.

I then moved on to the transmission pan. I scrubbed off the worst of the dirt, then removed the pan. It was filthy, I tried it first in the solvent tank, which wasn't working well, and then I got smart: I got out the pressure washer, which made short work of the mess. There was a gray-black film on the inside of the pan, the washer made short work of that too. After I dried the pan somewhat I took it to the wood shaper to use its cast-iron table as a flatness gauge. It was difficult to do because of the pan's 'ears', but I could see that the pan rocked in the middle. I took a straight-edge out to the transmission and its gasket surface was flat, so the pan was definitely deformed, obviously letting the back end lift away from its mating surface and thus leaking. In fact, the highest point on the pan had cut entirely through the gasket, though it was interesting that this wasn't the point that was leaking. I used a hammer and a rubber mallet to bang away on the pan until I got its sealing surface nearly flat. I test-fit it to the transmission, sans gasket, and it didn't rock anymore, so I cleaned up the mating surfaces and attached the gasket to the pan. I then removed the filter, and installed the new one. (At 222150 miles.) The old filter had the gray film on its upper surface too. I looked at the vacuum modulator as it really needs replacement, but I don't have another one, nor do I see exactly how to replace it. The job looks tricky, it might be that the valve body has to be removed. Another time! I reinstalled the pan, being careful not to overtighten the bolts. I made sure to tighten them in stages, to keep the pan flat.

Time for breakfast!

...Tummy full, I'm ready to recommission the car! I emptied the oil drain pan into an empty gallon oil jug, paying attention to the amount. About three quarts. That told me to put in four quarts of ATF, as a start anyway. I poured the salvaged coolant back into the car and topped it off with water. (A gallon of Zerex G-05 will be put in later.) I put another quart of the Royco 756 in the suspension tank. (There's only one can left on the shelf, then things start to get more expensive. I sure hope this takes care of that leak.) Ready to go? I started the car and watched it idle for awhile, looking for leaks. Things looked good, no dripping.

I then lowered the car and took it for a spin, it passed. Seemed to drive as before, and I didn't see any dripping. The coolant level had dropped a bit so I put in a little more water. Ready for the road! I put another quart of ATF in the trunk, in case we need to add more on the road. (Getting that level right is very difficult for me.) Then I cleaned up the mess I'd made.

...After a test drive I found some seepage of suspension fluid on the bottom of the pump. It's probably the head gasket, but might be one of the fittings. I lack the time to do anything about it, however.

Tuesday, June 1, 2010

Back from our road trip! (We went to Seattle and Yakima to see relatives. We also saw Candide, which was great fun.) The car behaved well, certainly much better than it had been. The car didn't overheat one bit on the freeways, hovering between one and two needle's widths over 80 °C as we went up and down mountain passes. (However, it never got to more than 70 °F out—most of the time ambient was more like 45 °F). It did climb to maybe 100 °C idling around the city; I'm not worried, I can blame that on the lack of the fan shroud. The heater behaved completely properly, that bad monovalve was certainly the culprit. No sign of coolant leaks. The suspension pump is still weeping a bit on the outside, I'm sure it is the head seal. I have another one of those too, I can replace it sometime. The level in the tank was basically the same at the end of the trip as when we started, which is a big change from before. The transmission leak is substantially reduced, but the exhaust pipe was still smoking a bit at stops, I could see oil on it. Not done there yet, I guess, though the problem is nothing like it had been. (Nobody pointing at our car and saying it looked like it might be on fire!) The transmission seems to be shifting a lot better than it had, though it is still not right. (If you floor it from a stop it will not shift out of first [or second?] until you back off the throttle, nor does it like to downshift when you punch it.)

The hot engine idle speed is much too high, around 1500 RPM. Not as high as it goes when you unplug the idle actuator, so it's at least trying to work a little, but it's definitely not right. Perhaps it is unhappy about the hot coolant and acid fountains it was sitting under during the flushing? I need to look at it.

Well, why not today? I popped the hood and pulled off the air cleaner for easier access. This thing sure seems light...WTF??? There's no air filter in it! Never has been, I can't believe I never noticed this before. What an idiot, and we live on a gravel road! The air horn was caked with oily dirt, as was the air metering plate. I used carb cleaner to remove all the dirt, then decided to go for it and so I removed the backfire stop and the air plate itself. I cleaned everything I could, as far down into the air chamber as I could reach with the solvent and a rag. I got a lot of it out, certainly the upper reaches were clean. I put the air plate back, and using a magnet (for grip) and a wrench got it centered so that it didn't rub anymore through its travels. It had seemed a bit rough before I started the cleaning, perhaps this will help the rough idle? I know the plate is sensitive at the idle positions. If it drags at all the idle mixture will be wrong.

I went to the garage and retrieved the surplus air cleaner housing I'd gotten for Jill's 560 SL, it had an air filter still in it. After cleaning the dirt out of the car's housing I put the used filter in it, it looked clean enough. (Better than nothing!) The spare housing also had the fitting/filter for the smog pump that this car was missing, so I moved that over too. That'll be better.

Anyway, on to the official project. I looked at the idle air valve, and when I tested it with a battery charger it worked perfectly. The Shoe-Goo'd rubber pipe was split again, that was probably the problem. I cleaned it and re-Goo'd it, this time cutting a ring of inner tube rubber to slip around the outside of the repair. That'll cork off any future splits that develop. I really should get a new rubber pipe, it can't be that much money!

Wednesday, June 2, 2010

I reinstalled the now-dried idle air valve assembly and buttoned up the car. I started it, and the cold idle was below 1000 RPM, and was fairly smooth. It'll take a real trip (where it can warm up) to know for sure if it's fixed.

Thursday, June 3, 2010

I met Jill at work to hand off Daniel, and I could tell that the car's idle was still high. Not done yet!

Saturday, June 5, 2010

I checked the idle actuator, and when powered solidly with the battery charger the car dies. A trouble light shows it getting steady-looking power, or almost no power when unplugged and the idle is really high, so it's not a simple problem. Perhaps the electronics are confused? While messing with this I managed to lose the plastic connector shell down in the engine valley. While trying to retrieve that I managed to kneel on and break the brittle plastic headlight surround on the passenger side. Crap! I removed the headlight assembly and glued the pieces back. Shoe Goo, of course. While I was there I bolstered the long crack that's in the one on the other side.

I also tried re-centering the air plate, Jill reports that it now has trouble starting, it wants to die unless she gooses it. If this drags at all on the close-fit walls there will be problems at idle.

According to the ETM (page 208), the Idle Speed control unit (N8) is "Front passenger footwell, behind right kick panel." The photograph, page 229 Figure 1, shows it next to the airbag switching power supply and capacitor block.

Sunday, June 6, 2010

I reinstalled the repaired headlight, and flush with success I decided that I wasn't yet ready to give up yet on the missing idle speed connector shell. I then fired up the shop vacuum on a 1/2" hose and poked around down where it disappeared with it and a stiff wire, and was finally able to drag it out of its hiding place and get it stuck to the end of the vacuum hose. I then fished it out. While I was in the area I tested the idle air actuator, and it closes off completely at about 6 V which doesn't seem bad to me. I don't know what's up. I looked for my spare air valve, but it has gotten temporarily lost in all the crap.

Tuesday, June 8, 2010

Jill says it's still overheating. In the 70's today and the car was creeping up near the red while idling in a drive-through line. She switched cars until I could look into it.

Wednesday, June 9, 2010

I pulled the passenger floorboard up, and it's a little different under there than the (outdated?) manual shows. The car alarm brain is there, and the engine control altitude module, and the O2 and airbag plugs, but no airbag power modules. (I think they were integrated by then.) The idle speed controller was there as indicated, however. It's VDO (Made In Germany) and labeled:
(MB) 006 545 85 32
Leerlaufdrehzahrlregelung   LR 0005
Idle Speed Control    8 Zyl.
412.214/001/004         12V
and ink-stamped with 501 and 19/90. It has 11 pins in a 12-pin site, labeled (facing the pins):

       /                           /
      +---------------------------+
      |  -31  15 87B  C   KL  V   |
      |                           |
      |   O   O   O   O   O   O   |
      |     *               *     |
      |   O   O       O   O   O   |
      |                           |
      |  50*  TD     87A  LL  TF  |/
      +---------------------------+

The black plastic shell popped off of the pin carrier with a bit of careful prying. Inside it's considerably different than the usual vintage electronics I've come to expect in these cars. Progress, I guess! There's a daughter card soldered on standoffs to the main card. The daughter card is all surface-mount and conformally-coated, and single-sided like a hybrid module, and has an exposed IC die clear-potted to the board along with two LM2902 quad op-amps and a 4.194304 MHz crystal. There are also surface-mount resistors, capacitors, diodes, and transistors. It looks to be in great condition, which is good because this kind of thing is next to non-repairable. The 'main' board is traditional through-hole construction, and has relatively few parts: four diodes, some resistors, two power resistors, three small electrolytic capacitors, and two small power transistors (BD437 and BD438, a NPN/PNP pair). This board is not coated, and some of the solder joints looked a little suspect, so I resoldered it.

It was raining today anyway (not convertible weather), so I threw the IR temperature gear in the car for testing the cooling system temperatures later. I put the 'repaired' idle controller back and drove it to work.

...Idle speed was unchanged, about 1400 RPM when warm and in neutral. Only a little above normal when in gear and stopped, but the car's pulling against the brakes more than it should, and it doesn't really slow down when you let off the gas—you need the brakes more than you should. It really must be the actuator and its hot acid bath, but it's an odd failure mode since it seems to work right on the bench. I really need to find my spare so I can try it in its place. I don't want to purchase a new one on speculation, as they're fairly expensive.

Engine temperature was rock-solid right where it needed to be, but it was only about 60 °F today. I felt the radiator after I stopped and it had an even temperature gradient, even behind the fan. That's an improvement, at least.

Tuesday, June 22, 2010

I've been driving this car a bit lately, and the idle speed is all over the map. Sometimes (rarely) it's nearly normal, once it was about 2500 RPM (!), and most of the time it's 1200-1500 RPM. Definitely something wrong there! Sure wish I could find my spare air valve...

Wednesday, June 30, 2010

Jill says it's been reluctant to go into gear again, so I put in another quart of ATF. No, the leak is not fixed...

Friday, August 27, 2010

10 PSI in the RR tire today. Oops.

Tuesday, August 31, 2010

Ordered new brake pads, all around. Pagid. About $80.

Saturday, September 11, 2010

Brake day! I got the right side jacked up and all pads replaced, and rotated the tires while I was there. I had to grind some ridges off the front disc, it should get a new one next time. One sensor was cut into, the other not. All four pads on that side are still suitable for jalopy use. I broke for breakfast, then came back out and did the other side. Eerily the same, nothing special to report. Should get new discs next time, noted.

Tuesday, October 12, 2010

Lately the car's been bouncing in the rear like it had no shocks, and when I checked the suspension oil tank was empty. I put in the last quart of Royco 756, after this that slow leak's going to cost us somewhat more money. I also put a quart of oil in the engine.

Friday, October 15, 2010

The suspension tank is empty again. Three days? There's something wrong.

Tuesday, October 19, 2010

I got a chance to have a look at the car, and it appears that the suspension oil has all leaked out the left (rear) hydraulic strut. Blown seals, probably beat to pieces when it was running without fluid. Oops.

Wednesday, October 20, 2010

I found a rather intriguing article about BMW's: strut rebuild. Very interesting!

Friday, December 10, 2010

It took forever, but I finally got the main garage opened back up enough to put the car into. Will let the snow melt off of it before tackling the suspension. The car started fine, but wouldn't move until I put another quart of ATF into it. We finally had enough of a thaw (from the big snow) that I could move things around, like cars with no snow tires and the lawnmower (which is now parked under the new deck with a tarp thrown over it).

Monday, December 13, 2010

I jacked up the back of the car, high as I could get it. Two jacks, two jackstands. I sprayed PB Blaster on all the hydraulic fittings. The height valve may have been messed with, the locknut isn't anywhere near the socket on one end. Looks to me like the shaft seal on the left cylinder is blown. Won't know for sure until I get it out. Need to do some reading, next. Starting with the manual's Hydropneumatic suspension 32-501, Functional description, 32-510, Checking spring struts, 32-520, Checking pressure reservoir, and 32-530, Checking pressure oil pump and level controller. Followed perhaps by 32-610, Removal and installation of spring struts, 32-620, Removal and installation of pressure reservoir, 32-630, Draining and filling hydraulic system, 32-640, Removal and installation of pressure oil pump, 32-645, Replacement of pressure oil pump seal, 32-660, Removal and installation of level controller link, and 32-670, Removal and installation of level controller.

I opened up the trunk to dry out, water had gotten in.

Wednesday, December 15, 2010

Yesterday I did some reading, so today I felt qualified to remove the rear seat. (This is harder on a car with the reclining rear seat option, I've done plenty of the others. The manual wasn't very helpful at all.) First remove the two 10mm bolt heads visible along the seat bottom, near where the release clips are on a non-recliner. That lets the seat bottom lift up and out, and you have to unplug the heating elements along the way. (Unplug the backs, too.) The seat back was trickier. Remove the three 10mm bolts that are tucked under the seat back, one of them in the center underneath the plastic shield for the recliner motor, and not the two visible ones that are attached to the geared track. That lets you lift up on the seat back, releasing the upper posts from the holes in the reclining rack. Then the seat back comes out of the car. Now remove the two 10mm bolts holding the reclining back frame to the geared tracks, and flip the frame up enough to allow the sound padding to be pulled back. This exposes the area where the two plastic body plugs have to be removed, but first you might have to unclip the radio amplifier and the seat heater relay to get them out of the way. Once everything is out of the way the two plastic body plugs may be pried out, exposing the hydraulic strut connections.

Sunday, December 19, 2010

I got the control link removed from the valve. To grip the flats on the ball I needed a thin 8–9mm wrench , which I didn't really have, but I made do with the prybar I'd made for the 380 SL trunk hinge pin operation. It gripped well enough somehow to crack loose the nut. That and a 10mm wrench and I got the link loose from the valve's control arm. I then had room enough to swing the 11mm wrench on the bleed screw. The valve body wanted to twist on its sheet-metal mount, so I used an 18" Crescent-style wrench to put a hold on it. I had the piece of tubing I use for bleeding clutch slave cylinders on the nipple, with the other end in a clean ATF bottle. Rather than the 1/2 liter that should come out, I got maybe half of the tubing filled. Yeah, the system was empty all right!

Anyway, a 17mm offset box wrench cracked loose the hydraulic fitting. I removed the two washers and the banjo fitting and wrapped the open bits with aluminum foil to keep out dirt. I got the two 17mm bolts on the bottom removed, but the 17mm nut on top didn't want to crack loose. I should have tried the penetrant first, because I managed to badly twist the 8mm flat that's on the top of the strut. Oops! I put penetrant on and left it to soak. A little red heat would cure the problem, but applying said heat would be unwise as the gas tank is right next to the nut.

After a couple of hours of soaking I got out a rubber mallet and a stick of wood. I wedged the wood through the keyhole shaped body hole and spun the strut with the wrench until the hydraulic fitting wedged up against the wood. I then put the vise grips on the twisted flat on top the strut and struck the wrench with the mallet. Between the penetrant and the shock transmitted against the vise grips and the stick the nut popped loose. It was then a simple matter to raise the tire a bit with the jack, to release the tension on the strut and then remove it bodily from the car. The strut seemed to be in very good shape, apart from the leaking. MB P/N 126 320 46 13, Sachs P/N 012400 102 178 R.J (According to the EPC, this is used in 1988+ cars.) The ruined accordion boot looks like MB P/N 448 006 10 0?, the last digit (and a half, really) is obscured by a vent hole. This part number doesn't seem to be in the EPC. There's also a 53932 and a 1–2 molded into it, and a mystery logo that looks a bit like a hand giving the 'OK' sign.

I cleaned it off some and pulled back the damaged accordion boot. I could see a circular snap ring inside the strut body, so I got out a bar clamp and used it between the protruding shoulder of the plug and the shoulder at the top of the strut. Modest pressure caused the plug to push in fractionally, releasing the tension on the snap ring. Unfortunately I was out of time to proceed further. It is clear that this strut isn't much like the one I found the rebuild article on.

Tuesday, December 21, 2010

A little digging with some small screwdrivers got the snap ring out of the strut, whereupon the end sealing plug could be pulled out. There was a second snap ring inside that kept in the piston, that came out much the same. The piston itself has what looks like an engine compression ring, and it seems there may be some fine holes covered with spring washers in it. (I could see how the damping might be set by this.) No way the piston could be considered fluid-tight. The difficult part was removing the ball-joint end from the piston's rod. I found a couple of flatter than normal wrenches. One of them, an Indian 5/8", I ground flatter and opened up the jaws a bit to fit the thin flat on the piston rod. The 3/4" fit as-is on the ball joint end. A bit of banging on the wrenches on the anvil cracked loose the threads, then I could just unscrew the ball joint. With that off the rubber accordion boot and the sealing plug slid right off the end. The sealing plug has a fat O-ring on the outside, which I don't think was leaking, and a blue plastic seal ring backed up with a rubber O-ring on the inside. The two rings are kept in place by a staked-in cup. I don't know how one would find replacements for these seals. I'm going to try calling hydraulic rebuild houses in town.

The ball joint feels good, and its boot is good too. Only the accordion boot and the rod seal appear to be bad.

Seems to me that the auxiliary spring pressure of the strut is set by the diameter of the rod versus the pressure in the strut, and that the amount of damping is determined by the larger piston diameter (and the size of the valved leak holes in it) as it plunges back and forth through the fluid that fills the cylinder. (A lesser amount of damping is due to the smaller amount of fluid flowing to the accumulator spheres on compression. [Determined by the rod size.] The ratio of the piston to rod size no doubt sets one of the characteristics of the suspension.) The seal plug is responsible for keeping in all the fluid, of course, sealing the piston rod against the pressure inside the strut. It's a rather elegant design.

...I called around town to hydraulic shops, and most didn't want anything to do with it. The gal at American Seal Company, an affiliate of American West Chrome, said to bring it in and they'd have a look at it. They weren't too sanguine initially, but once I picked the seals out of the plug things started looking up. They looked pretty normal to her and she got out the calipers for a bit of measurement and then ran upstairs. When she came back down she said that I should get a lottery ticket today! She plopped a seal on the counter that looked just like what I'd pulled out, except that the plastic was brown. The two parts I bought were this MKR-22X29.5X3 Metric Buffer (Date code 12/21/06, SKU 146886), at $7.36, and a MOR38X4 Metric O-Ring for the outside of the plug, at $0.80. The total bill came to $8.87, a far cry from the pushing $400 that a new strut would run to. It remains to be seen, however, whether I can get it back together in a leak-free state. The big problem is the hard plastic pressure seal, which I believe went in before the pieces of the plug were staked together. Perhaps if I heat the ring in boiling water it'll be soft enough to put in place the same way I took the old one out, but without deforming in any permanent way. She said that if I ruined that one another was more than a week away, as the one I bought was the last one on the shelf.

I also hear that www.activesuspensionsystems.com might rebuild these struts. Probably not.

Tuesday, January 4, 2011

Reading indicates that the steep interior slope of the buffer ring should face inwards, and that customarily such seals are used in conjunction with a secondary seal afterwards. (Fluid that gets past the buffer seal is captured by the secondary seal, and pumped back into the cylinder past the shallow slope of the buffer ring on its return stroke.) Well, there is no such seal here. There is also customarily a wiper seal at the outside to keep out grit, but I suppose that an intact accordion boot takes the place of that. The same source indicates that heating the ring in hot (150 °F) water is appropriate to soften it for ease of installation.

Thursday, January 6, 2011

Pan of hot water ready, I heated the plug (a bit) and the old seal. The plan was to push the seal into the plug from the narrow piston sleeve end, using a suitably-sized socket to fill the large diameter section of the plug to try to keep the seal from going in past the retaining lip and into the large section of the plug, in an attempt to get the seal to seat in its channel without damage. After practicing a few times with the old seal to get a feel for it I installed the new seal. I think it went fairly well, at least it didn't look damaged or deformed. I then used brake cleaner to sluice everything out and then dribbled ATF onto the sliding surfaces as an assembly lube. I installed the rod into the plug, then the piston into the cylinder, and then the plug into the cylinder. The two snap rings went in easily. The piston slides smoothly, but of course I won't know if it's actually sealed until I reassemble the system and try it out.

I cleaned the accordion boot in a pan of hot TSP, which worked pretty well, and it looks bad enough that I doubt gluing it back together will be worth the effort. More holes than not. I really need a new one.

...As I'd missed my chance to call to try to order an accordion boot today, and because I could find no mention of them in the online parts ordering systems or my copy of the EPC, I began gluing up this one. Shoe Goo, of course. If I can't get another boot this'll be better than nothing.

Friday, January 7, 2011

I called Rusty, and the boot is not separately available. (A new strut is $390 through him, I checked.)

More gluing, I guess...

It might be possible to find something from a place like Gardan Mfg., but their off-the-shelf selection didn't look that promising. The boot needs an extension range of 1.75"–6.5" (overall length), an outside diameter of no more than 2.25", and a clamping flange of 1.5" on one end, and 7/8" on the other.

I contacted them with these specifications, and they quoted $72 each. Too rich for my blood, I think.

Sunday, January 9, 2011

I reassembled the strut. The hard part was, of course, getting the repaired but still fragile rubber boot installed with its retaining spring circlips. Eventually I prevailed. I then installed the strut in the car. That was easy, especially when compared with getting it out! I heated the copper hydraulic sealing washers red-hot with the acetylene torch and quenched them in water, thus annealing (softening) them, and attached the hydraulic hose. I put a quart of the special hydraulic fluid ($12) in the tank and started the engine, and manipulated the leveling valve. When I next looked the tank was empty, so I put in the second quart. The car then started going up and down with the valve. No sign of leaks. I reattached the control link to the valve and took the car for a drive. It worked fine, except that I'd forgotten that we didn't have snow tires yet and I managed to put us into a ditch while trying to turn around on a rather icy patch of shoulder! A kindly neighbor pulled us out. Once home again I put the well-worn Hakkapeliitta 1 snow tires on, cleaned up the work area, and put the car away. Still no sign of leaks. I need to put the rear seat back next.

Somebody on the mailing list suggested:

Wonder if the Astoria Flexx boot for rack and pinion units would work?

http://www.astoria2000.com/fb4000info.html

I used their CV boots on my 300D and they are holding up fine so far.

That looks pretty interesting!

Monday, January 10, 2011

Everything still looks dry this morning, so I closed the access holes. First I had to glue the torn EPDM seal of the non-circular access plug, MB P/N 115 693 00 30. I cleaned it with brake cleaner and used cyanoacrylate glue. A bit of teflon spray and a rubber mallet took care of installation. The seat frame and back was next, after I replaced the seat heater relay and rear audio amplifier in their retaining clips. The seat back was very recalcitrant, getting things lined up so that the (five) bolts went into their holes was surprisingly difficult. It was easiest with the seat frame fully 'reclined'. I ran out of time to finish putting in the seat bottom, but I expect that to be relatively painless.

...I stopped at Les Schwab this afternoon and had the tire pressures checked. He said they all were a bit low. I put in a quart of ATF because it was shifting poorly. That helped a lot. Stupid leak.

Tuesday, January 11, 2011

I finished putting in the back seat. It went smoothly. It's odd that there are no captive nuts for the two retaining bolts, but with the seat reclined it's no problem to get a backing wrench in there. I left the center belts buckled and tucked underneath the armrest where they can be easily retrieved. The car's fluid levels were fine, no sign of drips underneath the repaired strut. The car's ready to give back to 'she who must have her butt warmed'. Just in time, another arctic blast is coming through. (8 °F this morning.)

Thursday, January 13, 2011

Wretched POS! My wife came to pick me up at lunch, and just before she got there she called me saying there were banging noises coming from the car. She rolled up, and there was steam rising from the hood. I popped it and had a look, and the washer tank was boiling. Weird! I'd guessed that the washer tank thermostat had failed open, and the car was boiling off the fluid. The engine was hotter than normal, but not in the danger zone. (Odd, in winter.) The radiator was cool to cold. The coolant tank appeared normal. We got in and went a block or so to lunch. (Evil intersection, hate traversing it on foot.) The banging noises resumed, and were coming from the console. While eating I thought about it, nothing added up. Afterwards I popped the hood and had another look. I opened the coolant reservoir, and what I'd thought was a visible level was just a stain in the tank, it was empty. 1.5 gallons of water into the reservoir later and it's full. Low coolant! Where did it all go? I have seen no sign of coolant leaks. Why did not the low coolant light come on?

Obviously the car lost its coolant, somehow, and gotten low to the point that radiator flow was disrupted. Enough was left to carry heat to the washer tank, which was boiling off, and coolant was boiling in the heater core. Very much not good. Perhaps the engine was not damaged, or perhaps it was already damaged and that's what started all this?

At least the suspension was still OK.

Friday, January 14, 2011

I took the car to work today, and noticed when I got there that the coolant level had dropped a bit, and the washer tank level had risen. Mystery solved! I grabbed some suitably-sized bolts from the lab, wrapped some solder in the grooves, and used them to plug the two hoses to the washer tank heater. That ought to hold it until I can fix it properly. I stopped and bought another jug of Zerex G-05 coolant. $15. (It's gone up!)

Monday, January 17, 2011

The MB P/N 126 830 07 84 thermovalve in the washer tank is known for leaking. I removed the washer tank from the car. Once the pumps were removed from the tank the heat exchanger could be removed from it. The plastic thermovalve had popped apart, there is a metal retaining ring around one end that is heat-staked to the plastic body, it holds the valve assembly in. This was blown off the end of the body and all the valve guts were rolling around inside the tank. The cooling system was freely open to the tank, no wonder there was a problem!

The design looks weak to me, it relies upon the eight little heat-staked plastic pins to hold the ring on against coolant pressure, and the action of the spring-loaded wax cartridge. It was probably fatigue failure, the thermovalve may or may not be reclaimable.

I tested the low-level sensor and it was fine, once it had been cleaned out a bit. (Got a bit gunky during the boiling coolant episode.) I ordered (Rusty, 1-800-741-5252) a new thermostat, it's easier than trying to figure out how to hold the old one back together, and fussing with it to see if it works. I also ordered new rubber tank seals (4) to replace the dead/dying ones, and a couple of quarts of suspension oil.

The washer tank was pretty slimy inside, and full of nooks and crannies, so I ran it through the dishwasher. That worked well because the access hole is so large; the slime was gone.

Thursday, January 20, 2011

It had turned cold in the last couple of days, so I left the car parked inside as I haven't dealt with the coolant yet. (The coolant level looked good, no significant leaking.) This morning I vacuumed out the crevices at the firewall, there were a lot of leaves and dirt built up. I tested the two washer pump motors by clipping them to the battery and they both ran fine, though the headlight pump was noisier. I replaced the LF parking lamp, which has been bad for awhile. I cleaned out the trunk a bit and found the extra suspension pump seal for this car, and the steering seal kit I'd bought for the 380 SL.

...Today at the junkyard I got a replacement driver's-side seat belt. (From a 300E, about $5. They also had a nice 126 280SE in Euro trim, a tidy little package with manual cloth seats, crank windows, no airbag, and manual dual-zone HVAC. It did have AC and a sunroof, and central locking. The 2.8 I6 in the engine compartment was a very nice fit, belying the 500SE badge on the trunk. Looked like it had once been a nice little ride. Far gone, now.) I can now move the passenger's-side belt that's on the driver's side over to where it belongs, and put this one in its place. That should get both seat belts working with correct-vintage and correctly-oriented swinging shoulder mounts.

Friday, January 21, 2011

I washed the new seat belt. It has a 124 part number, I hope it will fit!

...The washer thermostat came today, as did the tank lid grommets (MB P/N 010 997 13 81) for its plumbing, I can begin reassembly tomorrow. (I can't finish, I didn't get the pump to tank grommets yet.)

Saturday, January 22, 2011

The new thermostat is also made by Behr, but they've changed the retaining mechanism to a large screw-in plastic ring; this ring looks like it might be heat-staked in place. It looks more durable than before, I suppose, and yet cheaper. It turns out that the old thermostat's plastic locating pin (which mates with a socket in the MB P/N 126 869 08 20 tank) was broken off and missing. One surprise was that the two square O-ring pipe seals to the thermostat are not included with the thermostat, I had to reuse the old ones. At least they looked to be in good shape. It was surprisingly difficult to get the heater assembly properly located in the tank, that locating pin was recalcitrant. Once positioned exactly right, with my hand wormed into the tank, it slipped into place—and I even could get my hand back out! (The pumps definitely have to be out of the tank to do this operation, there's a heater loop that surrounds the pickup points.) Next in was the level sender (MB P/N 126 540 10 17), that's easy to do because of its narrow neck section. The big rubber tank lid seal was still in good shape, I pulled it off and cleaned it somewhat, it was still nicely flexible. The new tank lid to pipe grommets were a bit tight, but I first worked them into the lid, then worked the pipes through them. Saliva makes an excellent assembly lube for this kind of thing, if you can get past the pretty nasty taste of the various parts and residues. The lid snapped over the tank lip easily and solidly. The filler cap (MB P/N 123 869 01 72) and its tether (MB P/N 126 869 02 14) are still in good shape. The tank is ready to go, except for the pump grommets (MB P/N 123 997 36 81).

I then swapped out the driver's seat belt, the new 124 assembly seems to be symmetrical and can swing both ways. Regardless, it fits and works better. I then moved the old belt to the other side, for which it had always been destined. I don't think it fits as well, even though it swings the correct way. No worse, though, than the one that was there, so we will call it good for now. While I was there I hid the cell phone amplifier's antenna wire behind the B pillar cover. That's a lot tidier.

Wednesday, January 26, 2011

Swapped the wonky LF tire for one of the summer tires. We'll see if that cures the wobble completely or not. (The tire has an obvious bulge when you spin it while jacked up. I think this is the last of the original tires.) I also installed the washer tank into the car, heater pipes and all. It's going to be dry since there are no pump grommets yet, and the point is to see if it stays that way in operation.

Monday, January 31, 2011

Called (again) about the AWOL new parts. No sign of leaks into the (still-dry) washer tank.

Oh, and the one tire is definitely bad, removing it from the car seems to have cured the problem.

Tuesday, February 1, 2011

Yesterday the pump grommets finally showed up, along with the suspension oil. We really needed this car and its heated seats today, so I got up early and had at it. (It was 9 °F, and dropping, when I got up. I think it made it down to 8 °F before it turned around.) I first installed the two pump grommets, that went well (again using saliva, phhhhpt!), but the hose to the headlights leaked. I removed it and cut off the stretched-out end, and the twist of stranded electrical wire somebody had used in lieu of a proper hose clamp. I then used the heat gun to warm the cut end and slipped it over the barb. That and a small hose clamp from the junkbox cured the problem. I topped off the tank with washer solution. Done! Eight pieces of rubber involved in this tank assembly, and I only replaced four of them. Let's hope that's not a mistake! (I doubt it will be, there's been no sign of leaking into the tank, and while it was tipped up for the hose repair there was no sign of leaking from the submerged snap cover or level sender gaskets.)

Next I drained the radiator and put in the gallon of Zerex G-05, then topped it off with water. I had to jack up the car to do this, to fit a bucket under there to capture the drainage. I would have liked to have done another full flush to ensure that all the windshield washer crud was out, but that's far too involved.

Next was the leaking suspension pump. I removed the fan and the AC idler pulley, then the pump. I removed the old high-pressure O-ring and cleaned its channel, scraping off the tiny adhered rubber bits with a jeweler's screwdriver. I went over the sealing surfaces pretty well and cleaned them with brake cleaner. There is one small imperfection in the channel, but I think the O-ring should seal it nonetheless. I then attached the head to the pump body with the two short bolts, being very careful to get it together cleanly. I then used grease to stick the block gasket and drive spider to the pump, and put the pump back on the engine. As always, this is harder to do than you'd like. You do have to get the low-pressure fitting threads started a bit before and/or as you attach the pump to the block; you'll never get them started after you attach the pump. It went easier than some of the times I've done this.

I then reassembled everything. The AC idler pulley bearing was getting 'dry' again, so I oiled it with M1 gear oil. A 24mm wrench is used to tension the belt before tightening the 17mm retaining bolt, but it doesn't really fit well because of interference with the power steering pump. What should have been an easy task was much harder as a result.

I then topped off the engine oil, power steering fluid, the radiator (again), and poured another quart of suspension oil ($12) into the reservoir, and started the engine. Everything ran fine, but after I stopped it I could feel suspension oil on the bottom of the pump again. Damn! I felt around and determined that it seemed to be the high-pressure fitting leaking. I'd reused (of course) the aluminum sealing washers on the banjo bolt, and I think they're leaking. It's possible that this was the original source of the leak, but I thought I'd checked for that in the first place. (If it was, oh well. Due to an order mix-up I'd ended up with an extra high pressure O-ring seal anyway, and it only cost me the time to install it.) I may need to try re-annealing these washers. I tried loosening the banjo bolt and wiggling it back and forth, then retightening it; we'll see if that helps any.

Wednesday, February 2, 2011

So I've been driving this car lately and it seems to me that it has one other odd behavior to go along with its variably-high and sometimes rough idle: as it's warming up it is somewhat puny and rough running, but as the engine temperature gauge approaches normal operating temperature it's almost as if a switch is flipped and the car surges forward a bit and smooths out. It's more responsive to the throttle and stronger, you have to back off the pedal a bit. I'm not certain, but it may be that the idle is not really that high until then. I'm wondering if one of the engine warmup sensors is off, or if what it's hooked to is broken or maladjusted. I should look into this sometime.

Suggestions from the list:

What if it is woefully 'out of tune', but switches from open loop to closed loop mode at a certain temperature, checks the O2 sensor and adjusts itself?

I think your car has a WUR? Maybe it's sticking a bit. I believe it has a bi-metal strip and an electrical connection.

Daughter's 380SL ran fast at idle and variable speeds. We found the timing way off, and fuel turned up high.

Friday, February 4, 2011

It's official: I'm starting to hate this car. My wife went to pick up our son from school, and called me to say that the car was dripping. I had her drop by so I could take a look. Coolant, from the transmission area, a pretty significant flow. (The level wasn't really down much, though.) My guess is that the heater core is leaking, probably from the boiling-hot hammering it took, and it's dripping out the condensate drain. There's another possibility or two, though, more investigation is required. I'm not happy!

Wednesday, May 11, 2011

Wretched car. I put it up on ramps and started it, let it get good and warm. It was like a gentle warm rain under the car, all the various fluids dripping from above. The most immediately disturbing, and the last one to start, was coolant. I had thought that the heater core was holed and this was coming down from the condensate drains, but I no longer think so. I could see the drains pretty well from below, and they were dry. The coolant, though dripping from the front of the transmission, was coming from well forward of that point. It was very hard to tell, but it is definitely dripping from the head at the rear corner of #4. I can't really see if it's coming from above there, it may well be. Or not. Can the head leak coolant readily from there? I tried to examine all coolant hoses back in the area and all seemed dry, but of course you can't see everything 100%. Head gasket? The car did get pretty hot when it lost its coolant through the windshield washer tank. Did the head crack? The block? Time to remove the heads? (Job 01-415, doesn't look that hard when spelled out in the manual. I'm sure it's a lie!)

There is ATF everywhere back at the pan. On everything, especially the exhaust pipes. And dripping. It's so messy I can't even tell from where it's originating.

Power steering fluid, of course. But that's the normal bad seal weeping. The least of the problems I'd say.

And something clear-browny and runny dripping from the ATF cooler line where it straps to the oil pan. But it's not red, I think this is suspension oil running down from above and picking up a lot of dirt/grime along the way. I can't really see where it is coming from, but the two fittings on the pump seem dry enough, though the bottom of the body is wet with suspension oil. I've re-sealed that twice, I probably need to get another pump. (I did note a flaw in the sealing surface of the pump body.) That won't be easy. That may not be the only leak in the area, the suction line looks like it joins a rubber hose, it looks pretty wet there.

I also noted that the idle jumped up from what it ought to be once the engine had warmed up. It was sudden, like one of the warmup sensors is somehow being misapplied. That'll bear investigation.

Wednesday, December 14, 2011

This thing has been occupying valuable garage space for far too long. It's going to sit outside, at least. I put the battery on charge, it had gone flat. Initially it didn't take any current, but it started drawing after awhile. We'll see if it's ruined or not, I really need to disconnect the battery on any car that is going to sit like this.

Saturday, December 17, 2011

I started the car, it was reluctant but then was fine. I had to put a quart of ATF in it before it would move forward, but then I was able to move it down and around back of the house out of sight. I disconnected the battery.

Friday, March 30, 2012

I give up. We need this car either fixed, or gone. I took the car back to see Fernando at Motortech, this time to see about the coolant leak (and perhaps other things). Somewhat surprisingly, it made it there without incident.

Thursday, April 5, 2012

Fernando called, and said there were no visible leaks from the engine, nor did his combustion gas sniffer detect any leakage into the cooling system. He said the transmission leak was mostly (at least) from the rear pump, and that this was an easy fix. He's also going to look at the suspension system, paying particular attention to the hoses.

Thursday, April 12, 2012

I called on the car. He'd resealed the transmission and put the 'good' stop-leak in the cooling system, just in case. Said it was driving OK. He said the suspension pump hoses were not leaking, but that the pump probably was. He had a used pump, I asked him to try that. He's also going to replace the belts (shot) and the motor mounts (also shot).

Friday, April 20, 2012

Picked up the car. The bill was $1065.55, which I tried not to think about. The breakdown:
  1. Cooling system diagnosis. He found no sign of combustion gases in the coolant, nor signs of leaking. To be safe he put the good (NAPA) stop-head-leak stuff in anyway. $80 for diagnosis, $19 for the goo.
  2. Re-sealed the leaking (rear?) pump on the transmission, this can be done in place. $120 labor, $25 O-ring, $19 for fluid.
  3. New motor mounts, the existing ones were complete crap. $90 for the mounts, $140 labor. (I'll be able to put the fan shroud back on now that the engine's sitting in the right place.)
  4. New belts. $74.20 for the belts, $80 labor.
  5. Used suspension pump. Between his used pump and my new(ish) seals he got it to stop leaking. He said he had to take the pump off three times, and he steam-cleaned the front of the engine. $200 for the pump, $180 labor.
This totals about $440 in parts, $600 labor. (The rest is tax.)

I drove the 380 SL over, and swapped cars with him. (He'll be looking into its plug fouling problem.)

I returned to Spokane and tried to get it licensed, but its intermittent too-high hot idle speed made an appearance and prevented it passing its mandatory stink test. (They wouldn't even try, but at least there was no charge.) Crap.

Saturday, April 21, 2012

I swapped out the snow tires and put back the B pillar cover on the passenger side. Too bad that's not all that was left to do to return this car into service! I then removed the air cleaner and the idle control valve. While I was there I took their hardened (and broken, and glued, and glue-failed) rubber mounts and cleaned them, then tried gluing them with JB Weld. We'll see if that holds any better than the Shoe Goo did in the engine heat. It probably will not, I just need to break down and buy some new ones.

The list of things that might cause a high idle are legion:

  1. Air leaks.
  2. Dirty/faulty idle air valve.
  3. Bad overvoltage protection (OVP) relay.
  4. Faulty idle control computer.
  5. Bad Idle/WOT throttle switch.
  6. Bad ignition timing.
  7. Bad engine temperature sensor.
  8. Stuck rear cigarette lighter. (Really? Well, these weren't.)

The idle air valve seems to work fine. On the bench it responds nicely to voltage, about 6 V is enough to cork it off completely. It does respond linearly, to a degree. Seems fine. However, on the advice of counsel I pried the plastic cap out of the end and found the screw threads that are supposed to be there. I am, however, finding it difficult to fit a bolt into it. It's 5mm, apparently, but the thread is a finer pitch than anything I've tried so far. I managed to find a bolt that threaded in far enough that I could pull the plug out some with pliers, this reduces the internal spring tension making the valve easier to close. The plug came out to flush with the housing, which is slightly farther than I intended, the plastic cap now sticks out a bit. I measured the valve on the bench and it now corks off with about 3.5 V, so we'll see if that helps any. I can always push it back in if I have to.

I removed the fan and the upper radiator hose and reinstalled the fan shroud, which has been laying next to the garage for a year or so. With the new motor mounts there now appears to be plenty of clearance.

I did start the engine with the adjusted idle valve, and it was able to idle. The idle speed was somewhat variable, but never too high. This doesn't mean much until the engine is warm, however.

I opened up the OVP relay, it is glued together with RTV unlike the older models. You pretty much have to destroy a lot of the red plastic cap in order to peel it off, from there you can peel/pry enough to pry the guts out of the aluminum shell. With that done I could see that the OVP relay looked pretty good inside. The glue job has kept everything clean and bright.

Sunday, April 22, 2012

I resoldered the OVP and put it back in the car, and started it; the idle was where it belonged. I put the car back together, the air cleaner is a real pain to put back as the crankcase breather hose doesn't fit well. (This engine could really use some new rubber bits.) One glued rubber mount tore apart going back together, but that was because it was the wrong kind, and was too short anyway. I did end up replacing it with a good used one. (Once I was able to find it in the parts pile, that is.) The mount for the idle air valve also tore apart. Gluing these things is pointless, but I thought I'd give it a try since I was there. I took the car for a short test drive and it behaved itself, the idle was low even when it was hot when I got back to the house. (I'd been running the AC, which worked nicely, the outside temperature was 77 °F, this was the first really warm day we'd had this year.) Between the air valve adjustment and the OVP it seems to have done the job, but I don't know which one might have done it. (Probably the air valve.) I think we'll be able to get the car tested and licensed tomorrow.

Monday, April 23, 2012

It passed its stink test with ease, and I got it licensed. One disturbing thing, as the day got hotter the car started running poorly at idle, enough to die many times today. As I had swapped with Jill this did not please her much. I need to dig into this, and I'll be driving it until it's resolved.

Wednesday, April 25, 2012

Yesterday was cooler so the car didn't act so stinky, but it was definitely not right. This morning I had a chance to check the air metering plate, and it seemed to be catching a bit on the metering bore. That's not good. I probably never should have removed it two years ago, even if it was filthy inside. It's supposed to have a 0.1mm (0.004") gap around all sides at its tightest point. It was/is surprisingly hard to put back right, every time I used the feeler gauge I couldn't get it to be right at all points at once, and it doesn't take much of a shift when wrenching it to make it catch or drag. (If it does catch the mixture at idle will be completely wrong, but not at any higher RPM's where the bore opens up, which matches its recent symptoms.) Today I figured out the trick. I measured a sheet of copier paper at just about 0.004", so I wrapped one around the metering plate while I pulled it up to the tight point and tightened the bolt. It wasn't quite long enough, there was maybe a 1.5" open spot along the edge, and that was enough to let the plate scoot into it and drag. I tore another strip of paper to fill in that gap, and then the plate centered perfectly, and stayed that way while I tightened the bolt. There was no more catching when I tested the plate's travel.

I also found my pile of salvaged air cleaner mounts and replaced the other one, whose glue job had also failed. That's better.

I aired the tires and added some coolant to bring it up to the correct level. Might take a try or two before it stabilizes.

On the way to work the car performed normally again. At lunch, quite a bit warmer, Jill and I took it out, and it was still fine, even with the AC on. Fixed? I think so, at least for now. We swapped cars again, since she'd much prefer driving this to the truck.

Thursday, April 26, 2012

Jill reports the car is still dying at idle, but much less frequently. I drove, at lunch, and it died a couple of times on me when we started out. (But not thereafter.) Yeah, there's still something going on, though it's a lot better than it was.

Friday, April 27, 2012

I checked the plate's position again, and I thought I heard a faint 'ping' as I pushed it down. I loosened the bridge and I didn't seem to hear it anymore, so I wonder if there was some distortion of the air horn that caused a small catch? I left the bridge screws only slightly tight, we'll see if that makes any difference. I also aired the tires on the left side, which seem to have leaks, probably rim leaks, and I topped up the coolant level.

Wednesday, May 2, 2012

Another quart of coolant. (Water, this time.) Still going down? That's not good.

...Jill called me today and said the car was hissing and emitting steam from the hood. By the time we could switch cars it wasn't doing it again. The (hot) coolant level was still OK.

Monday, May 7, 2012

Still mostly behaving. The tranny was slipping on corners and I found it a bit low so I put in 1/2 quart. I wonder if it's still leaking? This is the first time I have checked the level since the operation. It's possible that it's being sucked out the vacuum modulator.

Friday, May 11, 2012

I stopped at Les Schwab this afternoon and had the leaking LF tire dealt with. Bad chrome listed as the cause.

Wednesday, May 23, 2012

Yesterday I bought some fluorescent dye for the cooling system at NAPA, about $2, and this morning I poured it in and washed it in with a bit of water. (I also bought another jug of G-05.)

Friday, June 1, 2012

The front doors have been creaking, so I thought I'd try something that is occasionally successful: I washed the door with Simple Green where it meets the heating duct and the sill trim, then smeared on a very light coating of Vaseline.

...Today was warm and I was driving around town at lunchtime, and I again observed it leaking coolant. This time I was able to see it apparently welling up around a large (19mm) bolt head on the rear of the righthand head, just inboard of the valve cover and right next to the coolant pipe to the heater system.

I also noted that the front door creaking was entirely gone.

Monday, June 11, 2012

The car vomited a great gout of coolant underneath itself today at work. Green tint was all over that rear corner of the engine, but still no obvious source. Spray? Vaporization? When I got home after work there was no sign of leakage, and I pried on the hose that is there, engine running, but no drips or sprays. The 19mm bolt head in that corner was also tight. Very puzzling!

Tuesday, June 12, 2012

Good news and bad news. I finally caught it leaking coolant when I got home from work. I popped the hood and was staring down at the (dry) back of the engine, wondering what to do about this intermittent problem, when "Psssst" a pencil-lead-sized stream started spraying out the side of the rubber hose that connects the back of the engine to the HVAC stuff between the firewalls, onto the engine! So it's that hose, and not the head, etc., that has been the problem. The bad news was that my attempt to relieve the pressure in the cooling system to prevent further coolant loss went awry when my fingers slipped and the cap shot off and down next to the hot engine where I couldn't retrieve it easily. I had to watch an expensive coolant geyser pretty much empty the cooling system over the next half minute or so, vomiting gouts of bright fluorescent green all over the place.

Sigh. I retrieved the cap, washed the green off of the engine compartment with the hose and lowered the hood in shame.

Wednesday, June 13, 2012

Ordered parts. Coolant hose, suspension spheres, one jug of the oil, plastic drag links. Also plastic connector shells for the idle air actuator and coolant temperature sensor to replace the broken ones.

I decided not to drive the car, I might as well take advantage of the low coolant situation and leave it emptied until the hose is replaced. No sense in losing even more coolant to this problem!

Saturday, June 23, 2012

The parts came Thursday, all but the oil, and today I went to install the hose. 126 832 28 94. After I removed the obscuring ABS controller I could see immediately that this was the wrong hose! This hose is for the left side of the engine, the faulty one is on the right side. Crap. I removed the faulty hose and could see the pinhole in it, it would ooze green coolant when squeezed, like a pinprick. I will have to order the correct hose, now that I know exactly what it's supposed to look like maybe I'll get it right. I haven't decided whether to return the wrong one or not, the other hose might not be far behind failure-wise. (This is a harsh environment, there at the back of the engine.)

So as not to waste the session I jacked up the rear of the car from under the springs and put a jackstand under the differential, then lowered the wheels to their full extension to reduce the pressure in the system to its minimum, and to take as much fluid as possible into the struts. I used ramps and blocks to put under the tires as a fail-safe. I then wire-brushed off the mounts and pipes of the accumulator spheres, at least so far as I could given the tight layout, and then sprayed PB Blaster on them and left it to soak.

I hit the (nasty) EPC myself, in Group 83 for the 126.039, and found a diagram of the HVAC water connections, and chose Item 59 from Sub-Group 180 (Diagram 10) as what looked like the correct hose for the right side of the engine. The EPC says this is a 126 832 12 94. (The hose I have is Item 158, from Diagram 12.)

I also checked the service manual regarding the accumulator replacement, and it says that the pressure in the suspension system should be relieved at the drain nipple on the level controller valve, and that the oil released there, if caught cleanly, can be reused. The other steps are all obvious, and they do caution to use flare wrenches in order to avoid damaging the fittings.

Monday, June 25, 2012

I ordered the correct hose. It's only about a $6 item, a far cry from the other (more complicated) hose!

Tuesday, June 26, 2012

I relieved the pressure on the suspension system this morning, an 11 mm wrench and my clutch bleeder hose was all that was necessary. About 150 ml of fluid came out before it reached the drip stage, I used one of the empty fluid bottles to catch it.

Wednesday, June 27, 2012

Yesterday the hose came, so I installed it this morning. I used Simple Green to lubricate the rubber so it went on easily, and it was a fairly straightforward process except, of course, that you can't get a screwdriver or a socket onto the inboard hose clamp. A 7 mm open-end wrench did the job, though slowly. I then poured the remainder of the jug of G-05 into the reservoir, maybe 3/4 of a gallon, and then a similar amount of water. Only a little water went into the reservoir, I poured the remainder down into the upper radiator hose. Once that started spilling out, of both the hose and the radiator neck where I held them mostly together, I closed the hose back up. That's the easiest way to eliminate the air bubble in the head. I did not run the engine to check for leaks, because I don't want to repressurize the suspension system yet.

Sunday, July 1, 2012

I installed the new connector shells on the idle air valve and the temperature sensor. As I found the car they were not the same kind of shells at all, but the ordered replacements both turned out to be 011 545 71 28, which fit and work. The idle valve's connector had been one of these, before leprosy set in, but the other one had been (incorrectly?) a Kindermann 9656. The new connector fits better, it latches on correctly.

I had a look at the RR side marker light that was out, and it was not the bulb. I used a battery charger to test all the lamps in the housing, and it's on Pin #1 of the connector, with a green/white wire. In-housing it worked just fine. A voltmeter showed that the harness was only supplying about 8 V, into the high impedance of the meter that is not too impressive. (The other marker light connection showed battery voltage.) I opened the connector and the connection looked good, so it's either the wire in the harness or the lamp-out module that is faulty here. Will take a more involved session than this one to chase this down.

I then tackle the oily nasty job of replacing the suspension accumulators (spheres). The penetrant, at least, had worked. The 11mm and 17mm crow's-foot flare wrenches were necessary, as was a 17mm backing wrench. A 13mm socket did for the three mounting bolts. I cracked one pipe fitting and then caught oil in the jug until it stopped streaming. Even relieved of pressure like that there was still a lot of leakage when I removed it. What a mess! I dumped the sphere into the jug, it seemed pretty full. I probed it with a screwdriver and there was no sign of the diaphragm, the new Febi sphere (123 320 02 15) had a prominent something-or-other right in the main fitting. The old sphere was obviously shot. It was fairly easy to replace, the secret there is to get both fittings' threads started before mounting the sphere to the car. You also have to first move the large compression fitting from the old sphere to the new, and don't lose the copper sealing washer! After that I tightened it all down, then moved to other side to repeat the operation. The only hitch there was that the mounting ear had gotten bent in storage on the new sphere, I had to remove it from the car to bend it back to where it belonged. All in all I recovered about 500 ml of oil, which I am supposed to be able to reuse.

Last was the (123 320 09 89) sway-bar links. The hard part there is getting the bolt started back into the brake backing plate. Other than the tediousness of that job it's quite easy, all you need is a 17mm socket and a 17mm open-end wrench. I then cleaned things up and came inside for lunch. Starting and leak-checking can wait 'til after that.

...Lunch accomplished I started the car and watched for leaks, nothing obvious showed up so I took it off the jacks and out for a spin. It drove properly, quietly, and I noticed nothing weird. (There were no significant bumps upon which to test the rear suspension, unfortunately.) When I got back I again looked for leaks, and saw nothing, so I buttoned things up.

Now, the car had been leaking ATF while parked, so I checked the level when I got back and found it a bit low, so I added 1/2 quart. The suspension tank level had dropped as the new accumulators had charged, so I folded a piece of new shop towel into a clean funnel and poured the recovered oil through it and back into the tank. Now the level is a bit high, as might be expected under the circumstances, but it should be OK.

Sunday, July 15, 2012

The RR tire was very low today, I need to have that one looked at.

Saturday, July 21, 2012

Jill has been reporting that the car will now die while on the road lately (not just while starting out or stopped at a light), probably when the throttle is let off. I checked the fit of the air metering plate, and it seems fine, both hot and 'cold'. Theorizing that the idle air valve (solenoid) might be biased too much towards 'slow' (when I adjusted it) I removed it and tapped the plug inwards a tetch. It still responds well on the bench, and in the car it was still able to idle at an appropriate speed. We'll see if this improves things, it may be that there's something else wrong, such as standard tune-up measures or the like.

I checked and topped off the AC charge. Seems fine, but couldn't get it to drop below about 60 °F, and it wasn't all that hot out. Odd. The center vent still seems to have a mind of its own.

Tuesday, September 4, 2012

We haven't been driving this car, but we wanted it today and so I resurrected it. The tranny had leaked down, I ended up putting in 2 quarts of ATF before it started moving around normally. Not too cool, actually.

Monday, October 22, 2012

Today I noticed that the temperature gauge was stuck on the bottom peg. When I hit a bump, or stopped quickly it popped back up. Sender connection problem? In the evening the heat cut off, matching the gauge. (It's been intermittently weak lately.) I figured it was just the used monovalve joining the party, but as it could also be a highly destructive low coolant issue I stopped to check that. It wasn't, but it's best to be sure.

Tuesday, February 5, 2013

I put the battery on charge, it was thirsty.

Thursday, April 18, 2013

Spring is basically here, and it's long past time to deal with that pesky RF tire that goes flat in a couple of days. I've been airing it all winter, and I'd even gone so far as to put the jack under it to save the tire from getting squashed. Today I took it off, and fought with the crappy HF tire changer until I got the tire off the wheel. I chalked the valve stem location on the tire before I removed it. The weird thing was that there was a 1/4" BB rolling around inside the tire. The leakage problem was, of course, the classic flaking of the chrome on the wheel, so I used the wire brush to clean the mounting flanges, painted them, and put the wheel in the shop oven to dry. (14" wheels will let the door close, 15" wheels will not. Sucky. I used some sheet metal strips to block the worst of the gap at the top of the door, maybe cut the power bill a little bit.)

Friday, April 19, 2013

The paint was dry and I reinstalled the tire. That was harder than taking it off had been! I got it back on, though, and clocked back where it had come off, and with the wheel weight installed back in the same place. It aired up fine, and I put it back on the car. We'll see how/if it holds up. I also put the car on charge, maybe tomorrow I can start driving it.

Saturday, April 20, 2013

The tire held air well, and so I aired the others and started the car. No problems. It didn't want to move, however, and a quart of ATF did the trick there. Definitely need a rebuilt transmission, maybe soon? It's also long past time to change the oil. Anyway, the car is ready to go except for license tags, which I can pick up Monday.

Tuesday, April 23, 2013

I was surprised to see that I hadn't changed the oil in 11kmi! The low-oil indicator was on, but I knew that the oil needed changing so I hadn't topped it off. Urgh. I changed the oil today, though I was bad and did not change the filter too.

Wednesday, May 1, 2013

I put in a bottle of Trans-X (by K&W) tranny snake oil, it's supposed to clean and swell seals, which I think is more what this transmission is needing rather than a viscosity modifier like Lucas. We'll see. ($8.14. The guy at NAPA said it's what the tranny rebuild guys put in if the rebuilt was expected to sit unused on the shelf for awhile.) I put in a bit more ATF too, it's been acting low.

...The transmission is definitely happier than it was. Worth doing—so far, anyway.

Friday, May 17, 2013

The last few days, and especially yesterday, the rear brakes have been making some horrid intermittent screeching as we roll along. Rock? Seemed worse than that, and it hung on for two days with some freeway trips thrown in, so it's time to take a look. I jacked it up and removed the wheel, and found what appears to be The World's Hardest Rock™: a little piece of half-flat pea gravel caught between the disc and the backing plate. Who knows how much longer it would have held on before finally disintegrating.

Sunday, June 30, 2013

Yesterday, on my road trip back from Spencer's memorial service, the engine sounded noisy, like the air pump was running. When I stopped and checked it looked like it was running, so I disconnected the plug to it which made no difference. Today I checked, and the clutch is all messed up. Air pumps (a.k.a. smog pumps) aren't rated for very many operating hours since they're only run for a minute or so at cold start, so I just removed the belt and called it good. While I was there I noticed that the top shock mounts were loose, the rubber mounts had collapsed and the nuts were out of travel on the shaft. I rustled up a second set of collapsed mounts and put them on too, which tightened things up.

The car's a lot quieter now.

Monday, July 15, 2013

Back from a week's vacation, and the car didn't want to really move forwards or backwards. I checked the fluid level and it was OK, and after that it started moving a bit. Once moving normally there were no more problems in that it acted the same as before. Weird!

Saturday, September 28, 2013

The heater's still not very functional, and lately I've been hearing clicking behind the dash when it's acting up. I've been relying on the seat heaters for comfort. But enough is enough, it's resoldering time! (It's also possible that the used monovalve insert has finally failed, too.) I removed the ACC controller and resoldered it. I first used the Dremel wire brush to remove what oxidation and crud that I could from the PCB. The secret here, as usual on these, is to scrape the reluctant leads with the hot iron until the solder sticks better. The two-lead components seem to be the worst for this, the IC's are all usually fine.

I also removed the scratchy fader and washed it out with soap and water, since it looked like it was full of dried coke/coffee, then I blew it dry. I used a dab of white paint to refresh the center stripe on it, let it dry, then used Deoxit fader spray on it.

I decided to try something I've been thinking about for years, I took a surplus flat red illumination LED (from one of my son's destroyed toys, in fact), and soldered its cathode lead to one of the ground pins on the top of the DEF switch, positioned and aimed so it'll shoot into the switch cap. (Lying right on top of the spring, just slightly proud of the edge of the PCB where the switch cap won't quite bump into it.) I wired the anode through a 680 Ohm resistor to the X1-9 pin that goes to the monovalve. (The LED needs a bit over 2 volts, and I aimed to keep it at 20 mA or less, which would call for a 500 Ohm resistor. 680 is what I had plenty of in the junk box.) If this works there will be a detectable red glow behind the DEF switch whenever the monovalve is unpowered, which means that heat is applied. The LED will be powered through the monovalve, but at only about 20 mA, not enough to affect the valve (I hope). Energizing the monovalve, cutting off the hot water, will thus also result in the anode of the LED being at cathode (ground) potential, and no light. We'll see if this works. (I had hoped that I could use the blue side [it was a dual] to tie to the AC compressor output, but the LED had a common anode lead, and that won't work here. No real problem, I was running out of time and needed the car, and I'm not sure of what circuitry I would need for that anyway.)

Sadly, I managed to break the temperature control dial's housing while taking things apart. I had to glue it back into place, which I hate to do. I used some light dabs of Shoe Goo, hoping that it'll hold yet be reversible if necessary.

The ashtray lamp was burned out, I replaced that while I was in there. The secret to removing the 126 console panel (fader) is to pry out the trim ring on the shifter first, it pins the console panel in place, preventing it from sliding forwards and releasing from the rest of the center console.

Driving off in the afternoon I could just see a dim red glow behind the switch in the daylight, once up to temperature it started blinking as expected. In the dark it was plenty prominent but not too bright, we'll see if the blinking becomes a problem in time or not. The heater was working perfectly, as it has not for the last year or more. The monovalve is in the clear, assuming no further troubles.

Friday, October 4, 2013

The heater's been working pretty well, certainly better than it did, but I wonder if it's completely right yet. At times the heat seems weak, yet the monovalve is being cycled. The fan speed is higher than it ought to be at those times, probably because the core temperature is lower than it should be. Could the monovalve itself be a bit bad, too, and not always letting through the gush of heat it should?

Also today I experienced something new. The heater was off as it was a mild evening, and then I heard a 'chunk' behind the dash, and I started smelling, then feeling, heat. When I looked the monovalve LED was on steadily and the recirculation LED was blinking. The ACC would not respond to any control. After a bit I killed the engine at a stop and restarted, and all was normal again. Obviously the ACC had shut itself down and reverted to failsafe defrosting on ram air alone, but that's sure a new one on me. The thing is, it didn't just stop working, it knew that it had stopped working, and was flashing the LED to call attention to itself. So what was so dire that it thought it wasn't even worth trying to operate?

Friday, November 22, 2013

The engine temperature gauge has been flaking out a lot lately, so I popped the hood and had a look. The wire pulled right out of the connector, it had corroded through. I cut off a bit and removed some insulation, scraped it off with a knife, and soldered the connector back on. I was very careful when taking apart the plastic shell not to break it. It was in the teens outside, rather cold, so I used the hot 85W iron to do the work, I don't think the regular size could have managed it. The insulation on the wire was very brittle, I slipped an inch or so of heat-shrink over it before putting it all back together. I also used a dot of Deoxit on the pin.

It's also been acting weird at cold-start, like it's not warmed up enough and running with retarded timing for too long. So I tried to clean up the connections to the other temperature sensors on the engine. It was so cold, though, that I had real trouble with cracking of vacuum lines, wiring insulation, etc. These things, fragile during warm weather, were really bad. I don't know if I helped or not, I'll be lucky if it still runs!

I did break off the EZL engine temperature connector shell, P/N 012 545 24 28 (internal #34611). I should get a new one.

Monday, December 2, 2013

Finally we've had a conjunction of cold and wet; snow and ice are here. Time to retire this car in favor of the Frankenheap. I'll miss the seat heaters! It's been running so poorly when it's cold, though, that I might not miss it much.

Friday, January 31, 2014

With the wreck of the Frankenheap I needed to drive another car. I tried to get this one started, but it would do naught but cough, even with ether. Must be a spark problem. Too bad I wasted all that time shoveling it out and getting the snow off of it. It never did like the cold.

Tuesday, April 1, 2014

Time to put away the Frankenheap for the year, and time to get this one going again. I put the battery on charge, jacked up the passenger side very high, then aimed the kerosene-fired torpedo heater under there at the engine. I let it cook for 20 minutes, and it started right up. No problems. It was low on ATF again, said the puddle under it, so I put in a quart. After that it would move again. I replaced the one bad windshield wiper with one of my NOS Trico spares, and buttoned everything up.

Friday, April 4, 2014

Car's running pretty ratty, so when I got home I left it running 'til I could pop the hood and assemble the tools. I then killed the motor and pulled all the spark plugs while it was hot. (I had tried this last year, cold, but they seemed pretty seriously stuck and I didn't want to risk stripping out the holes.) Some of them came out tough, but they all came out. I sprayed each one with PB Blaster before putting the (cold) wrench on them. I guess it helped, because they all came out without damage. I didn't look at them too closely, but #8 was pretty sooty.

Saturday, April 5, 2014

As #8 was fouled, and the EGR seems to feed back around there, I checked it. Seems to pass my .410 gauge test now. I sandblasted the worst two plugs and put them back in, with a bit of anti-sieze this time, and went for a drive. (I note that these were all resistor plugs, and should not be.) No difference, still running like crap. I parked and left it idling, and momentarily pulled off the wires on the 1–4 side, each reacted. When I pulled off #8 there was no difference, so I shut it down and got out the multimeter. Its plug wire was open-circuit. Others were equally bad on the meter, but I know that at least some spark was getting through some of them. It's time for new plugs and wires! I pulled them all out of the car. I had a junkyard set, Bosch, but they didn't fit right, and if anything were worse on the meter.

Friday, April 18, 2014

An uexpected day off, and all the parts are here, time to fix! First was tbe new non-resistor spark plugs. NOS Bosch W9DC0's, apparently NLA. $28. There are alternatives, but these are the 'real deal'. #2 was a problem, it wouldn't seat all the way. I think the PO had not seated it fully, and the threads are all clogged. I took one of the old plugs and ground a slot in it with the Dremel, then used it as a tap to clean it out, with PB Blaster as a lube. Quite a number of insertions, twisting in against scary resistance, and then removal and cleaning finally got the thing to seat, then I put in the new plug. Next were the new Beru wires, $159. The original wires had # labels, but they are non-transferrable. They also were sleeved, and more customized as to length. I installed the new wires, and used inner-tube rubber and tie-wraps to make protective sleeves. Getting access to the coil to replace that wire was difficult, but I eventually prevailed. Next was the four dead rubber air hoses (two on the valve covers and two on the idle air valve) and the mount for the idle air valve. They were no real problem. #116-094-07-91 $14.50, #117-094-08-82 $5.75, #117-094-09-82 $11.50, and #117-094-12-82 $7, all OE. The standoff was aftermarket, $4.50. After this I hit the key and the car started right up, and idled fairly well, much better than before. I had to put in some more ATF before the car would move, but that's not unusual. All this took about three hours.

Saturday, August 2, 2014

In the last few weeks I've been noticing a slight squeal from the right side of the car, perhaps from the rear. In the last couple of days it started making a scraping noise, brakey in nature, and so today I got a chance to jack it up and have a look. The bad noise was easy, there was a nicely glazed half-rock lodged in the caliper. The more subtle noise is worse: the wheel bearing is going out. This is distressing, because I'd had it replaced approximately five years and 23,000 miles ago. I suppose it's long past the warrantee, but still.... I had expected it to last the remaining life of the car.

Tuesday, August 26, 2014

Dropped the car off at the shop. Needs another new RR wheel bearing, and tranny rebuild. Fernando does his own rebuilds, let's hope it's good. (Says he was factory trained in Germany.) Here are the symptoms as I recall them:

Wednesday, September 10, 2014

The shop called, he's put a used transmission in, from a donor with about 130,000 miles on it, and says it's working great. He suspects that the wheel bearing may only be loose, so he's going to check into that. Still waiting for a seal of some sort, otherwise.

Wednesday, September 17, 2014

I picked up the car. $1500 for a used transmission and the rear wheel bearing tightened. Maybe not a great deal, but it's the one I had. The car seems to drive normally again. I did have to reset the clock and apply the radio code, apparently they had to disconnect the battery at some point.

Wednesday, October 29, 2014

The car has been running worse and worse lately. Intermittently. Feels like a misfire at low RPM's, it's pretty much fine when revved up. It's back to dying at times when trying to start out. I believe I smell gas when it's acting up. Frustrating, especially after just putting a transmission in it.

Today on the way home from work it completely cut out, at speed, twice. (That's new.) I was able to pull out of traffic on momentum and get it started again, then I made it home, with only the usual amount of pissy behavior, bucking and snorting.

I'm thinking bad connection in the ignition system. Somewhere. That covers a lot of ground, including the ignition switch, fuses, common ground points. Also a whole lot of the innards of things like the ignition module, coil, etc. (I recently put in new plugs and spark wires.)

I hate gas cars.

Sunday, November 9, 2014

I finally had an opportunity to dig into the car a little bit. With the air cleaner removed I found that the EHA valve is leaking. I went to my used stash and got another one, along with two used O-rings for it. I also unplugged the 4-pin temperature sensor and the cold-start valve, I've been thinking the sensor might be malfunctioning, causing intermittent timing degredation. We'll see if all this makes any difference on the next trip out. The CEL light is now coming on, methinks it is not happy! Plugging the sensor back in while it's running results in a lower, lumpy idle RPM.

I definitely need a new RH valve cover gasket, the old one is rock-hard and leaking.

Monday, November 10, 2014

It snowed a bit last night, and this morning it was 30°F out there. I believe our unseasonably-warm Fall is over! n

I put back everything I messed with yesterday. Yesterday's driving did not show sufficient improvement, and in many ways it was worse. It died a lot more than I'm used to.

Monday, November 17, 2014

Car wouldn't start in the morning. It was 18°F, not as cold as other times when it started fine. Came back at noon, when it had moved up to around freezing, and still no go. Starting fluid made no difference. Would cough occasionally, but no real fire. Sigh... I really want to be driving the Frankenheap, but I haven't had the time to get it ready to go again. I used the truck instead.

Monday, February 9, 2015

I started driving this car again. It started OK now that the cold winter weather seems to be over. It doesn't run very well at times, and it smells very gassy.

Thursday, March 5, 2015

I ordered a new EHA fuel valve from AutohausAZ. $266.04, ouch! The one that's on there is leaking gasoline onto the top of the engine, so it definitely needs replacing. Used valves from the junkyard aren't a particularly good value!

Friday, March 13, 2015

The parts came yesterday, so today I installed the EHA valve. Bosch part number F 026 T03 002, with associated numbers 453 and 250. It fit nicely, and matched in size and shape. I used the new O-rings that came with it, but kept the old slotted screws instead of using the new Torx screws that came with it. It didn't seem to leak any when I ran up the fuel pressure, so that's good. Let's hope that this cures the gassy smell, and the fire hazard.

While I was there I pushed on the air metering plate, and I felt a bit of a scrape as it went down. Not good, the plate was not centered properly. This has been a persistent problem, which I last worked on three years ago. I removed the plate, and cleaned it. The area is just a bit too dirty for my taste, I wonder if there's something wrong with the air filter? Anyway, I fiddled with the plate by hand to get it centered, using a bit of sticky clay as a handle for shifting the plate while I used the wrench to loosen and tighten the bolt. This is a very fussy operation. Once I got it to a point where it doesn't seem to hang at all, and looked as centered as I could make it, I tightened it down. It seemed to move freely, without any scraping. I started the car, and it started and ran well, so I guess we'll see. I put it all back together, ready to go to work.

Sunday, March 15, 2015

Today the car wouldn't start to take us back home from the restaurant. Somebody stopped to help, we poked at the engine for awhile. He had a screwdriver, and so we could see we had spark. Fuel pump was running, could hear it. Air metering flap was definitely springy, so there was fuel pressure. Once in awhile the car would cough, but that was it.

Eventually it started and ran for a couple of seconds, then died out. It kept that up for awhile, then finally ran and took us home.

This intermittent crap is very annoying.

Tuesday, March 31, 2015

My parts order from Autohaus AZ came yesterday. Two new Elring valve cover gaskets, 116 016 05 21 and 116 016 06 21, $5.62 each, 8 copper crush gaskets for the valve covers, $2, a Beru 008 542008 32008 170E 4-wire CIS/fan coolant temperature sensor, $26.97, and a nasty MTC monovalve insert, $15.35.

The temperature sensor was easy to replace, one 22mm wrench and done. Fifteen minutes, tops, including removing the air cleaner and getting out tools. The monovalve insert was a pain: for starters the monovalve itself is a bit hard to reach between the firewalls of the 126, I had to move the diagnostic socket out of the way to gain enough access. Worse, though, was that the new insert's body didn't fit down into the coil! While tapping on it with a small hammer to drive it in (and which was not working) I managed to break loose the retaining clip at the end, which flew away. Oh, man... So I moved the new rubber-equipped assemblage to the old valve insert, reusing its E-clip retainer and spacer. That actually seemed to work out just fine. (The new and old inserts looked identical in construction.) I guess we'll see if it works afterwards... This took maybe a half hour. The old monovalve insert diaphragm was torn completely free from the insert. That's the worst one I've ever seen.

I then pulled the valve covers, the old gaskets were rock-hard and cracking. (Hence, I hope, the smell of burning oil.) The job went smoothly, but took about an hour, including picking cruft out of the valve galleries where it fell in while removing the covers. I used new copper crush washers.

...The car started readily and ran well enough. I don't think it's running any better, but the heat was working correctly. Also I believe that the engine temperature sensor is a bit more accurate as to its operating point, so that is an improvement even though the crappy running is not yet cured.

Tuesday, May 19, 2015

The neighbors told me that a taillight was out. I have been in the habit of disregarding the lamp-out warning indicator because there is an intermittent in the RR side marker, but that doesn't mean that there are not other problems! I found the 10W bulb burnt out on the RR, though oddly that pesky side marker was working again. While I was there I noticed that the LR bulb seemed dim, and it turned out that it was not the correct 10W bulb, so I replaced it too. One of the license lamps was also out, that was a 5W cartridge lamp. There, all better! (All three replaced from the junk box.)

Wednesday, May 20, 2015

The wretched lamp-out warning system has annoyed me for the last time, it again was warning me of the RR side marker light being out. (Which it was.) I looked it up, and the part (126 542 01 32) is easily reachable as it is located within the fuse box. It just unplugs. I opened it up with a couple of screwdrivers, prying the plastic shell away from the plug assembly, and exposed the two coupled circuit boards. It was readily apparent that the solder joints to the connectors were degrading, so I resoldered all of them. When reinstalled into the car the pesky marker lamp was working again. This is like a 1/2-hour job, soup to nuts. Time will tell if this is truly fixed, and with no bad side-effects, but I am confident that this has cured the problem for now.

Thursday, May 21, 2015

I reattached the driver's door speaker cover that had started to come loose. It has a broken plastic clip or two that let it be pulled loose, but it seems intact enough to mostly stay in place.

I tried to use the Harbor Freight fuel pressure test kit, but it's wonky, not well documented, and the fittings leak. Looks like many were only assembled hand-tight. It'll take more time than I have today. I did get an 85–90PSI reading off of it, once. While I was there I noticed a fuel line that was starting to come loose, it wanted to leak when disturbed. I secured it better.

Friday, May 22, 2015

The speaker cover popped loose again within the first day, so I removed it again and used Shoe Goo to try to patch some of the cracks in the plastic that seem to be allowing it to deform under the stress of slamming the door. I also found the broken-off ear inside the door, so I'm trying to glue that back too.

...After it had dried most of the day I slipped it back into place. With all the mounting ears working, I suspect it'll stay in place now.

Wednesday, May 27, 2015

I'm thinking of having a professional engine diagnosis done, but before that I need to check the plugs. They're still good, excellent even. So I don't have a fouling problem. While I was there I lubed the throttle linkage, it was starting to get a bit sticky.

I made a diagnostic appointment today at a nearby Euro-centric shop. It'll be Monday, June 6, 2015, at 8 AM. I need to make them a list:

Symptoms:

Runs ratty, seems to be 'misfiring' a lot. Or equivalent. Often will die while idling at a light, sometimes when giving it throttle to take off. Occasionally when running down the road the engine cuts off like the ignition switch was flipped. (This is actually pretty rare, but highly disturbing when it does happen.) Usually it'll start running again on its own in a second or so, before significant forward speed is lost. (I.e. push-started on momentum, which does work on these cars, if you're going fast enough.) Not always, then I have to re-start it. Sometimes it doesn't want to, but if I'm patient I can get it going again. Weak acceleration, surge-y. Worst just off idle. Usually have to feather the throttle off of idle, else it can die. (It's possible that dying at idle is caused when the misfire [?] causes the RPM to drop too low, the idle actuator tries too hard in reaction, and the thing dies just as it might if I goosed the throttle too hard. But this is an uncertain conclusion.) Seems to be getting slowly worse with time.

Used to be that heavy acceleration felt normal, now it rarely does. Fuel economy is 'normal'. Behavior is worst in cold weather, when the car is warmed up. Cold starts are generally pretty reliable, though prolonged cranking and a reluctant firing is the norm. Fuel pump sounds normal. Was completely unable to be started at all in mid winter, ether was useless. Cold-started in warm weather it's on its best behavior. Such as it is. Running is actually at its worst just before the engine temperature gets high enough to engage normal spark timing, especially when it's colder out. Behavior is generally variable, not consistent. There are no codes thrown on the pulse reader under the hood. Spraying carb cleaner around is inconclusive. Sometimes it seems to react, but then it'll act just the same on its own. And sometimes it does not seem to react. Maddening.

Things I've done (and did it help or not):

Plugs recently checked, they still look great. So there's not an oil-fouling problem like I've had on other cars.

So, what I'm looking for is a diagnosis of what definitely needs addressing, so that I don't waste time and money shotgunning. I may or may not want to be doing the repairs myself, depending on what is found, and the estimates.

Parts like the ignition module are very pricey, so I'd first be looking at good used for that.

Sunday, May 31, 2015

The oil was very low. I checked, and it wasn't time to change it, so I added 2 quarts. There's a slow leak, somewhere.

Monday, June 8, 2015

I dropped the car off for diagnosis, and rode my bike (stowed in the trunk) to work from there.

...Big surprise, it was not done at the end of the day. Had to call my wife for a ride home.

Tuesday, June 9, 2015

I picked up the car. The charge was $154.79, for 1.6 hours of time. They said that the fuel pressure was fine, at 90–93PSI, but it is noteworthy that they did not check the delivery rate. The intake system smoke test showed leaks from the injector seals and the intake gaskets. The ignition voltage was 6–7kV, but #5 was 7–16kV. This reading followed the plug wire when they moved it to #6, so one of my new plug wires is bad.

Wednesday, June 10, 2015

Acting on a hunch, I cut apart the bad wire's plug end. That was tedious, and I found that the 1kOhm resistor inside was open-circuit. I rigged a piece of iron wire in its place and taped it back up. That should hold until I can find a replacement. (Beru ZLE 121.) I moved it back to #5. While running the engine I heard clicking on the passenger-side fender whenever the RPM dropped, and there was a vacuum switch there that was operating under those conditions. When I tried to pull off the hoses to see how it liked that the aged rubber joints fell apart, so I replaced them with some good ones from the junkbox.

...On the way to and from work the car certainly seems to be running better. More time will tell.

Thursday, June 11, 2015

The car definitely is running better, but has a new symptom: The RPM drops, almost dies, and the CEL flashes on then off. It acts like the idle actuator kicks in and the engine surges up and then back to idle, and then everything's back to normal. If your foot is only lightly on the brake the car will lurch forward a bit, too. The flickering light can happen more than once per second, and no codes are thrown. This is weird.

Friday, June 19, 2015

I re-resoldered the OVP, and used Deoxit on every contact, internal and external. No difference. Worth a shot, anyway!

It is possible that the light and everything else is just in reaction to the sub-par RPM being detected. That could be misfire, etc.

I ordered a new Beru ZLE 121 from Kinsgsborne, about $10. They still had a few in the back, apparently these aren't commonly used anymore.

Tuesday, June 23, 2015

The plug end came yesterday. I installed it this morning, it seems to work. It went on with more difficulty than I'd like, the rubber sleeve is tight.

Monday, September 7, 2015

Went to drive the car today, it was colder and the thing didn't really want to start. (It has always been cold-blooded.) Naturally it smelled a bit gassy at the start. But it kept smelling gassy, enough that I finally stopped and popped the hood before I got on the freeway. The engine backfired a bit as I opened the hood, and it smelled very gassy. Up goes the hood. Yikes! There was a gasoline fountain inside the engine compartment, arching back over to the brake booster. The fuel supply line had split at the engine end. I killed the engine, and used the tools in the trunk to remove the hose clamp, then I cut off a couple inches of hose and reinstalled it. (It was overlong, really.) That hose did not look bad when I last looked it over, but it was clearly not up to the job. Fortunately disaster was averted and there was no fire, and we weren't even delayed very long.

Friday, March 25, 2016

On the cross-state drive Tuesday the car was pulling quite a bit. The worn tires were seriously chewed. I took it to Les Schwab, and they determined that 3 of 4 tie-rod ends were bad. I had them repair that and align it, which was about $300, and then new tires were about another $400. Sure drove nicely afterwards, though.

Saturday, May 7, 2016

The AC wasn't working, and I checked the charge. Zero residual pressure. I vacuumed it and it seemed OK, but a test pressurization with propane showed that it leaks down some from around 100 PSI in minutes. I sprayed soapy water around what was easily reachable, with no results. My last record of charge was in 2012, so I tried to charge it, but the compressor wouldn't start. ACC panel? (It's been acting up lately.) Klima? Will definitely take more digging.

Monday, September 5, 2016

Long past time for some maintenance, I changed the oil and filter. Sludge! The suspension oil tank was empty, I put in my last quart of Febi. I only have one 560 oil filter left, I'll need to get more. I noticed that the oil pressure gauge pegs on key-on, I suspect that it is not working right. I'll have to look into that. Short?

Thursday, October 27, 2016

Driving to work today and all the dash lamps came on. Uh-oh! When I got to work and popped the hood I found the alternator belt laying on the inner fender. I left work early enough to have light, and stopped at NAPA to buy a new belt. A little over $5. But, I wasn't able to go even a block after that, the car wouldn't stay running. I pushed it into the Les Schwab store right there, and they were kind enough to install it. Gratis, but they suggested I bring donuts. No problem!

Tuesday, April 4, 2017

I went to take the car in to have it worked on, and found the battery exploded! (Split down the side, all the caps blown off, etc.) I guess I left it on charge too long. A Die-Hard, so it's been in there since I got the car. I stole the battery out of the Frankenheap so that I could drive it in to Fernando at Motortech.

Thursday, May 4, 2017

Yesterday he called. Said that he tried swapping out the fuel distributor, but no joy. He tried a coil swap, and said it cured it. He strongly suggested a new fuel pump relay, as that is almost always responsible for the sudden death symptom and was cheap. I've seen photos of these, it looks like a good resoldering is likely to bear fruit. I'll try that first. We picked up the car today, it started and drove well. Started easily, idled smoothly and didn't misfire, and didn't die if you stepped on it too hard. $278.60. When I got it home I pulled out the fuel pump relay, which is located between the firewalls. P/N 003 545 25 05, also marked "[02] KR0002 KPR" and "05 3702 40". The RTV seal around the shell was decomposing, I was able to rub it all away with my thumb. Prying it open revealed pretty much what I expected: two relays, two power transistors, a Microchip PIC16C54-10, and a LM2903N, plus the usual small transistors, diodes, and other components. Several of the solder joints were looking a bit grainy, so I resoldered the entire board. When reinstalled in the car, it ran, so I guess I did no harm, at least.

Friday, May 12, 2017

Yesterday I pulled the broken passenger-side sunvisor clip out, cleaned it with brake cleaner, and glued it back together with Shoe Goo. I put it back in this morning, and it works. The electrical connections for the mirror light are a bit flakey, but otherwise it's an improvement. The other side's clip is cracked, but still holding.

Saturday, May 27, 2017

I pulled the oily/dirty chain tensioner off and cleaned it. It looks to me like there is no oil seal inside the big cap screw. I threw an R20 from my Harbor Freight kit in there and put it back together. We'll see if that makes any difference on the oil leaking out in the area.

I tried to charge the AC, but the compressor would never start.

Sunday, May 28, 2017

I resoldered the Klima relay. It's a long shot, and it really looked pretty good inside. The problem likely lies elsewhere, probably in the PBU.

Wednesday, July 19, 2017

I pulled the Klima again, and used a hot iron to touch up the few large pins that looked less than perfect, then I vacuumed the system and tried again to charge the AC. I think the problem is that the low-pressure fitting doesn't open properly. I cranked it down very hard with vise-grips, and was finally able to get it to open enough to take a charge. After a lot of fooling around I was able to get vent temperatures down to 47°F, which while not great ought to be acceptable.

The oil smoke seems to be coming from the valley of the engine, not off the exhaust manifolds. It's hard to be sure, though. The big leak at the chain tensioner seems to be cured.

Thursday, July 20, 2017

I was pretty sure the aspirator motor wasn't running anymore, which will definitely lead to HVAC control problems, so I pulled it. Yep, it's spastic and doesn't want to spin. The resistor inside looks all burned. It's only been six years since I last worked on it. I ordered a new (used) one off eBay, about $23. P/N 000 830 96 08.

Monday, July 24, 2017

The 'new' aspirator showed up. It's clearly used, and has a different part number than what I ordered. The plug is different, and would not mate correctly. I tested it, and it does run, quietly, and pulls 0.10" of water according to my Magnahelic gauge. It did come with its mating plug, so I should be able to fabricate something out of the old motor and that plug so that this fan can go into the car. I'm not pleased, though!

Tuesday, July 25, 2017

I cut the connector out of the old aspirator and soldered it to the plug wires on the replacement, then installed the mess into the car. I put the knee bolster back too, that's safer for any passenger.

...

The new aspirator seems to work. A couple of good driving sessions with the AC on today showed that the fan speed dropped to pretty low once the setpoint had been reached. I can finish putting the car back together now.

Wednesday, July 26, 2017

Put the car back together. Somehow I ended up missing a screw, and I had to scrounge in the parts bucket to find a suitable one.

Thursday, September 14, 2017

Some time ago the lamp-out warning lit, and it was a brake lamp. On the road I swapped bulbs with the reverse lamp. Today I finally got around to replacing the bad bulb.

Saturday, October 28, 2017

The heat control has been flaky for some time, and as things cool down it's getting more critical. Just the lightest touch on the control wheel would make it cut in and out. (The monovalve LED I added some time ago is really crucial for this kind of diagnostic.) Today I finally made some time and removed the ACC panel. I removed the potentiometer from the PCB and opened it up. It's custom, no way to come up with a replacement, except out of another unit. I cleaned it out, and used DeOxIt fader spray on it, and did a very light wire-brushing of the circular tracks and the sliding metal fingers. According to my meter, the resistance change is smooth, with no intermittency. We'll see if this works any better. While I was there I added another LED, this one for showing AC energization, behind the center button. I used the other LED from the same toy, but used the blue side for this function. I used another 680 Ohm resistor from the junk box, and hooked the series combination between the X1-7 (Klima) pin and power. Also, one of the two illumination lamps was intermittent, so I replaced it with a new one. All this took a little over two hours. On the test drive today it behaved well, but as it was a warm day nothing much was proven. The next cold morning drive should be more definitive.

Monday, February 19, 2018

Oops! A moment of inattention and a sunny patch on the mashed 12°F snow drifts in the corners and all of a sudden I'm into the guard rail. Well, the car used to be pretty. Gouged up the passenger side front and back fenders, both doors, and broke out the sides of both the front and back lights. Had to get Jill to come with the X5 and a rope to pull me out of there.

This is so not a winter car!

Wednesday, February 21, 2018

I removed the broken front turn signal amd gathered up my bag of shards and some glue, and reconstructed it as best I could. I used clear packing tape to cover the holes. Looks.... tolerable.

Thursday, February 22, 2018

The front lens turned out well enough, so I did the rear too. As before, looks.... tolerable.

Wednesday, March 28, 2018

I bought new headlight doors, URO. The old ones had looked bad for years, and recently chunks started falling out. About $96 shipped, took about an hour to install. You don't need to remove the headlights, but you do need to remove the turn signals. They are clearly much more cheaply made than the Bosch originals, but look good enough, and a lot better than the old ones did!

Sunday, May 6, 2018

The rear end had been getting noiser in recent months, I finally had a chance to jack it up and check the oil level. Perhaps a bit low, but not scary low. I had some M1 gear oil I'd bought on clearance, I shot some in until it started running out, then capped it. It definitely seems quieter now.

Monday, May 21, 2018

I was at the U-Pull looking for a bolt for the truck's tailgate, and ran across a 300SE, white. I grabbed the side lights I'd glued together ($20), the front fender ($36), and the rear deck speaker grilles and center stop light. These were about $17, and are not broken, though they are grey and not cream beige. I wonder if the FLAPS has a reasonably-close plastic paint match?

Wednesday, May 30, 2018

I bought the front door too, $46. The rear door would have been nice to have too, but it's too short.

Saturday, July 14, 2018

Charged the AC, was only getting about a 10°F cooling effect. It took forever, I think the low-side Schrader valve is sub-optimal. Afterwards we got 48°F vent temperatures on a 90-degree day. The last recorded charge was in 2009, so that's not an unreasonable leak rate.

Tuesday, December 1, 2020

Tried to move the car down below and out of sight, for political reasons, but I couldn't get it started. I was getting close when the starter decided to stop engaging, and now only whirs ineffectually.

Sunday, January 10, 2021

It still wouldn't start, even after I dragged/pushed the car in front of the garage where I could jack it up to gain good access to the starter, and banged on it good with the BFH. All it would do was whir. Pisses me off that I'm going to have to buy a starter to put into a car I want to turn around and sell, but I don't see any other reasonable option.

Saturday, April 17, 2021

I got the starter removed, took about 1.5 hours. What a messy, greasy, PITA. At least the weather was nice. NAPA had one, remanufactured and not Bosch, for $117.99 with an $82.50 core charge. Not in town, it had to be ordered.

Thursday, May 6, 2021

I installed the new starter today. It was, as usual, a greasy PITA, but was fairly straightforward. The car started instantly, with under one second of cranking. (It was a warm day.)

I then cleaned off and removed the neutral safety switch, which has been intermittently bad for a long time. With luck I can clean it up and not need to buy a new one.

Friday, May 7, 2021

I drilled out the rivets and opened up the NSS. I cleaned it out, cleaned the contacts with DeOxIt, and lubed the cam surfaces with grease. I used small machine screws to put it back together, and reinstalled it on the car. Seems to work fine. I moved the car down below out of sight for now.

Tuesday, March 1, 2022

I put the battery on charge, it was flat, flat, flat. Due to the 190D breakdown, we might be needing this car, temporarily. [Through March 12.]

Wednesday, March 2, 2022

I started it and brought it up top. I put it on charge again, as it wasn't done, and cleaned off the windblown mud and pine needles. The two rear rubber exhaust donuts were gone, so I grabbed a couple of used ones from the pile and put them on.

Thursday, March 3, 2022

Licensed. Drove it to pick up Daniel.

Friday, September 8, 2023

I stopped by the U-Pull, and picked up a taillight ($14.18) and a fan assembly ($18.90 for clutch and blade) from a W126 380SE. (Fee-free, as I was actually there to get something else.)

Sunday, September 10, 2023

I ordered two new Lemforder motor mounts and a crappy aftermarket neutral safety switch (NSS), from Pelican Parts. (The earlier NSS repair didn't 'take'.) If I put all this recently-collected stuff on the car it should be fully driveable again.

Monday, October 9, 2023

I installed the new $16.50 NSS today, which is predicted to be the last good-weather day. Giant PITA, simply because you can't quite reach anything except with fingertips, and it's all very oily. But, it seems to work. The cheapie switch looks just like the old one, except the electrical contacts are much cruder looking, and one of them wanted to push into the switch body unless great care was taken.

Thursday, October 19, 2023

A beautiful day, I installed the new $41.74 Febi motor mounts. (What came off were Meyle, what I'd ordered were Lemforder, what I got were Febi.) What a greasy PITA! Here are the steps:
  1. Disconnect the battery, the back of the starter is 'live' and you don't want to hit it with a wrench while it is capable of welding it in place!
  2. Remove the cooling fan, to allow the engine to be lifted up significantly. I used a 10mm open-end wrench.
  3. From beneath, use an 8mm Allen socket on an extension to remove the two bolts (one each) holding the motor mounts to the arms on the engine. There are holes in the subframe for access.
  4. Use a 10mm socket and a small open-end wrench (on the shaft flats) to unhook the lower ends of the two motor shock absorbers.
  5. Using a floor jack, and a jack stand for safety, jack up the engine until you can get a 6mm Allen (either bent key, or a socket on a ratchet—whatever works for you) onto the four bolts that hold the motor mounts to the subframe. Don't forget to set the jack stand before you put your (irreplaceable!) hands in there! This is where the disconnected battery becomes important, because you're wrenching right next to the starter.
  6. Remove and replace the two motor mounts. Marvel at how bad the ones that came out are.
  7. Get both bolts on each new mount started before you tighten either one down. Important.
  8. Lower the engine onto the new mounts, guiding the motor shocks back into their mounting brackets.
  9. Using a long spike, wiggle the engine through the motor mounts until a bolt can be re-inserted. Get both sides started before you tighten either one. Important.
  10. Tighten both 8mm mounting bolts.
  11. Re-attach the motor shock absorbers.
  12. Replace fan.
  13. Reconnect battery.
  14. Clean up, and drive car.
This took me a solid 2 hours. It shouldn't take that long. The driver's-side mount was extremely oily, and falling apart. It was completely collapsed. The passenger-side mount was also completely collapsed, but still intact. The engine sits at least ½" higher than it did.

To try to protect the new driver's-side mount from oil I cut a square of a heavy aluminum sheet (from the corner of a Costco lasagne pan) to make a 'hat' for the mount. I formed it over the new mount while it was on the ground, and poked a hole in the center for the bolt with a big screwdriver. Before lowering the engine back onto the new mounts I slipped the hat over the mount. This may or may not help, but it was free and didn't take much time.

Sunday, October 29, 2023

Put it in storage, and put a Battery MINDer on it.

Return to Site Home