A belated log of the Chicken Wagon's life with us.
...
Tuesday, February 20, 2007
The snow tires on the SDL are going out, twisted
belts or something, so I thought I'd un-retire this car for the
remainder of winter driving season as it has snow tires on it. I
drove it to the licensing place, where they vectored me to the
emissions testing place. They tell me it's its last test! After that
it'll be old enough to be exempt. Fortunately the car passed (not
difficult for a diesel), but it's still not licensed. I'll have
to go back another time.
While driving the car around I found that the RF brake was dragging
pretty badly, the parking brake was inoperative, the brake fluid in
the rearward reservoir is low, and the tranny was misbehaving rather
scarily, at least at first. (Couldn't seem to solidly engage the
final gear [4] unless I feathered the throttle.) That got better
as the car warmed up. Sigh.
Wednesday, February 21, 2007
I polled the mailing list for suggestions on removing the neutral
safety switch. Got a few, some helpful! Jacked up the car
preparatory to surgery. Plan to work on the neutral safety switch,
the dragging caliper, the parking brakes, the bad half-axle, and a
fluid change for the tranny. (And anything else I find while I'm
under there.)
Thursday, February 22, 2007
OK, I got the switch off. As predicted (not by me), there is
no sign of internal shorting. Oh well, I always wanted to know
how to take them off anyway! Back into the trunk I go, I guess.
What a grimy mess. For those who want to know, the tricks are to
remove the crossbrace and the speedometer and kickdown couplings.
That makes enough room in the area that you can use a wedge of wood
to shift over the tranny to make a bit more room on the side. There
is a rotating collar holding the connector in, that has to be
persuaded to the right position, then the round plug (with funny
angled boot) will pull straight out. Then you can remove the
shifter linkage, yes the bolt must be entirely removed. (Same
as for the speedometer cable.) With enough scrubbing in the
area I found the two 10mm bolts that hold it in, one's above
the shifter linkage and the other is above the connector.
Then the whole thing pops off, and is ready for the solvent
tank. (I didn't immerse it, just scrubbed it under the flow.)
While it feels kind of nasty for a switch, there was no sign of
electrical problems. At least it's clean now! It's pretty solidly
riveted together, in the absence of any overt problems I don't think
I'll go in.
While under there I noticed that there are some (two?) missing rubber
clamp buffers on the fuel lines. Will add it to the list. There's
also some frame surface rust starting where the undercoating and paint
is gone, partly due to a brake fluid bath. Must attend to that.
Friday, February 23, 2007
A disassembly of the taillight assemblies revealed no smoking guns. I
took them completely apart, down to the individual socket level, and
disassembled the wiring harness connector shells as well. Nothing, no
signs of abraded insulation, corrosion, broken connector springs...
So, I hooked up a battery charger to the connector for the neutral
safety switch (NSS) and ran the lights that way. Flexure and pounding
did nothing, the lights just worked. Left with few other suspects, I
drilled out the five aluminum rivets that hold the NSS together. (It
is possible to have a pinched wire or something in the harness, but
good luck finding that!) The inside of the switch looked good. A bit
of crud built up in the bottom, if it was conductive it could maybe do
some harm as the lamp switch contacts are very close to the aluminum
cover there. But not so close as to make me suspicious. Otherwise
the insides looked pretty good. I did notice that the 'hot' leaf for
the lamps had more sideways flex in it than I'd like, if it got far
enough out of plane it could perhaps contact the cover and blow the
fuse, but that is really stretching it. To 'cure' this I put a blob
of Shoe Goo over its mounting end, there should be no way once that is
cured for the thing to flex much towards the cover. But I really
don't expect this to have any effect. At this point I think I just
need to put it all back together and see what happens, I'm running out
of ideas. I am positive that the fuses blew upon shifting
into reverse, I don't think it could have been anything else on the
same circuit.
I'm going to have to purchase some suitable screws for putting the NSS
back together, I don't think I have anything that will work.
Sunday, February 25, 2007
A pissy weekend, it's been snowing and thawing. We got about 6"
of snow at our house, most gone by mid-day today. Definitely not good
working-on-the-car weather. But there was a nice sunny patch
mid-afternoon, so I went out and liberated the sticking RF brake
caliper. The pads are heavily worn down, the rubber sealing boot was
not properly seated on the frozen side, allowing corrosion to set in.
As I recall, the PO had said that he'd spent money at a shop having
the brakes worked on fairly recently before the sale. Well, we
haven't driven it much at all, and from the looks of this caliper he
got ripped off.
Anyway, I determined to do the usual disassemble and clean job. Getting
both pucks out is what is difficult, my grease gun and water
trick can get one out easily, but sealing the hole up to pump out the
other one is difficult. I end up putting the cleaned puck back in,
but then getting it out becomes the problem. After much
fiddling I got it out, slamming it out with compressed air when the
other puck was loosely wedged in place. Both ended up loose, and I
was home free. I hate doing that air thing...
The corrosion in the outer (non-sealing) parts of the bores was
interfering with the installation of the pucks, so I'm trying the electric
rust-removal trick on it in a bucket in the sink. I'll do the
pucks too, just for grins. One of them looks a bit dinged up, I
suppose I really should replace the entire brake assembly. But my
spare is an ATE, not Bendix, and I don't want to get two new ones for
a jalopy, as symmetry is supposedly important. Maybe I'll keep the
need in mind for future trips to the U-Pull.
The pads were fairly well worn, and the pad sensors weren't even there.
By combining the best of these pads and the used pads from the SDL I should end up with a passable set, at least
for awhile. As was usual, one pad was worn a lot more than the other,
the better one usually has quite a few miles left on it. I even have
decent used pad sensors that I can install.
Oh, and the bolts I bought for the neutral safety switch are just
a bit too short. Guess I'll get some more!
Monday, February 26, 2007
Washed off and blew dry the caliper. Looks good. I welded up a ring
anode out of scrap strips of sheet metal and put the first of the
pucks into the tank for de-rusting. I'm using the 6V setting on the
battery charger since the items, by necessity, will be in the tank for
many hours per. There is a lot of rust out in the open end of the
puck, and a bit along the sides where it doesn't belong. This will be
a stopgap, not a permanent repair. I expect this caliper to start to
stick again relatively soon. Not this year, I hope.
...At lunch I bought some more screws for the neutral safety switch.
They'll be too long, so I'll have to grind off the excess after
assembly.
...This evening I switched pucks, the one in the tank was rust-free,
though there is more pitting along the edge than I'd like. As I said,
this isn't a long-term repair. I dried it and set it aside. By
morning the other one should be well done.
Tuesday, February 27, 2007
Dried off the other puck. Looks good! I reassembled the caliper.
Easily said, not easily done. Getting the rubber boots back on, with
heat shields, is a real pain. But with the caliper reassembled I hung
it on the car for storage. I've still got to properly install it,
then move on to the car's other pressing needs.
Wednesday, February 28, 2007
What a fine day to finish the brake, NOT! Blizzard conditions, my
brake parts and tools are buried in snow drifts. More than four
inches accumulated this morning, and still coming down. Sheesh. Will
work on the Frankenheap instead.
Friday, March 2, 2007
Still very cold out, but enough of the snow has left that I could find
the parts and tools again. I did have to point my old half-radiant
half-convective heater downwards to free them from the ice. The
radiant heat was melting ice, the warm air was blowing on me. Nice!
I reinstalled the brake caliper, with grease on the backs and edges of
the pads. (I assembled the best set of pads from my used pile, and
put in used sensors.) Remaining to do (on that corner) is bleeding
and putting the wheel back on. I'm not sure I could get the hood open
to get at the reservoir, what with the snow pile on it and the doors
probably frozen shut too, but I didn't have time anyway.
Saturday, March 3, 2007
It's thawed enough to get into the car, so I topped off the brake
fluid reservoir and bled the brake. Not easy to do alone, so I
enlisted my 5-year-old son to man the brake pedal. He did a good job,
and we got it bled out OK. I did notice one problem while bleeding:
often when he pushed the pedal I heard a "splorch" up by the brake
booster. Some examination showed that brake fluid was spraying out of
a weep hole on the bottom of the master cylinder mounting flange.
Great, I think it's leaking into the booster and getting pushed out.
Time for a new MC, or at least a rebuild kit. I hope it hasn't ruined
the booster yet. This also explains the low brake fluid level, and
the streak of missing paint inside the engine compartment. Sigh, more
work! I put the wheel back on and put on a bleeder cap, which it
didn't have before.
Monday, March 5, 2007
Time to get busy! I greased and reassembled the neutral safety
switch, then put it together with the too-long screws. (The 6-32's
only came in 1/2" and 3/4" lengths at the hardware store, what I
needed were 5/8".) I had to grind most of the head off of one so that
it would fit under the locking collar. After it was all put together
I ground off the excess thread length to prevent interference when
putting it back on the car. Which I then did. That was a pain, for
such a 'trivial' job. I didn't need to adjust the switch position
after assembly, the reverse lights seemed to work right, as did the
starter safety. If I need to, at least I'm familiar with it now.
There may be brake fluid leaking out of the LF caliper, it was hard to
tell. I'm not impressed with the 'brake job' that the car had had
before I got it!
Tuesday, March 6, 2007
I removed the RR wheel and brake caliper. The pads are paper-thin,
but it otherwise seemed OK. I was able to use channelocks to squeeze
the pads away from the rotor, so the pistons aren't frozen. It really
needs new pads and a hose, and probably a rebuild as well. The drum
came off with some pounding with a rubber mallet. There was a lot of
rust inside, but the brake assembly looked good, shoes and all, and
the drum didn't have much of a lip on it. (Nor did the rotor.) I
used a wire brush to get off the rust, then the grinder to shave off
the lip. (Before I've mounted them inverted to the car and used the
engine to turn them like a lathe, but this time I just set it on a
spare steel wheel. It would turn [by hand] in place much like it
would in a lathe. With a light touch and some care I was able to
shave off the lip with the grinder while rotating the drum so as not
to put any divots in it. One hand spinning the drum while the other
rests lightly on its surface, holding the grinder cocked at an angle
so the wheel crosses the lip. Light touch with the grinder, never
letting the grinder against the drum surface when it's not moving.
It's harder to describe than to do.)
I had a look and both axles should be replaced as the one
that's not split is soft, deeply cracked, and ready to fail. I do
have a decent pair of spare axles for it, so that's no problem.
Wednesday, March 7, 2007
I removed the LR wheel and brake caliper, pretty much a repeat of
yesterday's performance. The pads are better than the other side, but
it may be that one of the two pistons is frozen.
I then found that the fill plug on the differential is completely
ruined. No matter, in the worst case I can replace the rear cover
with a different one. (I'll try removing it while it's off the car.)
I scraped off the worst of the gunk and then removed the differential
mount and the rear cover. I was then able to remove the two retaining
clips (using small vise-grips) to free the two axles. Out of time, I
put the cover back loosely afterwards to keep windblown dirt out of
it.
...At lunch I bought some Permatex Anaerobic Flange Sealer, and its
spray-on activator. This is probably the same stuff the MB dealer
uses, recommends, and even gave me a tiny bit of once. Expensive!
Thursday, March 8, 2007
I removed the old axles. One was a bit rusted into the wheel bearing
and needed some 'gentle persuasion', the other came out easily. Both
axles had fibrous stuff wrapped around them inside the wheel bearing
interface. (That's harmless.) With the differential mount removed, a
floor jack can lift the differential body up high enough to make
enough slack to free the axle shafts. I didn't have to loosen the
shocks. The axle with the ruined boots was very loose and floppy when
compared to the other three. The dirt had obviously been doing its,
ahem, dirty work!
I cleaned off the 'new' axle ends in the solvent tank, then installed
them. As usual, the small pair of vise grips is all that was required
to install the retaining clips. (Same as for removal.) One very
important point: make sure the differential-end spacing washers from
the donor car are removed first, and that you retain the spacing
washers from your car. They're likely different thicknesses, and the
correct spacing matters. I also reused the former retaining bolts and
washers.
The buggered fill plug, however, promises to be difficult. In the
worst case I can always swap the back cover (with decent plug) off the
old differential from the Albatross. I played
with it a bit but I ran out of time, so I again put the cover on with
two bolts to keep the dirt out.
Friday, March 9, 2007
I checked the part numbers, and the scrap differential's rear cover
was the same as this one's, so I pulled it. I used the wire brush to
power off most of the exterior dirt and grime, and a fair bit of its
paint. Oh yeah, and it was full of that nasty sticky black sludge (I
believe from one of the Albatross's PO's
attempts to deal with its noisy differential). I spent quite a bit of
time in the solvent tank removing the residue as it was quite tenacious,
then I used brake cleaner to sluice off the solvent and put it in the
shop oven to dry. A couple of rattle can coats of black paint renewed
its baby freshness. (The oven at 200 °F really helps speed this
up.) The breather was also clogged with goop, solvent and compressed
air helped open it up. Made a bit of a mess, though.
With that done I cleaned the mating flanges with brake cleaner and a
putty knife. Then I sprayed the Permatex Surface Prep on both (should
only do one says the goop tube—the spray can says to do both but
I'm inclined to trust the goop's label on this, too bad I didn't read
it first) and let them dry. The Permatex Anaerobic Flange Sealant is
not the same as the runny orange stuff I once got from the MB dealer,
it is thicker and purple. Oh well, I'm sure it's good stuff, it
certainly cost enough. I ran a small bead around the cover and then
bolted it down. At this point I was again out of time.
Saturday, March 10, 2007
I used the floor jack to push the differential back into position,
then bolted it in place. Next I filled it with fresh oil, which was a
tedious squeeze-fest using those pointy oil bottles. I tried not to
snug the filler plug too tight, we'll see. Then I put back the brake
drums and put on the calipers. (They'd been sitting on top of the
brake backing plates, still plumbed.) Next were the wheels, no
problems. At this point I went under and tightened the parking brake
adjustment as much as was reasonable. One side seems stretched, it
may not work well. Its cable was very stiff too. The other side
seemed a lot better. Next I removed the two cushion-less hard fuel
line clamps, cut some pieces of rubber fuel hose and slit them open,
then clipped them around the fuel lines, then reinstalled the clamps.
Perhaps not as good as the real deal, but much better than
nothing. Finally I installed two more rubber exhaust donuts to
replace the missing ones. Then I cleaned up the mess I'd made, and
drove the car off the ramps. Time to take it in to be licensed!
...And off we went! Uneventful, except there was a bad shift or two.
We got the license and came home, where I parked and left the engine
running. I then checked the tranny fluid, and I believe it was very
low. (But I am notorious for having difficulty checking the ATF
level.) I put in 1/2 quart of ATF I had laying around, we'll see if
it affects the shifting positively. While it was running I ran down
the driver's window and put some weatherstrip glue on the torn part of
the channel at the top. With it still down I let the glue get tacky,
then pressed the torn strip back into place. I left the window down a
crack so as to keep tension off of the channel until the glue fully
sets. I then removed the sun-baked and cracked passenger seat (my
wife won't need this right away) and set it aside. Out came the
vacuum and I sucked up all the mouse poo from storage. I pulled all
the carpets and the rear seat as well. The jury-rigged cupholder came
apart, so I glued that back together. (My wife insists on that and a
radio, nothing else is supposed to matter.) I then pumped up the
spare tire and buttoned things back up. The remaining cosmetic items
should be done over the next few days, but as of now this thing is a
driver!
...Which my wife promptly used. She was quite pleased, except for the
badly-cracked windshield. We also went to dinner in it, and it was
quite pleasant. Quiet and comfortable, and no bad tire wobble. She
and I noticed no shifting anomalies, so it looks like low fluid was
definitely to blame. I'll dial that in over the next few days.
Sunday, March 11, 2007
I removed the chewed driver's-side B-pillar cover and peeled off the
ruined windlace, both front and back. I grabbed the decent used pair
that I'd stored in the trunk and installed them instead. I painted
contact cement down the glue stripe on the frame with a small
disposable glue brush, and pressed the 'new' windlace strips into
place. I placed the sun-baked ends down, where they don't show quite
so much. I removed the bottom seatbelt retaining bolt and slipped the
B-pillar cover off. I then reinstalled the replacement pillar cover
from the trunk. Looks a lot better! Too bad I only had the two
windlace strips, the car needed four. (I wonder if the good bottom
halves can be pieced together into something that looks presentable?
I'll look into that.) I then cleaned up the smudging with Simple
Green, and got it ready for my wife's use just in time.
...Many complaints from my wife about the windshield. Besides the
cracking from road rocks it's also pitted from road sand. She also
didn't like the level of illumination from the instrument cluster.
(On a 123? Imagine that!) And she was annoyed to find that the
Becker tape deck wouldn't accept a CD! Sheesh, honey, I don't know
what you want. It doesn't wobble on the road and it has both a
functioning radio and a cupholder. Were those not the main criteria?
At least it's clean and quiet.
The windshield replacement job scares me, I hear it's rather
difficult. I have a good used replacement and a new rubber seal. My
big plan had been to pull the badly-cracked and chewed dash (for
replacement and for repair of the center vent ACC pod) and, while it
and all the associated window trim was out, to try tackling the
windshield then. But I don't want to attempt any of this while the
car is in service.
Monday, March 12, 2007
I removed the B-pillar cover on the passenger side to expose the
windlace. While there I noticed some mold in some of the seat belt,
so I got a bucket of water and some Simple Green and washed it out. I
then pulled down the ratty windlace pieces, front and back, and
snipped them off to leave the still good parts in place. Then I took
my collection of ruined windlace, cut off some good ends, and pieced
together a serviceable, if not beautiful, set of windlace out of it
all. I just glued up the pieces much as if it had been a new set. It
doesn't look as bad as you might think, but it in no way can be
mistaken for a nice new set! Better than it was, though. I then
reassembled the B-pillar.
...Tonight while driving I had a serious transmission non-shifting
episode. After the panic cleared I remembered that it's done this
before, if you drive too much/fast with it held in first gear (as I
often do in parking lots) it won't upshift once you take off unless
you come to a complete stop for a bit. I'd forgotten, and on the road
it would rev and not shift, then slip and not accelerate at all, etc.
(Rolling while in neutral does not clear it up.) A total mess.
Pulling over and sitting in park for a few seconds restored it to
normality. This transmission is not right! But I think we
can learn to work with it. My wife, however, will probably not notice
this, its worst problem, because she uses the brakes rather than the
shifter. (I use it to prevent upshifting when I don't want it to do
so, I don't use it to force downshifts.)
Tuesday, March 13, 2007
I went into storage and found the best spare seat. Unfortunately it
is about as discolored (from sun) as the existing seat, but at least
it is not all cracked. The back might be a little better, but there
are some chewed spots in the side of the would-be replacement. I'll
just have to be content with replacing only the bottom cushion. I
separated the two seats' halves and cleaned the new seat bottom, but I
ran out of time to finish the job. It takes a fair bit of time to do
seat work. And space! I was spread out in the yard (a soft place)
trying to avoid all the nasty bones the dogs have littered all over
the place. Unfortunately the seat tracks have to come all apart in
order to liberate the frame assembly, and that takes even more time.
Wednesday, March 14, 2007
I tackled the bad brake light I noticed yesterday as my wife drove
off. The bulb was good, but the socket area was badly corroded, as
was the barrel of the lamp. I got out the Dremel wire brush and went
at it. Ditto the parking lamp, though it was still working. I
replaced one of the dead rear side marker bulbs, but I only had one
spare and both were burnt out.
The glove box door was down because the latch assembly had again gone
'sproing' and wouldn't work anymore. So I teased that back together
again. What a steaming pile! I've never seen one of those 123 doors
that works very well. The design would probably be good if it were
all metal, but the plastic deforms too much and then it jumps track.
I've got to tell her (again) to treat it very gently.
With the fraction of time remaining this moning I got the seat tracks
moved over to the other seat bottom. But that was it.
Thursday, March 15, 2007
I put the two seat halves back together, and swapped on a better hinge
cover from the donor. (The trick to removing these without breaking
the snap ears is to spray a little soap on it then slip a tight socket
over the end then whack it with a mallet.) I mopped off the worst of
the dirt and grime with Simple Green, then installed the seat. Looks
good!
I also replaced the remaining rear side marker bulb with one my wife
bought yesterday.
Friday, March 16, 2007
I had a look at the spare window regulator I bought, and found it to
be probably as bent as the one that's in there! The regulator's
wretched pot-metal base plate is a bad design. (Too thin.) So I
disassembled it a bit and took it to the anvil. I got it mostly
straightened out (which I have done before and found not to last) when
I hit it once too many times and cracked it. Crap! I was looking at
it trying to figure out how to bolster it with some steel, but I'm not
sure that any such measure will work once the thing has cracked. And
zinc pot-metal just doesn't weld. Now I'm not sure what to do, will
have to think.
Saturday, March 17, 2007
Fluids time. Put in engine oil (needed a fair amount), more
transmission fluid, windshield washer fluid, and a bit of water for
the radiator. Power steering and brake fluids were fine.
Sunday, March 18, 2007
Started messing around with the ruined window regulator. Did a bit of
surfing, and found that zinc castings can be welded or soldered, but
not easily. Not at all. One source implied that most such castings
should be treated as aluminum for the purposes of soldering. I had
some aluminum solder, so I thought I'd try it. First I wire-brushed
the area to clean it off some. The feeble propane torch wouldn't even
begin to heat things properly, so I got out the acetylene. Oops!
That is a bit too hot, the cracked casting slumped and holed before I
could even begin to solder to it. But what I did notice was that
where it had melted into a big drip there seemed to be no longer any
crack. Throwing caution to the winds, I vise-gripped a steel backing
plate across the crack, slopped some acid on there for flux (fizz
city!), and used an old-style broken door check body for filler. I
then proceeded to make a real mess. While things did melt, the zinc
tended to want to burn out of the metal, and I never got good
puddling. I suspect in part that my filler material wasn't quite
right. Eventually I got tired of messing around and had a look at the
results. Nasty-looking! But there did seem to have been some
strengthening, at least when compared to a zero-strength crack. I
then decided that I'd had enough of the melting, and dug out some of
my epoxy glues. I mixed up a big wad and potted the whole area in the
stuff. I have no idea if it will set up with any strength or not, but
at this point I have little to lose. I think it'll grip all right
because the melted area is all wrinkly and lumpy, there should be lots
of surface area. I set it on the wood stove (which is on low) to cure
after it had set up enough to avoid dripping.
Really I think I'm going to have to find a good regulator to
install into the car. While I haven't looked yet, the 'chunker' is
one I believe that I worked on before, trying to straighten out the
nasty pot-metal casting. It's either bent again, or has cracked where
I straightened it out. Either way I doubt it's salvageable any more
than this one I've been killing.
Of interest is that both the 450 SEL currently in the junkyard and
this 300D, according to the EPC, use 116 730 21/22 46
(L/R) window regulators. Maybe I'll stop by the yard today and see if
the regulator is still there and any good. Doubtful, but worth a
shot.
...So I dropped by the yard after church. There was a swarm of guys
stripping the 450, one of them had just bought a grey-market '80 380
SEL for $50. They'd had to yank it out of a swamp where it had sat
for two years, the PO was going to enter it into a demolition derby.
The new owner fiddled with it a couple of hours and got it started
then drove it home. He didn't know too much about such cars, and
appreciated knowing a few things about it. (Unfortunately his fuel
pump packed it in as it sucked on the dregs of the tank, and the one
from the 450 was long gone.) I tried to tell him that the steering
column he was liberating from a 116 was likely no good in his 126, but
oh well... In spite of the buzz of activity I was able to nab the
appropriate window regulator from the car. Seriously warped, but
still intact. We'll see how it goes.
Monday, March 19, 2007
I ground off some excess epoxy so the sector gear could clear the
repaired area. Flexing it by hand it seemed strong, it didn't
immediately crack off or anything. Thus having not one, but two
potential replacement candidates I opened up the door to have a look
at the 'bad' one. Yes, bent. But not broken. In fact, overall it's
less bent than the one I bought yesterday, though it's bent more right
at the motor hence the 'chunking'. Since the door really isn't that
hard to open up I decided to gamble on the welded/epoxied one since it
was the straightest of the bunch. I kept the original motor because
the connections had been cut off the spare's. It seemed to run OK on
the battery charger I was using to run it, so I buttoned it back up.
All went smoothly, we'll see how it holds up. I have the other two in
reserve if I need to try again later.
As of today the short list is more-or-less done. Time to do something
else for awhile. I promised my wife I'd build a shelf in the closet.
...My wife called me at work and during the course of the conversation
I reminded her that the sunroof worked on this car. She was excited,
as the weather was very good, and it turns out my son
was really excited to have it open. However, when it came
time to close it again, nothing. I came home a bit early to take care
of it and found the switch not making good contact. I took it apart
and burnished it so it worked again. I decided that this was also a
good time to address the center tube lubrication issue that I missed
the first time I had it apart. I didn't
have to take everything apart, just the headliner panel, and the six
screws/bolts and retaining clip that hold in the black drive bar.
With that all out I could swab out the center tube of the drive bar,
and I could also mop off the outside of the cable sheath where the
drive bar's tube slides over it. (This being the lubrication point I
didn't address the first time.) I then put some Lubriplate inside the
drive tube and reassembled everything. It worked fine again.
Wednesday, March 21, 2007
Harbor Freight was having a sale. (Got a fuel-pressure test kit that
has Bosch CIS fittings in it. $70. The diesel compression tester is
again on sale at $17.) But what was particularly interesting was a 1#
box of Alumiweld rods. These are
some kind of zinc alloy meant for brazing aluminum and pot metal.
$12, usually it's more like $20 there, or $30 elsewhere. The printed
instructions were fragmentary and the importance of a clean dedicated
stainless steel (no substitutions!) cleaning brush was not made
sufficiently clear. I think I may go back and get a brush, and maybe
another 1# box of rods. This is the stuff that would probably have
been very good for fixing the window regulator.
Thursday, March 22, 2007
Went back to Harbor Freight, bought more Alumiweld. They didn't actually
have a stainless-steel brush, so I bought one at the hardware
store that's adjacent to my work. (And a couple of 6" Phillips
screwdrivers that I needed for another project.)
Saturday, March 31, 2007
I decided to surprise my wife by putting the portable CD player (Sony
Discman) in her car. (I bought her some books on disc she might
like.) When I put the cassette adapter into the Becker it blew its
fuse. Not the car's, but the one in the clip-on holder behind the
radio. When I pulled it out enough to temporarily bypass the
(undersized?) 2 A Euro fuse, I found it wouldn't retain the cassette
adapter. The tape safety was kicking in. I opened up the Becker and
had my memory refreshed by the sight of belt pieces floating around.
Oh yeah, the cassette in this
was defunct! I'm mulling over ways to bypass the tape
adapter right now...
So, the Becker 599 Europa Cassette has a rear-panel DIN connector for
external sourcing, but it's mono, not stereo. So that's out.
Internally the cassette transport mechanism is a hinged subassembly.
It unplugs and pivots out, then you pry the snap-ear hinges open a bit
and remove the whole thing. Easy. Removed, you lose the four tape
buttons and the dial/band-selector light. There is a four-pin
connector (with only three used) and a three-pin connector on the main
board for the transport. The three-pin is for the head: the center is
common ground, the pin towards the volume control (black) is R, the
remaining one (red) is L. It seems to be 'hot' at all times, even
with the radio playing on the bench touching one of the signal pins
results in superimposed hum. On the four-pin connector the big red
wire towards the tuning knob is +12 V, the next one is a no-connect,
the next (yellow) is switched by the transport to +12 V to disable the
radio, and the last (black, towards the volume control) is grounded by
the FF/REW buttons on the transport to attenuate the signal. Ground
is through the metal chassis. It should be relatively easy to
fabricate a plate of some sort to cover the tape button hole, and to
rig some jacks into which to plug the CD player or her iPod. (The
iPod is the real reason I'm going to this much trouble, an auto CD
player is not expensive. Ones new enough to already have an iPod
jack are expensive, and have 'steal me' written all over
them. Unlike old Beckers. And if I'm going to operate it makes sense
to do it on an old Becker of little value. And let us not forget
that this is the Chicken Wagon, after all.)
I suppose that I need to plan out what I want to do. OK, in a perfect
world the cover plate will have a mini phone jack for the
iPod/Discman, a mini power jack for the Discman, a USB jack to power
the iPod, and an incandescent lamp or bank of LED's to light up the
tuning dial and band indicator and to indicate (by omission) that the
auxiliary input is active. The USB jack requires 5 V, the
Discman requires 4.5 V. As the Discman uses a 3 V
non-rechargeable battery pack I suspect that the 4.5 V is not too
critical, and that the Discman and USB power plugs can thus share
5 V. That means only a single 5 V regulator is required.
USB calls for 500 mA, the Discman's adapter is rated about the
same. If I make the cover plate out of metal it should be a nice heat
sink for a 7805 regulator. Perfect. Now I need to scrape up some
parts, it's probably time for a trip to Radio Shack.
...Did some research at Radio Shack, and did some surfing on the
Internet for the iPod dock connector. Radio Shack has changed a bit
since I was last there, not much in the way of parts anymore. Nothing
compelling there today, though they did have a bunch of iPod
accessories. Did better with the Internet, I found an inexpensive source for the
docking connector, and found some specifications on
wiring it. I think I'm going to have to mail-order any parts I
need. More research is required.
Anybody ever noticed that there's a lovely iPod-sized blank spot in
the 123's upper switch bank? You could put an angled docking socket
there and the iPod would be perfectly placed for use. I doubt I'll do
it, but it is an intriguing thought.
Sunday, April 1, 2007
Started working out the fabrication of the cover plate for the hole in
the Becker. I'm not exactly sure which jacks will end up in it, but
"Have drill, will travel!" I'm thinking that the mini-DIN serial
connector/cables from an old Macintosh will work well for the radio
end of the iPod link, I have some parts boards I bought just for this
kind of thing, if I can find them! Pretty sure I ought to put regular
power and phone jacks in too, though, for the Discman etc. (The only
problem with the Discman unit itself is that it refuses to play
recordable media. I know that Sony did this on purpose, and it bodes
ill for the Discman's long-term suitability for any car of my wife's.
She's a musician, and symphony-issued compilation CD's for rehearsal
purposes are a big part of her automotive listening experience. I am
assuming that there are other, less limited, units out there on the
trailing [cheap] edge. It's probably easier than getting her to burn
them to the iPod on the computer and then just using that. In her own
way she can be just as reactionary as myself. But I'm angling for the
iPod connection, which is why I don't just replace the head unit with
a suitable CD player.) While I was in there I realigned the band
selector letter indicator (U/M) with its window. It's adjustable, and
has always been a bit off.
Monday, April 2, 2007
Started compiling my parts order. More involved than I thought!
Tuesday, April 3, 2007
More parts compilation. Kid in a candy store time! Parts finally ordered.
Tuesday, April 10, 2007
Some parts have come, but not all. I started fabricating a steel
plate, to replace the cassette transport's face, which will carry the
jacks.
Wednesday, April 11, 2007
More fabrication. It's not easy making a 'stamped steel' faceplate
filler piece!
Thursday, April 12, 2007
Out shopping I bought two different non-Sony portable CD players, $1
each at the thrift shop. (It is said that Sony, owner of Columbia
Records/Video, deliberately made their player incompatible with
recordable CD's, and recordable rehearsal CD's are a part of my wife's
musical career.) The older player has line out, but wants 6 V
power. We'll see if it works well on 5 V. The slightly newer
one wants 4.5 V, and has only a headphone output. I'm hoping one
of these will work well for this application, naturally I'd prefer the
one with line out.
Friday, April 13, 2007
The fabrication is not going well, I don't have dies in which to form
the piece I thought I needed. It came out too big in one dimension
and was interfering with the radio dial cord. So I cut it in half
which relieved some of that overdimension, then I tack-welded it back
together. (I think that for such things welding up multiple pieces of
simple 90° bends made with the vise would ultimately work better.)
However, as I worked with it and the faceplate it seemed clear to me
now that my original plan to replace the tape button array with a
socket panel will not work, there isn't quite enough room for the
sockets I intend to use. (I sort of forgot about the plastic
faceplate, it covers part of the hole.) So I moved on to Plan B. I
traced and cut out a piece of sheet metal that exactly fills the hole
in the faceplate that is the combined area of the tape hole
and the button area, in effect making the bottom part of the faceplate
a solid area. With some grinding and filing this will fit well,
though I have to relieve some areas on the back side to result in a
flush fit. (More hacksaw and file work.) I will then attach this
panel (somehow) to the subpanel I have made that fits behind the radio
dial and bolts to the old transport retaining points. (This subpanel
will still be important in restoring the dial lamp, and as a heat sink
for the 5 V regulator, and for providing electrical ground.) The
jacks will come through the panel where the (larger) tape hole was. I
was hoping to recess them a bit, but that cannot be with Plan B!
The parts came! That 2.5mm power socket looks awfully large though.
May have to rethink that one.
Saturday, April 14, 2007
The USB jack, though large, still fits through the tape slot. The
power jack is a big issue, I'm not sure what to do. It doesn't fit
the cable I bought for it, and it's borderline too large to fit
through the tape slot. Will need to do some more shopping, I think.
I checked, and the older of the two $1 portable CD players (with line
outputs) works on 5 V and plays Jill's CD-R rehearsal CD's. It's a
GPX, whatever that is. So it's in. (The other, Lenoxx Sound, turns
out to have a broken hinge and otherwise doesn't seem to have any
better features.) I just need to figure out the cabling. One end of
the power cable I bought fits the CD player, poorly, but the other
does not fit the chassis jack.
I filed and ground the filler plate so that it fits well, including
necessary relief chamfers on the back to tuck into place. I then
welded and cut the rear plate so that it no longer covers up the tape
slot. I next need to figure out how to attach them together. (Then
on to cutting the holes in the filler plate for the connectors.
Scary.)
...I stopped at Radio Shack to check out their connector bin, and
found a pair of power plugs that fit the CD player and their mate for
the front panel. So I'll probably just cut up that cable I bought and
put new ends on it, then use the RS jack in the face. Not quite as
pretty, but at least it's a size I can use. And I really can't put
this off any longer.
Sunday, April 15, 2007
Not much time today, but I did make up the power cord. (Cut off the
old ends and soldered on the new ones. I had to drill the plastic
caps a bit to let the large cord fit through. Looks decent.) Drilled
the mounting holes for the rear plate. A drop of oil really helps it
drill, and I used the Variac to slow down the Dremel to a more
suitable rate for drilling metal.
I ran the GPX portable CD player using the new power cord, and I
finally thought to check its shock resistance. Not great, we'll have
to see if it works well enough in the car. It also doesn't have a
resume function, it starts over each time it's powered back up, or
even stopped. There are other players out there, if this one turns
out to be unsuitable. (The Sony has excellent shock resistance and a
resume option, too bad it's no good for my wife's purposes.)
The power jack has a separate 'inserted' contact, I think I can use
that to gate off the radio. (Need to invert it.)
Monday, April 16, 2007
The inversion of the power jack 'signal' should be easy. I have a
tiny 12 V incandescent bulb for lighting the dial, if I just hook it
between the switched ground pin of the jack and +12 V I can tap the
bulb's ground side directly for the radio shutoff signal. It doesn't
get any easier than that.
I got the front panel mounted in place, I drilled through both panels
and ran long screws through. Once everything was aligned I stacked
nuts on the back side of the front plate to make standoffs. Without
these spacers the panel bows when the nuts are tightened. I may or
may not weld the bolts in place and grind off the heads on the front.
We'll see how it looks once all the connectors are mounted, it may be
that two more screw heads will be nothing to worry about. The front
plate seems very solid, this is good. I then began marking it for the
connectors. I've got to get this right, I don't want to ruin the
panel, it's too hard to make another one! Current plans are to put in
the USB power plug, the coaxial power jack, and the 1/8" phone jack,
and to forgo the mini-DIN. That will require two cables to plug in
for both the CD and the iPod rather than the single cable I had in
mind for the iPod, but that's how it works out. I don't think there's
room (on the inside of the tape slot) for another large-ish connector,
and I want the USB connector for charging purposes.
The profile of the two sheet metal pieces is:
|
|o <------- New dial lamp
-----
|__| <- Bolt intertie
| |
| <- Face plate covers all tape holes
|
|
Tuesday, April 17, 2007
The holes are now cut in the faceplate. (I tried to leave enough free
space for the mini-DIN if I should ever want to add that.) Cutting
the rectangular USB hole was the worst, since you have to drill, hog
out between the holes with the Dremel and a burr, and then file to
final shape. (Using a ratty rusty old file that was the only one I
had small enough to fit in the hole.) Time-consuming. The two round
jacks were a snap by comparison. The face metal is thick enough to
take a semblance of threads for the two round jacks, so they can be
screwed in flush and locked from the rear. I really like the smooth
appearance that this gives it, so I think I'm going to weld all four
through bolts in place (two to mount the plate, and two for the USB
jack) and grind them flush with the face, converting them to studs.
More scary stuff!
In the evening I tried out one of the new surplus USB workspace
lights. Pretty feeble, nasty, cheap things. May be good for a gag
gift, but not going to be much of a car map light! In a dark room it
does throw a tiny amount of light on the center of the keyboard,
that's about it. Oh well, the radio's USB jack is really for charging
toys, not lighting.
Wednesday, April 18, 2007
That was fun! The welder is a bit rude and crude for such
small work. (No surprise, that.) I had quite a bit of trouble with
the larger bolts that hold in the USB plug, and almost none with the
longer thin ones (with nut stacks on them) that hold the faceplate on.
I had to do a lot of grinding and filing to put things back
more-or-less right. There was some dimensional shrinkage, but I don't
think it'll look too bad in the end. I also ruined one of the new USB
studs, but I think I can put a dab of glue on it to hold things in
place. Not my favorite idea, but it should be fine. After all the
metal work I took the plate to the belt sander and smoothed off the
face, then rattle-canned it with primer and black paint. I used the
shop oven to hasten the drying between coats. The plate is hanging on
a wire to dry now. With luck, tomorrow I can begin installation and
wiring. (I still have to mount the dial lamp and the voltage
regulator to the interior plate, and paint the lamp chamber white.)
...After work I fiddled with it a bit more. I installed the
connectors, and ended up having to glue the one nut on its chewed
stud. The glue accelerator messed up the face paint a bit, so I had
to respray that too. It's still not perfect, but I really
need to be getting this done, so it'll stand as-is for now.
Thursday, April 19, 2007
The rubber mounting ears for the USB plug protruded a bit on one side,
I used the Dremel burr to shave it so the plate will fit easier into
position. The white center plastic piece of the USB connector was a
bit 'bright' against the black face, so I used a Sharpie to touch it
up.
Time to finish up the rear plate. I drilled holes for the new dial
lamp and the mounting screw for the voltage regulator, then primed and
painted (white) the interior lamp chamber. I mounted the 7805
regulator, put wires on all the connectors, and installed the plates.
The 7805 is a metal-tab TO-220 version, this is important here because
this is the main ground point for all the new accessories. I took
care to ensure a solid connection. Continuity to ground on the
regulator (which is through the metal and mounting screws) measured
good. The stereo jack is a very tight fit given its nature and
location, I hope I don't have trouble with it contacting ground.
The faceplate doesn't look quite as good as I had envisioned, but it
doesn't look as bad as it might have, either. It's going to be good
enough. By decree.
...After work I started wiring it up. I put in a basic 3-terminal
5 V regulator circuit, with all three protection diodes, an input
electrolytic capacitor, and an output mylar capacitor. The 14 V
grain-of-wheat dial lamp is hooked between the regulator input and the
switched ground of the power jack. (I had to sheath the bare lamp
wires using insulation stripped from some telephone wire, I used a dab
of cyanoacrylate glue to hold the insulation in place at the lamp.)
The switched ground is also run to the Becker's radio disable
connector pin, the lamp acts as a pull-up resistor when the jack's in
use. The USB jack's power pins are wired in parallel with the main
power jack and to the regulator. Using the USB jack does not disable
the lamp or the radio. I stuck a little notebook computer work light
in it and it worked. I used loose DB-25 connector pins (sockets,
really) to attach to the Becker's transport power connector pins. A
dab of Shoe Goo holds the two wires (power and radio disable) in
relative position, I'll do some more gluing to fake having a connector
shell. (I have a close-enough mate to the three-pin audio feed
connector, no need to screw around there.) The wiring is very haywire
point-to-point rat's nest, but it should serve. No one will see it in
operation.
With the circuit checked out and powered up the dial lamp worked
correctly. You can also hear radio background noise cut out with the
dial lamp. (No antenna, so no signal.) I plugged in the CD player
and it worked! The line-out feed from the player is much too 'hot',
I'm going to have to attenuate it. I used a
200kΩ potentiometer from the junkbox to turn it
down and it worked much better. I'm also a bit concerned that the
head feed from the Becker transport might be equalized in some fashion
that is incompatible with line-in usage. More research is required,
in the worst case I just have to trace out some more circuitry to find
a better input location. I need to get out a decent speaker and my
Sheffield test CD to do some more research. I've been using an
ancient transistor radio speaker and a Carmina Burana CD that is much
too quiet most of the time.
I checked the dial illumination in the dark and it looks good. I will
need to tape off the former 1 & 2 track LED holes. The
illumination is probably not quite as even as the original had with
its plastic light spreader bar, but the bulb looks to be about the
same and the illumination level is good.
Friday, April 20, 2007
A small piece of black electrical tape took care of covering the
tape track lamp holes.
I found my Sheffield test disc and a spare Radio Shack Minimus 7
bookshelf speaker. (They had a decent reputation for their size and
cost back in the day.) Once I got everything wired up again it became
clear that head equalization is definitely an issue. Pressure
Cooker's Dish Rag sounded, well, limp. Muddy, in a word. I think I
remember now that tape EQ is a big feature of the tape recording
process. I dug out a 0.0047 µF capacitor and jumpered it
across the attenuator, and there was serious difference. Probably too
'hot' now. More research is called for, but I think I can come up
with a passable un-EQ attenuator circuit.
Surfing yields the fact that tape EQ is 6 dB/octave, due to the
basic physics of magnetic recording. And that a simple RC network
(one each) provides 6 dB/octave. So I was on the right track,
and merely trying out a few capacitor values from the junkbox will
probably be sufficient.
I found that the attenuation potentiometer was set at about
200Ω, out of 200kΩ! The
junkbox had a plethora of 150Ω resistors, and
several 0.010 µF dipped capacitors. I found that two such
capacitors in series (resulting in about 0.005 µF) feeding
the 150Ω resistor in a classic high-pass
configuration seemed to work well. The audio sample tracks sounded
decent, and the overall volume approximately matches the radio's. (I
hate getting blasted when switching from one to the other.) I also
checked the left/right channel assignment using the test disc, and
made sure it was correct. I then wired it all up, more rat's-nest.
It sounds good!
Now I just have to physically secure the circuitry a bit, especially
the stereo jack and the internal transport power connector, then
install it back in the car!
Saturday, April 21, 2007
Finishing day! I made a schematic for future reference, in Illustrator, PostScript, PDF, and GIF formats. I took some pictures (inside, outside) and slipped a piece of cardboard
in above the stereo jack's connections, then buttoned it up. After a
quick check of functionality I ran it out to the car and installed it.
(I had to dig up a new 5 A Euro fuse.) It seemed to work fine, so I
hooked up the GPX player and slipped in a CD. I presented it to my
wife, and told her that if that CD player didn't work out we could try
others. She seemed happy to get the radio back. Sorry it took so
long, babe!
Sunday, April 22, 2007
Now I'm starting to remember that this particular Becker had serious
volume control problems, and that I worked on it a lot years ago in
order to get it sort of functioning again. (I may have transplanted
the volume control from an older model, I know I did that
to something.) But it has left the right channel 'weak', and
the left channel with a non-functioning tone control. I poked around
at it for awhile on the bench, but nothing was accomplished. I may
try to find another, better, radio to move the mods to. No rush,
though.
Tuesday, April 24, 2007
A fellow lister has another Becker I can purchase. $20 w/shipping. Will
see if it's any better when it gets here. (Or at least I'll scope out
the internal wiring.)
Thursday, April 26, 2007
I glued the hinge pin back onto the Lenoxx Sound CD player. That'll
give my wife another choice. I used cyanoacrylate glue to tack it in
place, then potted it in Shoe Goo. I also bolstered the hogged-out
center hole of the Becker's tuning knob with a bit of cyanoacrylate
glue. It feels somewhat better now, the slop is gone.
Friday, April 27, 2007
With the glue dry the cover snapped back onto the Lenoxx CD player, no
problem. Good as new! (Except for the missing battery hatch cover.)
I'll throw it in my wife's car, she can try it out too to see which of
the two suits her better. (No line-out on this one, so she'll have to
watch that volume control.)
Sunday, April 29, 2007
Jill reports that the Lenoxx CD player is not working properly.
Monday, April 30, 2007
A trip to the thrift shop netted me a Panasonic SL-SX290. It's
supposedly skip-proof. But it doesn't have a line-out, and its
power plug is smaller than the others'.
Tuesday, May 1, 2007
A trip to Circuit City for a brand-new-for-real portable CD player was
a waste of time. They're all the way in back, obviously no longer
mainstream. No way to find out which blister-packed units might have
Resume Play, and the PFY had never used such a thing, nor could he
find out any information. When he wasn't looking I slit open the pack
of a likely-looking suspect (Memorex) and slid out the instructions to
read, but they were pretty unhelpful. I put them back and left,
disgusted.
Wednesday, May 2, 2007
I went to Wal-Mart and had somewhat better luck. Still had to do the
slit-and-slide trick, but the $25 Philips AX2411/17 I settled on
looked like it had what I wanted: 4.5 V power jack, CD-R compatible,
Resume Play, line-output, big buttons on the face. No MP3, but we
don't need that. At home it seems to work fine, and Resume Play does
function (though with a reset of the volume control output to a low
level), but I could only test on batteries. I didn't have the
right-sized adapter plug to see how it fared when running on external
power. I think it'll be fine. Let's hope that the default reset
volume level is appropriate for line-out (the single connector is
marked both headhphones and line-out).
Thursday, May 3, 2007
I tested the Philips in the car. No, the default volume level is
much too low, it has to be turned all the way up. Beep-beep-beep...
Steaming piles of crap that these things all are. I'm not happy.
Other than that it seemed to work all right.
Trying to find a player that meets all my criteria feels
like Highlander, "There can be only one." Unless there
isn't even that.
...After work I stopped by Radio Shack and bought a power plug.
Friday, May 4, 2007
Now that I have external power I tested the Philips on the bench. It
worked. I made up another power cord, which was more difficult than
expected. I had to do some filing on the one end's plastic 'bump',
and then sleeve it with a piece of .22 shell casing! If only I'd
known it wasn't really the right end I'd probably have cut it off and
put on a better one. I thought it just had the extra plastic ridge as
a retention device, but it turns out it didn't make good contact on
the outside either, it was a bit loose. (Hence the sleeve.)
Anyway, with all the fooling around I ended up wrecking the power
jack's switch, again, so I had to open up the radio and fix that. A
lot of fiddly bending and prying. (I didn't have another jack.) When
the smoke cleared everything was working again, but...
The Philips, while it does remember where it was, reverts to an
unusable volume level every time you power-cycle it. POS. Also,
there is an extreme amount of an intermittent farty noise coupled in
from the motor, much more than any of the other four players I've
tried so far. I'm thinking about returning this one, it's really not
working out very well for our uses. I don't like the purely circular
design, because it's never obvious where the buttons are on it. No
'front'.
I did notice that the Panasonic will remember which track
it's on, but not where within that track. Better than nothing? It
uses the same power plug as the Philips. However, it also has that
wretched forget-the-loudness feature (pushbutton volume control rather
than potentiometer), and as it's also missing a line-out jack it's not
going to be any more satisfactory than the Philips. The cheap price
of the thrift specials is a lot more palatable than the brand-new
price of the Philips, given that none of them turn out to be what I
want! (Even though they're non-returnable.)
I'm thinking I might just keep buying thrift shop specials until I get
lucky. I can get a dozen or so for the price of that one Philips.
Tuesday, May 8, 2007
Ordered brake parts.
Returned the Philips to Wal-Mart. It cost too much for it to be
anything other than completely satisfactory.
Wednesday, May 9, 2007
Trouble! My wife called me and said the car wouldn't start. (She'd
just filled it up, too, it turns out. Four miles ago. Bad fuel?)
After much fooling around I ended up with the key and over at the
neighbor's where it sat. (Better that it acted up there than just
about anyplace other than our own driveway.) Apparently it would
crank OK, but not run. I pumped the (new-style) primer, which felt a
bit 'airy' at first, and it started right up. As we prepared to
caravan it home it started running rough and died. Weird. I pulled
the primary fuel filter and it was very free. So was the secondary,
we dumped it out and saw no sign of water or dirt. The contents
looked, felt, and smelled like diesel. The aluminum washer and its
seat look somewhat galled, though. Heavy-handed Hans may have had a
whack at it at some point in time. I blew backwards into the fuel
feed hose and that seemed to be OK. I pulled off the vacuum shutoff,
no difference: it would start fine, but not run well after a bit.
Sure seems like a cracked fuel line. As re-starting it was so
repeatable I gambled and drove it home, I figured that if it died I
could just prime it and get going again, limping home that way. It
ran great in S, the only trouble it had was again at low RPM's at the
house. I parked it and went inside, disgusted.
It could be, in no particular order:
- Cracked fuel line sucking air
- Leaky primer pump sucking air
- Galled fuel filter seal sucking air
- Bad fuel pump
- Occluded fuel strainer or filter
- Algae
I've got a new primer pump on the way that I ordered for the Frankenheap. I might try it in this car if
it gets here soon enough. One of the fuel return lines is weeping,
I'll replace that. I never thought the return system could cause
this symptom, but it's certainly easy to try a fix.
...When my wife got home she sheepishly admitted that upon reflection,
she'd put 15.5 gallons, $50, of gasoline into the car, not
diesel! She was in a hurry and was worried about running out of fuel,
so she'd gone to a different station than usual. She was positive
she'd done this, remembers "87" on the pump (octane), and noticed that
it didn't foam up like it usually did.
Yeah, that'll do it. That also explains the new-found 'stickiness' of
the primer pump, and the extra 'fuminess' I experienced when blowing
through the main fuel filter. The large reserve capacity in the tank
explains why I didn't think there was anything particularly wrong with
the fuel: the dilution wasn't quite so bad as to make it obviously
gasoline, nor to keep it from running. It explains everything.
Fortunately the fuel system in this class of car is extremely robust,
it is unlikely that there has been any lasting damage done.
She admits that she didn't really want to tell me what she'd done, but
I'm awfully glad she did. I don't know how much time and money I
could have wasted trying to find what was wrong.
Tomorrow I need to siphon out enough of the tank so that the three
gallons of diesel I have in cans here can push the gasoline dilution
down to no more than Mercedes' old-time recommended limit of 25%. That
should get me to the gas station where I can fill it up with diesel,
pushing the dilution down to something tolerable. Over time I can
then use up this contaminated fuel a little at a time, that should
keep the dilution from being harmful while not wasting the $50.
Anybody need 20 gallons of custom 'injector cleaner'?
Thursday, May 10, 2007
One whiff of the fuel filler neck with a fresh nose and the smell of
gasoline was obvious. Must remember to do this first in the future,
before my sense of smell is dulled by getting fuel all over the place
whilst messing with the fuel filters. I got out the siphon and all
the spare gas cans. I managed to siphon out about 20 gallons then put
in all the diesel I had on hand: about 3.5 gallons. We'll see. I
also replaced the weeping piece of fuel return line, and the end plug
which was also weeping a bit. (The gasoline seems to have exacerbated
the leaks.) Both ends of the string got replaced, the inter-injector
links are still OK which is good, as I'd just used up all the new hose
I had left. (In the miscellaneous department I also put in 2 quarts
of oil, I think it's burning some. I pumped up the tires, etc. Also
put the recycling into the trunk, might as well do that while I'm out
and about. Just the usual morning car routine.)
The car started fine but was a bit cranky at first and died once in
the driveway, just as before, but by the time I got to the bottom of
the hill it was back to normal. The 3.5 gallons was not enough to
turn out the low fuel light. Fueling, including replacing the
contents of the little cans, took 20.7 gallons, $60. That makes the
contaminated fuel better than 3/4 gasoline. Maybe it'll run fine in
the lawn mowers? We'll find some way to use it, that's for sure. The
car is running perfectly well again. Looks like no harm, no foul.
I bought another two CD players at the thrift shop that's next to the
fruit stand where I bought lunch. (They had about eight to choose
from.) One has a dead drive motor, but the other one works fine. No
anti-skip buffer, and it doesn't resume play. Oh well, I'll persevere!
Friday, May 11, 2007
When we got home from dinner out the sunroof wouldn't close. Stupid
switch, I pulled it apart while parked in the driveway and managed to
lose a piece (switch contact) down in the seat rail. Fortunately I
had another switch in the garage. It, at least, worked properly.
Also, the front passenger door check strap chose that moment to lock
up again, it's been making some noise lately. I'll need to address
that again. Not a good impression the car's been making lately.
The box of parts from Rusty came today, brake time!
Saturday, May 12, 2007
I dug the missing switch contact out from under the seat, cleaned
things up, and reassembled the switch. It worked fine on the bench.
Of course. It worked fine in the car too. We'll see if it hold up
this time.
Unfortunately, after jacking up the car I found that the rear calipers
were ATE, not Bendix. Oops! Wrong rebuild kits.
(The fronts were Bendix, and I thought I remembered that the
rears were as well. I guess I should have looked.) I put a set of
the pads on the scraping side and put it back down. Will have to
order the correct parts.
I opened the wonky passenger door and it wouldn't close again, no
matter the coaxing. So I opened up the door panel and removed the
door check. It looked OK, but wouldn't move properly. Messing around
with it blew out the side of the slider. It's dead, Jim. I dug out
the spare check strap, it's one of the old pot metal ones, but intact.
Put it all back together. Works fine again.
Friday, May 18, 2007
Happy volcano day! I ordered the correct rear brake rebuild kits, and
some more fuel return hose to replenish my stock.
Tuesday, May 22, 2007
Filled up today, I put in 2.5 gallons of 'Jill's Custom Injector
Cleaner'. The car ran fine, you can't tell that there's 2 gallons of
gasoline mixed in the tank. We'll be able to burn this stuff up this
summer.
The tiller was empty, so I put some of the crud in it, too. It ran
OK, but seemed a bit weak (though usable) and needed the choke on
halfway to run smoothly. If we can use it up this way too we should
be able to get rid of this stuff fairly quickly.
Thursday, May 24, 2007
I got out the replacement Becker 599. It worked fine, both channels,
both bands. I removed the modified Becker from the car and compared
the wiring of the volume control boards. No, it's OK. So I pulled
the modifications out of it and transferred them to the replacement.
That went fairly easily, I'm glad I made it to come back out again.
While I was in there I put in an additional power supply filter to the
external power jack. I dug a 2.25 mH torroidal choke and a
1 µF capacitor out of the junkbox and ran the power lead to
the jack through them. I think it has helped some in cutting down on
the motor noise from the CD player. I modified the schematic to
match. Oh, and the replacement Becker came with the missing tone
control knob and matching filler plate for putting behind the tuning
knob. Between the two of them I now have a full set of the cosmetics.
(And an extra knob.) Beauteous!
Another thrift-shop special, a Sony Discman of some sort,
induced hideous amounts of chirping, shrieking motor noise
into the audio chain. The worst yet, even with the new power
filtering. We keep looking...
Friday, May 25, 2007
Just wanted to note that the sunroof switch is still working properly.
Usually it didn't hold up this long. Perhaps it's finally fixed for
awhile? It is also time to note that the intermittent reverse-lamp
fuse-blowing behavior seems to be entirely gone, so I guess it was the
neutral safety switch after all. We shall call the surgery successful.
Tuesday, May 29, 2007
The remaining brake parts came. I also want to note that the
replacement Becker seems to sound especially 'tinny'. Not sure what's
up with that, if anything. Other than that it's working well enough.
The sunroof switch is starting to get cranky again. Sigh.
Wednesday, May 30, 2007
It's starting to warm up. When will I find time to recharge the AC?
Has to be warm out to do it right, so mornings (my usual car time) are
not a good choice.
Thursday, May 31, 2007
Brake day! I used the brake pedal to force out the frozen puck. As
always, removing the second puck from the caliper is the hard
part. I finally fabricated a seal/clamp out of a big washer with a
circle of inner tube rubber glued to it, and two 7×2×3/8"
strips of heavy metal plate to clamp it in place. I had to notch one
of the plates to fit around the grease gun's pipe. With two C-clamps
I could then clamp the seal into place yet still leave enough room for
the other puck to come out. It just walked right out using water
pressure from the grease gun. I have thought about fabricating this
clamp every time I've had to do this miserable job, I finally got
around to doing it! (I need to get a big bolt so that I only need one
C-clamp for this operation in future.)
With the sticky caliper all apart I got all the rust sanded out of the
bores (outside the seal) so the pucks would slide easily again. (600
grit wet-and-dry under running water in the sink.) They now fit
nicely into their bores and will slip out under their own weight. The
rubber parts were actually in fairly good shape. I'll still replace
them with the kits', but I will keep the old rubber for jalopy use. I
blew everything dry to prevent rust and set it aside for tomorrow. A
little WD-40 went into the clamps' Acme screws and the grease gun's
guts. (Water displacement [WD: trial formula 40] is what it's
actually for!)
I may want to paint the parts of the caliper where the rubber boots
clip on. Perhaps they will seal better keeping it drier inside and
helping to prevent further rust?
Tool fabrication took a lot of time so I was unable to finish the job;
I had to take the truck (with camper) to work. Perhaps tomorrow. I
did squirt PB Blaster on the hose fittings to let it work overnight.
Friday, June 1, 2007
More brakes. I spray-painted the caliper black, taking some care not
to get paint inside the bores, and put it in the shop oven to dry. I
then removed the other caliper and rebuilt it as well. I used a
Dremel wire brush to clean out the grooves in the pucks, as well as
the seats for the boots. Experience and having the right tools really
makes it go quicker. I also gave it a blast of paint and put it in
the oven.
The master cylinder came off easily, and once it was off I stuck a
plastic tube (from my topside oil sucker) down in the booster to the
bottom and sucked on the other end. A lot of nasty-looking fluid came
out! It was definitely time to replace the master cylinder. I washed
off the booster and blew it dry, then rattle-canned it black. There
was a lot of paint gone because of the brake fluid leak. I then
installed the new master cylinder and transferred the reservoir to it.
The calipers went back together easily. The big secret is to put the
boots on the pucks before they go into the bores, otherwise it's a lot
harder. Brake fluid is used as an assembly lubricant. I don't know
if the orientation of the asymmetrical face of each puck is
significant. I could find no information about this, so I didn't try
to line them up with anything in particular. The calipers went back
on the car, and the hoses were replaced. The PB had presumably done
its job, the old ones came off easily.
Finally I enlisted my wife's help to bleed the brakes, which went
smoothly. I then cleaned up the mess.
...Driving to work the brakes worked very well. No more squeaking and
scratching noises, and braking power was even and good. Nice. At
lunch I stopped at Schuck's and NAPA, but neither had the little
rubber covers for brake bleeder screws. I'll liberate some more next
time I go to the U-Pull, I'm missing three. It was hot out today,
time to work on the AC! (It needs a charge.)
Saturday, June 2, 2007
I jacked up the front of the car. I then wire brushed off the
brake-fluid-damaged paint areas and rattle-canned black paint on
there. I even had some medium blue that I used to hit the bodywork
below the brake booster. I found a can of spray-on undercoating, so
once the paint had dried I put that on the bottom surfaces. I did a
bit of chipping at the undercoating on the rocker panel, and it was
good. One small loose spot I removed and treated as above. No sign
of rust in the rocker panels, or anywhere else underneath. The body
brace behind the driver's brake strut was loose so I tightened that.
I vacuumed out the crevices in the hood hinge areas.
I then checked steering linkages. All seemed tight, yet I could still
wobble the wheels a bit more than I liked. I backed out the adjusting
nut on the steering box 3/4 turn, about half of what I could back it
out using only my fingers. (Which was definitely too far.) It's not
really much tighter, but we'll see how it behaves. I don't think I
went too far, but we'll see. If there's a 'notch' in the steering
around center I'll know I definitely went too far and will have to put
it back some. The steering box may be worn out, or I (working alone)
may have missed something loose beneath.
I next drained the tranny fluid. I enlisted my 5-year-old son's aid
to lie under the car on the creeper and tell me when the torque
converter drain plug showed up in the access window while I rolled the
car over via the power steering nut. Slick. I dropped the pan and
found it pretty clean inside. The fluid in the pan was a bit murky,
but not bad. Stinky, too, like mothballs. Fresh fluid smells more
fishy to me. I removed the filter and put the new one on. (There's
no way you can do this job without getting oil all over the place, no
matter how careful you are.) I washed off the pan, and scraped off
the grime on the outside. I mopped it dry and wiped it out with my
hands to remove all lint and grit, and set it in the sun to finish
drying. I put on a new gasket, wiped off the pan gasket surface on
the bottom of the tranny, and reinstalled the pan. I then poured in
three quarts of fresh fluid, started the car, and poured in another
three and a half. No leaks appeared during this.
I took the car for a quick test drive and it drove normally. The
transmission shifted as before. Sadly, there was no miracle cure.
The steering seemed a bit tighter, and I don't think I've taken it too
far. We then broke for a late breakfast. (My boy was still hanging
about.)
In the heat of the day (80's) it was time again to charge the AC for
the year. I put on the gauges (why, oh why, is that stupid high-side
fitting on the bottom of the car?) and found there was still some
residual charge, so there was no need to vacuum the system. I put in
a can of Isopro, AC on, and then followed it up with a slow propane
leak until the gauges looked right. Some time during this the
auxiliary fan started up with a roar. Looks good. I put a mister on
the condensor and got in and revved the engine to 2000 RPM
. The vent temp gradually dropped to 45 °F, which is
about as good as you can get in this car. I buttoned things up, and
tightened the Schrader valves a bit before putting on the caps. The
high side valve seemed a bit loose, perhaps that's where the last
charge went. On a short test drive the vent temps got down to
47 °F which is OK. Not as good as the 38 °F that
I'd gotten once, but tolerable. The AC seems
to cycle on and off yet the vent temps aren't at their lowest.
Probably the pressure (charge volume), or perhaps the gas ratio, is
off a bit. If it's overcharged that should self-correct through the
season.
With all this done the scheduled operations for this car (this year,
anyway) are done. Now we'll just drive it, and I'll try to work on
something else. Until something breaks!
Monday, June 4, 2007
That didn't take long. We drove to band in this car and the AC kept
cutting out, especially on bumps. I'd suspect the blower brushes,
except that I could hear a definite click behind the control panel
each time it cut in or out, and cycling the switches would bring it
back. I think it needs some more resoldering and/or contact cleaning.
I suppose it could be fuse related as well, I'll check that too. (OK,
I think it has had this problem for awhile, but it was less noticeable
in the heating season.)
Other than that, and its current cosmetic challenges, the car is
sweet. Purrs down the road like a kitten. It is shifting
better than it was, at least a bit, and the steering feels better.
The brakes are now unremarkable. That is, you no longer notice
anything, it just stops like it should.
Tuesday, June 5, 2007
Another thrift-shop CD player. Had a Resume switch on the side, so it
might be what we need...
No, it doesn't really work, and takes a long time to sync up to a
track. Bad laser?
Wednesday, June 6, 2007
I removed the ACC panel. After I opened it up I could see that some
of the joints on the switches were crystallized, a few didn't look
like I'd ever worked on them. I recall now that the joints to the
side boards had been broken when I got the car and that is what I
spent the most time on. They still look good. I dug out the hot iron
and attacked the troublesome joints on the main PCB. It takes a lot
of heat to do some of the relay pins, and I've had trouble using my
regular iron for this before. That's why I have an extra-hot
iron, for the hard cases. Anyway, it went well enough, after which I
shot contact cleaner into the switches and worked them. I then put
the panel back in the car. We'll see how it works.
...On the way to and from work today the heater worked perfectly.
(We're having a cold snap, no AC this week!) It's a little early to
tell if the problem is fixed, but it's certainly a good sign. I know
that the heater occasionally needed a jump-start by turning on and off
the AC, yet the cold engine lockout switch tested good. It didn't need
any such help today.
Friday, June 8, 2007
Just wanted to note that the ACC seems to be behaving itself. Haven't
needed the AC lately, however, just heat.
Friday, June 28, 2007
Locked the car in the morning as we were going on vacation. (It
hadn't run since yesterday.) All the locks operated, naturally.
Monday, July 9, 2007
Unlocked the car to go to work after the vacation was over. All the
locks operated, the vacuum system is thus good for more than a week.
Good. I should also note that the tranny is shifting better than
ever, even the 3–4 flare is improved. We may have staved off
the bad tranny wolf for a bit. Also good.
Sunday, July 22, 2007
The odometer has finally stopped, this is a common malady with these
cars. Supposedly a drop of cyanoacrylate glue on the shaft will fix
it, naturally getting to the right place is the hard part of
the job.
Monday, July 23, 2007
I removed the failing odometer from the car. I looked at putting
cyanoacrylate glue on the shaft, and even tried a bit, but it didn't
want to wick into where it needed to be and tried to sieze the shaft
where it goes through the frame. Things are just too tight there for
the 'quick fix', I don't know how anybody does it without ruining the
odometer. Time for Plan B. I removed the face of the speedometer,
first lifting the needle over the zero stop and ensuring that it
rested on the little mark on the edge of the dial that marks its zero
tension position. I then used the two-spoons trick to pop off the
needle. Next I removed the odometer drive shaft entirely, liberating
all the plastic dials. The pot-metal drive gear (in the non-visible
tenths position) was really quite loose, but sometimes would bind a
bit. Looking inside the bore of this gear it appears that there might
be a bit of spring wire coiled in there that is supposed to 'bite' on
the shaft. Anyway, I knurled the shaft where the metal drive gear
seats using a pair of pliers. One must be very careful not to mar the
shaft where the plastic dial gears are as they must spin freely.
While it was apart I used alcohol and a swab to clean all the dial
faces, the trip odometer was particularly filthy. I then reassembled
the shaft and dials, which was not easy. It took a few tries before I
got everything aligned so that it would function and the dials lined
up through the holes in the face. I added some miles to its reading
to partially compensate for the (short) time that it was broken. I
had to tap the shaft into its final position with a hammer as the
knurling made for a tight fit. After it was all together it worked
freely when driven by my thumb. I then reinstalled the speedometer
face, put the needle on the shaft so that it pointed at the resting
mark, then lifted it back over the zero stop. I then greased the
drive gears and put some M1 5W20 on the sleeve bearing. With this all
done I reassembled the instrument cluster and installed it back in the
car. I also squirted a bunch of oil down the drive cable. We'll see
how it goes!
Regarding the apocryphal warning against resetting the trip odometer
while moving, having just become intimately familiar with the guts of
the offending unit I can in no way see how resetting the trip
odometer, moving or not, can place any significantly greater torque on
the drive gear. If it does, the amount is nearly trivial and the
drive gear is already about to fail. It takes considerable
torque to roll over a bunch of dials at once, that drive gear is
supposed to be tight.
...and it works. Good.
Thursday, September 13, 2007
I found an interesting link involving slipping shifts for these
transmissions: Here
Saturday, September 22, 2007
Road trip! To Yakima and back, its home before ours. Car worked
well, but the cruise control didn't want to resume. That's because
the switch hits the back of the steering wheel! I wonder why that is?
There was a weird little intermittent screechy scraping from the left
rear of the car while returning home on the freeway. I will have to
keep an eye on this just in case it wasn't a small rock trapped in
there.
Monday, December 3, 2007
The passenger door check is 'grunching', so I took it apart to grease
it. Oops! Wasn't the (old-style) check at all, in fact it was the
side trim of the door rubbing on the fender. Old-style checks aren't
prone to seizing, anyway. I greased the thing since I had it apart,
and the hinges as well. Grease on the offending molding stopped the
noise.
Friday, December 7, 2007
After many complaints from my wife, and some goading from successful
examples on the mailing list, I removed the instrument cluster, pried
off the light pipe covers, and lined the pipes and the lamp
compartment with aluminum foil. Dabs of Shoe Goo hold the pipe covers
back on. I put the cluster back into the car, but didn't push it back
into the hole yet. No way I want to there to be any chance at all
of gluing the cluster into the car!
Sunday, December 9, 2007
Jill's been complaining about the car driving 'wonky', and the last
time I drove it I thought there might be something wrong with the
front left tire, so I'd jacked it up and give it a spun, but noticed
nothing wrong.
Well, today I followed her home, and OMFG, the left rear
definitely has a problem. Even Daniel could see it, and he's no car
expert! When we got home I took it off, and there's something like a
1/2" bend in the tire, the tread's now in a serpentine course. Shot
to hell. These tires are the original Michelin Arctic Alpins that
came on it five years ago (and they weren't new then), but they're
pretty much worn out anyway. They're 195/70R14's, but we got a set of
studded 205/70R14 Hankook tires (no wheels) with the 380 SL that should serve. Relatively few miles
on them, the tread looks very good. I removed the bad wheel and put
on a spare that I had on a bundt rim to get her through today, I'll
send the load of Hankooks with her in the trunk to have put on at the
next opportunity.
This evening she reports that the wonkiness (tire wobble) is all gone,
and that the dash lights are almost tolerable in brightness.
Monday, December 10, 2007
Hankookified!
Tuesday, December 11, 2007
Jill asked me today if the car wasn't supposed to have a piece of
molding on the driver's door. "Why yes, it should." Apparently the
thing fell off somewhere in the last day or two. All but one of the
round retaining clips are gone from the door, the one left is near the
back. Probably there were two left, and when the (front) one fell out
or broke the whole thing stripped away.
Crap.
Thursday, December 13, 2007
Jill found the missing trim in the driveway today. Looks to me like
it got run over once, but is probably still usable. Oddly, it didn't
have the stock red plastic retainers, it had some weird metal clips.
That's why it fell off, no doubt.
She also reports that the car only got something like half the normal
mileage this last tank. I've been smelling a bit of diesel around her
car lately, I guess there's a leak. I popped the hood when we made
the son exchange today, and I could see that the line from the fuel
pump up to the filter was wet. This could be just the line, or perhaps
the (new-style) primer pump could be leaking. A couple of the return
lines are also wet.
Friday, December 14, 2007
I replaced two pieces of large fuel line, and three sections of the
skinny return line. The large was generic McParts, but the skinny
stuff was official. With any luck...
I also filled the washer tank with some mixed-up 20/20 and a shot of
isopropyl alcohol, and topped up the engine oil.
Tuesday, December 18, 2007
I finally got a chance myself to drive the car at night, and the
instrument lights are indeed brighter. One can actually read the
odometers at night now.
Thursday, December 20, 2007
I finally had some time to take a look at the mashed trim strip. The
old nasty incorrect metal retaining clips pulled easily off the trim's
bumps, all the bumps looked good. I dug in my junk box to find six of
the correct red plastic retainers (used), and snapped them into the
car's door. The trim then just snapped into place. Looks a little
wonky, but better than it did without trim at all. I'll have to keep
an eye open for a better used strip at the junkyard.
Saturday, December 22, 2007
On a trip back to Yakima Jill was driving (and thus had control of the
heat), and I was baking. When we swapped it turns out that there is a
small cold draft in the footwell of the driver's side, which is
missing the underdash panel. (I'd taken it off for access years ago.)
I'll have to do something about that. The steering is a bit loose and
darty too, which is not normal for this car.
Sunday, December 23, 2007
On the trip back from Yakima I found that the engine was squealing a
bit as we got home. I checked the belts, and found the alternator
was very loose. I hand-tightened it which restored the belts
to a more normal tension, but it squealed even worse on a short trip
after that. I need to tackle it more properly tomorrow.
Monday, December 24, 2007
I tightened the alternator belt some more and the squeal seems to
have gone away. We'll see. Since I was there, and it was sunny out,
I dug out the missing under-dash panel, which took some finding. (It
turns out I had stored it in the trunk of the 250C.) The staples holding the two halves
together had failed, so I pried them out and glued the two pieces back
together, clamped them, and set them aside to dry. I also jacked up
the front end of the car to have a look, and it appears that the idler
arm might be a bit loose. The steering damper is also not what it
should be, so I'll need to order those two (wear) parts. The ball
joints and tie rods all seemed fine. The steering box may need
replacement, I think it may have too much play in it. I already
adjusted it once in June.
...This evening the driver's lock felt weird when I locked it at
church. (And isn't that necessity an indictment of modern
times!) When I got back out I couldn't turn the key. At least I'd
repaired (long ago) the passenger door keylock, and could get in that
side. I don't think it's just frozen, but we'll see tomorrow.
Tuesday, December 25, 2007
I installed the under-dash panel. (It was surprisingly difficult to
get that thing back into place, which I think I recall from working
with it before.) That should (I hope) stop the draft. Merry
Christmas, honey.
The door lock works again. I think it was just frozen. I also think
it could use some lubrication.
Thursday, December 27, 2007
I wrapped a bit of duct tape around the torn speedometer cable boot.
Could that have been the original source of the draft?
Friday, December 28, 2007
Jill finally drove the car again. She didn't have too much to say
about the draft thing (it's early days, after all), but did
comment on its quieter nature.
I also ordered the steering damper and idler arm kit.
Tuesday, January 1, 2008
The car hadn't been driven for a few days, and again it started rough
then died, and required much cranking to get going again. It may be
that we have an air leak in the fuel system causing loss of prime.
Monday, January 7, 2008
The steering parts came today. Jill managed to get to the box on the
porch before the dog did.
She also took the time to point out to me that she hates the
iPod-ified radio, always has, and wants a plain in-dash CD player. Oh
well.
Tuesday, January 8, 2008
No time for installation, but I did put the steering parts in the
trunk. Whee.
Friday, January 11, 2008
I installed the new steering damper and the idler arm kit. Jill
reports that she has noticed nothing, it may be that there is no
material improvement. After installation I didn't think the new idler
arm kit made any difference in 'slop', so I saved the old parts for
jalopy use. I probably need to replace the steering box if I want to
actually tighten things up any more.
Sunday, January 13, 2008
Driving the car I can definitely detect that the steering is more
damped than before. Not tighter, but not sloppy-loose. Still a huge
contrast with the very tight steering of the Frankenheap. (Which may indeed only have
50kmi on it as its odometer indicates. Its steering is tight, and its
engine starts readily in the winter. On the other hand, it's not
power steering so that is probably inherently tighter.) Still
thinking about that spare steering box in Smelly (the 300D parts car
in the woods). Don't know what kind of shape it's in, however.
Sunday, January 20, 2008
Seattle road trip. A few thoughts come to mind. One is that the car
might need a new thermostat, it was quite cold out and the engine
temperature was a little bit low, and cabin heat was approaching
marginal at times. There is still a draft in the driver's footwell,
now it's leaking out from behind the panel at the parking brake. Not
as bad as before, but not optimal. Weather in the teens is bringing
out the problems, naturally. The steering is too loose. I
need to pursue a replacement steering box. Perhaps they just don't
make it to 300kmi? Mileage was sub-par, about 23 but verging on 25 on
one short easy leg. No obvious fuel leaks or dragging brakes to blame
it on. The RR door check is starting to bind, I need to take care of
that pronto. Other than that, and the ratty windshield and poor wiper
blades, the car behaved pretty well.
Hmm, I guess this doesn't add up all that well after all. Most of it
is fairly straightforward to address, but there's a few stinkers in
there.
Saturday, February 16, 2008
I opened up the RR door. The replacement (used) check strap still
looked OK, but the grease had dried out in the track and there was
some corrosion starting up. I put it in the solvent tank while I had
breakfast.
I then took it apart and cleaned off all the grease and dirt, and
found that one of the two large BB's was getting rough and corroded.
I put it in the angle of one of the welding magnets and brought it to
the wire wheel, and with some brushing and spinning I got it much
smoother. I then sanded off the tracks in the solvent tank, dried
everything off, and greased it all up. Getting it back together was
(as always) a real joy. It didn't go too badly, I used a woodworking
bar clamp to compress the BB's into the slider with it nearly in
starting position on the track, and then used a heavy iron bar and the
BFH to drive it into the track.
I put it into the door and tried it out. Not as smooth as new but
tolerable. I then reassembled the door, everything works fine now.
Sunday, February 17, 2008
My wife's taking a road trip today. So I prepped the car. Changed
the oil, first time in (OMFG) 17kmi! Last record I have is sometime
in '02, though the ATF and filter has been changed twice in that time.
Somehow this one got away from me, imagine that. It came out kind of
sludgy, even though warmed by a long idle. Delo may be good oil, but
it's not that good!
I didn't even get to change the filter, turns out I don't have one.
Boxes of 60x filters, no 61x filters at all. I think I bought one,
and that's what I used in '02. Next time. I'll do a short service
for this batch, call it a sludge-removal stage, then change both
oil and filter. Stupid.
Oh, and Jill pointed out a cut in the driver's seat belt, it probably
got slammed in the door latch. I'll get a replacement next time I
find a 123 in the junkyard.
Wednesday, March 12, 2008
Jill reports that the car's transmission slips sometimes when cold.
Theorizing that the small ATF leak is to blame, I poured in half a
quart that I had in the trunk. We'll see.
Tuesday, March 18, 2008
I put the car down below, now that Jill's driving the 190D. It's time to stop driving with studded
snow tires, anyway.
Friday, November 28, 2008
Snow car day. I put the battery charger on the car after I got the
Frankenheap going, and it drew a heavy
charge. (It needs a battery cutoff switch too.) After it had charged
a while I tried to start it, but nothing doing. It would cough a
little bit, but not run. I tried priming the fuel system, and
nothing. I tried several times, but I don't think I was waiting long
enough. I even stole the boat's battery (which
I'd been meaning to bring inside anyway) and used jumper cables to tie
it to the car's battery, but nothing doing. With the extra battery's
help I did get it to run once, but it died after a few
seconds. I cracked the fuel bolt and primed, a lot of air kept coming
out. I wonder if I've got an air leak in the fuel system? I decided
to let it charge overnight before trying again. It's a drag because I
threw all the Christmas decorations in the car to haul it up top, and
now it'll have to wait as I don't want to unload it all and bring it
up by hand in the slippery snow.
Saturday, November 29, 2008
The first crank-fest didn't work, so I primed it again. This time I
could feel and hear it 'take', and when I tried starting it again it
started, no problem. I was able to run it up the hill in spite of the
snow, I left it idling to warm and dry out the interior while I
unloaded the car and put the lights and decorations on the garage.
Saturday, January 31, 2009
I readjusted the headlights, they were a bit wonky. I tried the fogs,
and it blew the fuse immediately on the passenger side, taking the low
beam with it. Great, more work!
Sunday, February 1, 2009
The problem was that the fuse had corroded and stopped making good
contact, but it didn't blow. I replaced it with another, and the
lights worked again. I also burnished the contacts in the fuse box.
Monday, February 16, 2009
I stopped by the U-Pull today,
and got a driver's seat belt from an older 123. I hope it fits, I've
been looking for a year. I also got a pair of tire chains, Jill will
feel more comfortable with them in the trunk of her winter car.
Tuesday, February 17, 2009
I checked the seat belt, and it fits. I used vise grips to keep the
belt extended from its roller. I then washed the belt out in the sink
and hung it to dry in front of the fire while I removed the old belt.
(They roll a lot easier when they're clean and supple, rather than all
dirty and stiff.) Installation was fairly uneventful, I left the belt
out and buckled to the other seat to facilitate drying.
I also noticed that the center belt in the rear has a nick in it, and
the passenger-side rear belt's plastic handle is broken. Today?
...At the U-Pull today I picked
up the two seat belts. I had to get the driver's-side rear belt, but
it should swap OK if I just turn over the buckle on the belt. I also
got the driver's-side door molding to replace the one that got driven
over last December.
...In the evening I washed out the two new belts and hung them in
front of the fire to dry overnight. They were filthy! While the one
belt was all nice and wet and slippery I turned it over in the buckle,
so it should fit into place tomorrow on the opposite side of the car.
Wednesday, February 18, 2009
I removed the rear seats of the car, opened up the C-pillar cover and
removed the one seat belt with the broken plastic on the buckle. (I
found a mouse nest inside the rear seat back, how nice!) The new belt
went into place fairly easily, though it doesn't have the anti-twist
plastic guide behind the shoulder mount point that the newer ones
have. The new center belt turned out to be sufficiently different
that I couldn't use it, the original shared a mount point with the
receiver for the side belt, the proposed replacement did not and was
an individual piece. So I left the nicked center belt in place. The
side plastic C-pillar cover is all buggered up, which is no surprise
as that whole rear area is a mess. Somebody who worked on it
previously was a hack.
Monday, March 9, 2009
I jacked up the LF end of the car and checked the suspension and
brake, Jill has mentioned a 'clunking' when braking (which I haven't
noticed when I've driven the car). Nothing wrong that I could see/feel.
I then added some ATF, because I have noticed some slipping
at times. The dipstick (cold) showed low again, so I felt fairly safe
here. I also refilled the washer tank and topped off the radiator
with a little water, it was a bit low. I wonder when I last serviced
the cooling system on this car? 'tis a pity I didn't start keeping
good records earlier.
Saturday, March 14, 2009
Preparing for yet another trip in the Yakamobile I found that the AC
belt was broken and chewed up. The compressor hub doesn't seem to be
seized, so I'm not too sure why this happened. I'll look into this
sometime later.
Saturday, March 28, 2009
I removed the rock-pipped and wet driver's-side fog light and cleaned
it out. (This necessitated removing the light's rear lamp fitting,
which is tricky to remove from the glass and metal shell—you
have to bend back three bent ears that hold it on.) I then used clear
5-minute epoxy to fill the crater. (The original glass bits were too
shattered to restore.) In five minutes (?) it was dry enough to
reassemble and put back. Now this one matches the other side, which
also had a big rock pip in it. Though the epoxy yellows with age, on
these yellow fog lights that's not a problem at all.
Wednesday, April 1, 2009
Today at the U-Pull I was
shopping for parts for the 560 SEL and found
that the 123 they had in still had one of the little plastic screw
covers for the knee bolster, this will fill the one remaining hole in
our dash. Yay! I also got another rear center seat belt, this one is
a double-header like the bad one. I got a 190E's dome light, which
looks a lot like the 123's except with an auxiliary reading lamp.
Maybe it can be adapted, the switch on this car's light is getting
really flakey. I also found about $2.25 under the rear seat,
including the first-ever bill I've ever found in such a place, so that
paid my way in. I noticed that the steering box on the donor is
tight, I should come back Saturday and get it, the one on this car
sucks.
Saturday, April 4, 2009
I went to the U-Pull and got
the steering box. This went fairly well, though it's a surprisingly
expensive part ($22), and they charge extra for the Pittman arm ($13).
(Like you can actually remove one of those with any ease.) I also
picked up the glow plug relay, engine-side wiring harness for same,
and the three pencil-style glow plugs left on the engine. A veritable
bargain: $3 for all that—the price of a relay. I was there less
than two hours, and that included browsing around the other cars.
At home I got the car jacked up before we had to go off for dinner.
I'd hoped to get further along, but no...
Sunday, April 5, 2009
I started removing the steering box. I cracked loose every bolt
before beginning to remove everything. It was all pretty uneventful,
practicing yesterday certainly helped. (The puller I'd made for these
joints works excellently. Some pressure and a few hammer taps and
POP! Off it comes.) The tie rod ball joint had a torn boot, though
it hadn't worn loose yet due to dirt getting in, so I pulled off the
boot and cleaned it off and out with brake cleaner. I used
cyanoacrylate glue to tack the boot's tear together, then potted it in
Shoe Goo for strength and set it in front of the fireplace to dry
while I proceeded. I got the steering box out, that went easily
enough. When removed I could see some frame rust underneath it, so I
brushed it off and hit it with some black paint. Trying to put back
the new steering box was difficult. It was too heavy for me to push
up from below, not from the angle I could reach, and even if I could I
couldn't see to attach it to the steering shaft. Instead I tied a
string around its shaft and ran it through a hook in the ceiling, and
lifted it up to almost the right height and tied it off. Then I could
use both hands from above to try to finesse the thing into position.
Once I spread the retaining collar with a screwdriver and a hammer the
thing then went on, and reassembly was uneventful. I cleaned out the
one dirty ball joint and pushed grease into it, then slipped on the
repaired boot. That should help keep it good for a few more years.
I then filled up the reservoir and took it on the road. It was much
better, but still not as good as our other cars. So I began
tightening the adjustment screw (CCW!) fractionally and then driving
again. You do not want to go too far! I think I ended up
about 1/4–1/3 turn by the time I decided I'd gone far enough,
over about six tries. The car drives infinitely better than it did
before, so I'll call the whole thing a success. I did have an oil
leak on the low-pressure line, so I tightened that some more. We'll
see if I got it, I may need to take it off and clean up something if
it keeps oozing. I have a spare hose that came with the new steering
box if I should end up needing it. (I kept the hoses on the donor box
to keep dirt out of the guts at the junkyard.)
I'd say that's $35 well-spent.
Tuesday, April 7, 2009
Today I drove the 380 SL, and it said
75 °F on the bank sign. Hard to believe that we had maybe 4"
of snowfall not even a week ago. I think I can now swap Jill to
another car safely. I put the car down below and disconnected the
battery for the summer.
Sunday, November 21, 2010
Got the car out for the Winter. (Long past time to switch cars!
The 560 SEL is not yet ready to go.) It was
sub-freezing today, and snowing, but starting was not an issue. With
the battery reconnected, the tires pumped up, and a battery charger
connected for a bit the car started immediately. No problems. I ran
it up top and plugged in a space heater to fully dry it out.
Wednesday, November 24, 2010
0 °F this morning, and the car wouldn't start for Jill when
she went to leave at about 10AM. (It hadn't been
plugged in.) The battery wasn't up to trying more than once. It got
it plugged in before we left, and when I got home from work I put on
the battery charger, and after 15 minutes I started it without any
difficulty. I left the charger on overnight, too.
Thursday, December 16, 2010
The rear dome light wasn't coming on, and it wasn't the fuse. When I
pulled the fixture the bulb was good, but it had corroded a bit and
wasn't making good contact anymore. Easily rectified.
Friday, December 17, 2010
Again with the rear dome light. I scraped it better this time, we'll
see if it holds. I found a front dome light assembly, with auxiliary
map light, in the glove box that I'd obviously procured at some time.
I disassembled it and cleaned the contacts, and used a little light
lithium grease on the thumbwheel pivot and detents. It works nicely,
and worked well when installed.
Saturday, January 1, 2011
The car has acquitted itself well the last week we've been on
vacation. It rolled over 300kmi early in the trip, runs like a top.
This morning we were back on the East side, in Yakima which was
actually a bit warmer than what I later found here at home, and temps
were colder than we'd been experiencing up 'til then. It was in the
teens this morning when I went to start. Two full glow cycles and it
still didn't go. Another two and the battery was getting weak, but I
kept on the starter and it finally started firing. After a bit it was
running, died once, and I laid on it again until it was running. Then
it was fine, I left it idling to thaw out and recharge the battery.
It really wants to be plugged in under such conditions! I'd
say we put on about 1000 miles this trip. We got 23–25 MPG.
Monday, January 17, 2011
Ordered a new ($12!) windshield washer splitter/check valve, MB P/N
000 860 08 62, the old one has blown apart and is
leaking badly. The tie wrap holding it together isn't really doing
the job.
Thursday, January 20, 2011
Today at the junkyard I got a replacement washer splitter. It's more
fitting to put used parts on this car than new, where practical.
Saturday, January 22, 2011
I installed the used washer splitter. The new one that came yesterday
can stay in the parts reserve. [Since
used in the 190D.]
Sunday, March 13, 2011
Jill called from the gas station and said she couldn't get the key out
of the ignition. I went and found that the lock cylinder appeared to
be 'caught', and with a lot of jiggling I freed it. It wouldn't cycle
to 'unlock', and the ignition lockout prevented it from starting
again. I think it's time to order a new ignition cylinder with key.
(The one that was in there when I got the car was cut up, probably due
to a sticking incident, and I transferred its brass locking wafers to
a different cylinder from a parts car. At the time I didn't want to
invest in an unknown car, but the car has been reliable enough that
it's worth a bit of investment now. Also, a spare key would be nice
to have.)
Tuesday, March 22, 2011
New license plates, 'required'. The State has found a new revenue
source...
Last night on our trip to a concert the sunroof was dripping on my
tuxedo. At least I was the passenger and could fend it off. This
morning it wasn't raining so I opened the sunroof and checked the
front corner drains. (It was cold and the roof was sluggish, but
operated correctly nonetheless.) I slipped a windshield wiper blade
spine down into the front drain channels, and when I blew compressed
air into them I could hear it coming out by the wheel wells. There
was a piece of rubber seal about 4" long that was loose underneath
the windbreak support rail on the dripping side. No sign of where it
should have come from, nor one on the other side, so I removed it on
the theory that it could have been impeding water flow and causing it
to spill up over the rail when braking. I blew air backwards to the
rear drains, but couldn't hear anything. We'll see if this little
operation has helped any, the rains are due to continue for awhile.
Saturday, April 2, 2011
The rear dome light still wasn't coming on, that was really puzzling.
I'd had it apart for cleaning several times, and it's a different
bulb too. I took it out of the car and checked the power plug with a
test light, there was power. But the bulb showed no continuity on the
bench, yet looked fine. I fiddled with it and one of the end caps
came off in my hand! The end wire had corroded in half, and since I
didn't have another bulb readily available I scraped the nub and
soldered another wire to it and soldered that into the end cap's hole.
It worked again, and next time I'll know just what to do. (Replace
the damned bulb!)
Windshield glass replacement is imminent, I scoured the garages for
the windshield seal I'd bought years ago and couldn't find it. Very
distressing! (Though not all that surprising...)
Wednesday, April 6, 2011
Windshield day! The guy showed up and we moved the car
into the garage and out of the wind/rain. He brought new Pilkington
glass and a Precision (brand) gasket. The new gasket looked good:
heavy dense material, formed corners, etc. The new glass looked good:
no waves that I could detect. The old gasket was cut out and the trim
and glass were removed. No rust was seen under the gasket, it looked
quite good to me. He stretched out the gasket and fit it to the frame
first, then he pulled it off and put it on the glass. Glass cleaner
was used as lubricant, as required. Then he wrapped a 1/4" cotton
(?) cord around the outer channel, 1 wrap. Then he put on the glass and
roped it in. He took his time, and there was a lot of fiddling,
pushing/pulling with the aid of a big rubber suction cup, slapping of
hands on glass, kneading of the gasket, work with various picks and
plastic wedges. A gigantic PITA, and we're leaving out all of the
false starts. Voila, after about two hours the glass was in, but the
locking trim was not. I had to go. Apparently shortly thereafter he
did too, but came back in late afternoon to finish. While trying to
put in the trim he broke the windshield, three cracks from top to
bottom, nearly in the center! He left in disgust, no charge. Trim
still not on the car. Not sure what the next step is, or should be.
He put in maybe four hours, a new gasket, and new glass. We put in
nothing but the heat and light in the garage. So far. (We do have a
new gasket and no pitting, but it's still broken and the trim is out.)
I think I'm glad I didn't try this myself. (If I had I'd have done
what worked for the Chevy: trim in the rubber
before it goes into the car. OTOH I broke that glass too, but at
least the trim was on.)
Friday, April 15, 2011
Jill started off on a road-trip halfway across the state today, and
called because the car was shrieking at her. Very displeased she
headed back home whereupon I tightened the alternator belt, which had
(somehow) gotten just about as loose as it could be. Odd.
Monday, April 18, 2011
Jill's back, and said that for the last few miles it was starting to
chirp again. I checked, and the belts were completely loose again.
Whatever's supposed to hold the belt adjustment in place is not doing
so, I'll have to look into that. I tightened it up again, it'll hold
for a bit anyway.
...And a bit was only one morning. It was shrieking again at lunch
time, and was completely loose. I tightened it, went to the auto
parts store, and procured some blue Locktite to douse it with. We'll
see if that holds.
Tuesday, April 19, 2011
From the mailing list: "There are 3 bolts that have to be loosened."
I looked closer, and he's right. The top bolt had a 17mm nut that has
disappeared. I replaced it with one from the junk box, with lock
washer, and tightened it. That should help immensely. I see in this
log that there was an earlier episode of belt
squealing, I think the nut has been missing for at least this long,
perhaps since we got the car. The state of the exposed end of the
bolt would support that, it looked 'old'.
Friday, May 6, 2011
The Sony Discman (car-ready) CD player shrieks and burbles weirdly,
and today I finally noticed that the noise is coming by way of
the power plug! When I powered the Discman with batteries,
yet left the power plug in the radio (which is what causes the audio
input cutover) it still made noise. The other power cable (for a
different portable CD player) doesn't do this. Very weird. I'll make
a new power cable for the Sony, that should cure it.
Saturday, May 7, 2011
The LF tire is wearing excessively on the outside. I rotated the
tires on that side to mitigate the problem, at least until/unless it
gets addressed properly.
Friday, May 20, 2011
Long past time to put this car away for the season, but no chance to
work on it 'til today. I wire-brushed the rusty spot under the
bumper, it's where the RF fender joins the front piece of metal. It
holed, but it's not really in a visible place so I contented myself
with cleaning it off, priming it, and shooting some random rattle-can
silver paint at it. The color blends in far better than I'd thought
it might.
...After work I cleaned out the car and ran it down to storage for the
season. I disconnected the battery this time.
Sunday, November 6, 2011
Time to dust off the car for its winter tour of duty. I charged the
battery and started it, first having to do a little work on the
positive battery clamp to get it to connect tightly, and it started
easily. Then it died after idling a little while and refused to start
after that. I primed the fuel system and charged the battery, but no
go. It tried, but wouldn't fully catch. I finally grabbed one of the
batteries from the genset and some jumper
cables, which did the trick. A huge black cloud poured out of the
exhaust, the engine had gotten loaded up with fuel. I ran it at high
RPM for awhile to stabilize, and after that no problem. I drove it up
top and put in power steering fluid and aired all five tires, then put
it back on charge to replenish it after its episode. The battery is
thirsty. Will need to clean it out, washing glass and etc., but for
now it looks nearly ready.
Thursday, November 10, 2011
Another dust-up about the audio system in this car, so to solve (?)
the problem we stopped by Car Toys and bought a new Alpine CDE-100 CD
player. On sale, $99 with installation, not that I'd let the
clock-racing butchers near one of my cars, not even a Chicken
Wagon! (Without installation: also $99. Sigh.) It will do MP3 (also
WMA/AAC) CD's, and has both an auxiliary jack and a USB port on the
front, and doesn't have a freakin' light show to distract you from the
road. The lighting also seems somewhat subdued, which is important to
me, although the main buttons are blue, which I hate. (Alpine used to
use a nice gentle green, which I really liked. Everybody seems to
want blue now but I hate it, because due to the biomechanics of the
eye it is generally fuzzy and out of focus, especially since they're
usually using ultra-bright monochromatic light... just because they
can I suppose.) We'll reserve judgement until I can see it at night,
lower-end units like this do not dim when the dash lights are on.
Friday, November 11, 2011
I stopped by the junkyard to try to get some special Becker sockets
to make a cut-free adapter cable for the Alpine, but I was skunked.
They only had a 116 in, and apparently it uses different connectors.
I thought I already had some in the junkbox, but I haven't been able
to locate them.
Saturday, November 12, 2011
Acting on a hunch I went down to the parts cars. Smelly (300D, 123),
as it turns out, had the same connectors as the junkyard 116. The '87
300TD, on the other hand, had just what I wanted! I grabbed the two
Becker sockets for the dashboard speakers and took 'em to the bench,
and soldered them, two spade lugs, a ring, and a bullet connector to
the CDE-100's harness. Everything will hook right up to what was
there for the Becker, except that new radios have embedded clocks and
electronic station memories and thus require continuous +12 V,
which isn't provided for the old Becker. Fortunately I found that
there was an unused factory 2-pin connector taped to the cable that
feeds the cigarette lighter and radio, and it had battery power on it.
Score! (That's what the bullet connector was for, I ransacked the
junkbox and found one that was a little larger than the norm and which
fit snugly into the bore of the connector.) With this done the Alpine
installation is completely reversible, and/or can be transferred
quickly and painlessly to another similar car.
I tried it out and the clock was easy to figure out how to set, even
without the manual. The antenna goes up and down, and (nice!) goes
down when it's on CD or Aux. The radio works and I set a couple of
stations. I tried out a home-recorded CD and it worked just fine.
The clock and station memory held with the key off. Yay, Alpine.
Hopefully this will eliminate the nasty noise that was coming from the
general vicinity of the other seat. RIP, iPod-ified Becker, I wish I
had never wasted my time on you.
Monday, November 14, 2011
I cleaned the insides of the windows with my usual 1/2 ammonia, 1/2
alcohol mixture, in a spray bottle, and paper towels. Smelly, but
effective.
It shifted oddly a couple of times yesterday, so I added 1/2 quart of
ATF. (The dipstick [cold] showed low again.) I was out of time to do
more, but I did notice that the oil was low and it was long past time
to change the oil again. Jill really can rack up the miles when
you're not looking...
I bought an oil filter at NAPA. $12.
Tuesday, November 15, 2011
After work I changed the oil and filter. Another 11kmi, not good!
The oil was sludgy enough that it didn't want to suck out the top.
Eventually it did and I got things put back together. When I started
it there was the usual delay until the oil pressure came up. When I
got out to check for leaks... OH, YEAH!!!!
I botched the filter install somehow, the cap isn't sealing. (The
NAPA cheapie's O-ring was loose-fitting, and wouldn't really stay in
place while installing the cap. I hate working in the cold
and dark, it's hard to work and hard to see, even with a bright work
lamp.) Black oil everywhere. In disgust I shut it down and went
inside for dinner and to warm up.
Wednesday, November 16, 2011
20 °F this morning, not too fun to be working on the car! I
got the filter sealed right, but it was wedged down due to the pinched
O-ring, and during my attempts to get it loose I broke the pressure
line to the ALDA. Duct tape, for a temporary fix, I was out of time.
...When I got home I shoveled dirt over the big black puddle on the
concrete. It started snowing while I did this.
Thursday, November 17, 2011
The brake pad light has been coming on, so this morning I jacked up
the car and had a look. Bendix calipers on both sides, but the LF
side didn't have any pad sensors. The RF side did, and both where
being sliced into. I got out my junkbox brake pads and found two that
were better, and put those in instead. The car could use a full brake
job, methinks.
...The car drove well and the brake light business was gone. At noon
I swapped cars with Jill, this'll be hers for the winter.
Thursday, December 8, 2011
I got home from work and it was about 25 °F outside and I knew
Jill was going to rehearsal within minutes, and yet I found the car not
plugged in! I'd told her, repeatedly, that it needed
30 minutes to an hour of preheat in this kind of weather in order
to start reliably, and yet...somehow it would be my fault. Yeah. So
I plugged it in.
Sure enough, within 5 minutes she was ready to go but the car wasn't.
We fought it awhile and really gave the battery a workout, I even went
so far as to point a space heater down its throat but no good. It
half-caught at times and really filled the air with a stinking cloud
of vaporized diesel, but there was no running that night. I noticed
that the glow plug light was no longer coming on, which was not a good
sign. We finally gave up and she drove off, late, in a huff in the
Frankenheap (not her favorite
car, though it was all warmed up and has the happy Christmas lights); I put the
battery on charge.
Friday, December 9, 2011
This morning I went out in the 25 °F cold, rigged some lights,
and tested the glow plugs. Two of the five, #'s 3–4, were
open circuits. Yeah, no way that'd start in this weather! (We may
finally be seeing some fallout from the car's poor-man's violet-wire
afterglow system.) I went to the parts pile to see what, if anything,
I had on-hand in that line, and found five pencil-type that weren't
obviously labeled for the OM60x engines. Two Bosch
0 250 201 039, two Autolite 1103, and one Beru
0 100 221 138. The Bosch, at least, cross-reference to
this car. I was able to replace #3 easily enough with a used Bosch
plug, but I ran out of time on #4, it's hard to get a 12mm wrench on
it securely enough to not round it off. I did get the wire off of it,
at least.
...After work I came home a bit early to get enough time to finish the
job before Jill had to go to orchestra. I was able to get an open-end
wrench on the bad plug and break it loose. It was a pain walking it
out half a flat at a time, but I eventually prevailed. The new (used
Bosch) plug went in easily and I got it all connected back up. (The
block heater'd been on all day, the engine was pleasantly warm to work
on though it was still about 25 °F outside.) I tested the
plugs with the ohmmeter and all were good, then I used the Fluke
current clamp and a bit of 10-gauge wire to feed power to them
serially through the connector plug from the big fuse screw. All drew
20–25 A at first, dropping down to about 14 A over a
period of some seconds. I then buttoned up the car and started it.
No problems and less than half a second of cranking was required. It
didn't really want to shut off, however, and I didn't see any problems
in the vacuum connections from working on it. It's just really cold,
and whatever leak it has is most unhappy in the cold. That will need
addressing soon, methinks.
The car started for her just fine and off she drove... When she got
back (late) she reported that all was well.
Wednesday, December 14, 2011
Jill says the car intermittently doesn't start, just cranks, so I
checked the glow plugs again this morning. All test fine with the
ohmmeter, and the fuse looks good. Strange. I used the repaired trouble light to see
what I was doing out in the cold and dark. (On the end of an
extension cord, its troublesome reel cord doesn't reach to where the
car is normally parked.) Worked great.
I also got out a piece of rubber vacuum coupler and patched the
pressure line to the ALDA that I broke before.
The duct tape had come loose, imagine that!
Saturday, December 17, 2011
Many moons too late, but I finally was able to park this car inside
(since I moved the SEL out of the
way) as an anniversary present of sorts for Jill.
Friday, December 23, 2011
Jill's been having persistent starting troubles, but all the GP's are
(now) good. It cranks just fine, but won't start. Intermittently,
according to her. To me it sounds like the GP's just aren't doing
their job well. Today I had a chance to dig into it a little bit. I
started by cleaning the relay connections and putting Caig Deoxit on
them. I pulled the big fuse and it was good, but I still cleaned it
off with a little wire brush and put it back together with Deoxit. I
pulled the relay and took it to the bench, but it seemed to behave
well there. (Interestingly, if the big fuse is not there the relay
will buzz loudly after it times out, I wonder if that is deliberate?
I'll look into that further later, it may be one of the system's
self-diagnostic traits.) Back on the car I checked the GP current, it
started out at a peak of 130 A and dropped down to about
50 A steady-state. The GP's, however, were only getting at most
10 V on them, they're rated at 11 V. I measured 0.2 V
drop on ground side of battery to the engine block, which was good.
Between the battery positive post to the relay power post I measured a
2 V drop while the GP's were on, that's terrible! She had to go
so I didn't get to dig into it further, but I imagine that either the
feed end of the power wire to the relay is corroded or loose, or else
the wire itself has been damaged somehow. I checked the ETM and found
that C105 is where this wire supposedly originates, and that this is
the three-terminal power block right next to the battery. I'd already
loosened and tightened its three screws, and sprayed Deoxit on them,
as part of what I'd first done, but nothing more. Next time.
The car started beautifully, of course, but I'd had the block heater
on while I was working on it, and of course the glow plugs had gotten
run a fair bit while sleuthing. (The battery charger was on it all
the time, to replenish the losses.) And it was parked inside. I
expected no trouble this time.
Sunday, January 8, 2012
Jill's still having starting troubles so I went and did a bit more
testing. There's still a 2 V drop on the positive lead during
glow. I opened up the terminal block near the battery and it seems to
be all OK, it's looking like the wire itself is degraded. I may need
to route another one. That's a bit scary, since it's unfused, gotta
do a real good job so that there's no chance whatsoever of pinching or
abrasion over time shorting it out.
I also think that the glow timer light is being overly optimistic, I
suggested to Jill that she use the seat belt light instead as it runs
longer.
I queried the mailing list, and three other 123-model cars had drops
of 1.0 V, 1.3 V, and 1.7 V. Sounds like there's a bit
of a spread there, but I wouldn't be proud of any of those
figures. Perhaps MB skimped a bit on the wiring here?
Wednesday, January 11, 2012
The coolant level was low, very low. I'd noticed a leak weeks earlier
and had tightened the drain cock, which seems to have cured the
problem, but I didn't notice at the time that the coolant was
particularly low (it probably was), it's hard to read the level in the
reservoir in poor light. I ended up putting in about 3/4 gallon of
G-05 mix, which is a lot. I also filled up the washer reservoir, the
nasty crap they spray on the freeways around here is really tenacious
goo.
Jill said that yesterday the radio acted weird and cut off when the
glove box was opened. I checked this morning, and it was indeed
repeatable. Weird. I pulled the radio out and checked the wiring,
and the +12 V switched feed dropped to about +6 V when the
glove box was opened; the light itself didn't come on. The glove box
light, radio, and cigarette lighter all draw from the same fuse. It
turned out that that fuse was intermittent, though looked fine, so I
reversed it in its socket and used Deoxit on it, and its neighbors;
that cured the problem. It probably happened because she's using a
new, cheap seat heater pad I gave her for Christmas and the fuses are
old and have divots in the contact ends from vibration and age. I put
the radio back, we'll see if it holds up.
While I had it out I used the Deoxit on the dome light switch, and
refreshed the paint on the white stripe on its knob. I've wanted to
do that for awhile.
Jill also had said that the windshield washer nozzles were clogged. I
pulled the hoses off of them, poked them out with a dental pick, and
blew backwards through them with compressed air. I also flushed the
lines to remove any dirt that might have been in there. Unfortunately
one of the 90° fittings broke when I pulled it apart so I cleaned
it off with brake cleaner and tacked it back together with
cyanoacrylate glue. (I should have warmed it with the heat gun before
pulling on it.) I then mixed up some 5-minute epoxy and potted the
break, and held it over a warm light bulb and rolled it around until
the glue started to set (both to keep the glue coating even and to keep
it from dripping), then I clipped it in place over the lamp to finish
curing while I got ready for work. When ready I put it back together
and re-aimed the nozzles with the pick. (Yes, I need a new fitting but
I didn't have a new fitting on me, doing this got it back
on the road today.)
Thursday, January 12, 2012
I thought it was cold, at 16 °F yesterday, but today it's
13 °F! Good thing I'm able to work in the (one) heated
garage again since I moved out the SEL.
Jill's new iPhone charger plug doesn't fit in the cigarette lighter
socket, nor did the USB port on the radio seem able to charge it. I
took a look, and she'd bought a 'mini' charger, which didn't have a
round plug but rather an oval, and it didn't fit securely into an
actual cigarette lighter at all. (I'm sure it's fine in a power-only
socket.) I checked, and the radio was unable to charge the iPhone, it
either doesn't have enough current available or it needs some kind of
configuration on the USB plug that it's not seeing. The radio
did power a USB memory stick, so it's not defective. I had a
wall-wart power-only socket in the junk box, so I sacrificed it (sob!)
and a spare cigarette power plug and spliced them together to make a
short extension cord. (I used heat-shrink tubing to re-insulate it
and make it neat.) With this in place the iPhone would charge without
problem.
I then removed the Bosch 0 333 402 507 (MB
002 545 06 32) 12 V/5-Cyl glow plug relay from the
car and opened it up. Besides the big relay it had the usual
counter-wound 4:1 plug windings around a reed switch (tres elegant!)
and some circuitry: five transistors, two thermistors, nine diodes, a
bunch of resistors, two precision capacitors, an LM2903 op-amp, and
two electrolytic capacitors (one 220 µF, one
100 µF) on a coated PCB. I pulled the electrolytics and
tested them, but they seemed OK. I replaced them anyway, but I doubt
it'll make any difference. I used hot glue to attach the new
capacitors to the board for vibration resistance, the originals had
also been glued in place. I filed the one pitted contact (of twins)
on the relay on general principles, and put it back together as I was
out of time. In the ~50 °F garage the GP light was on for
about 5 seconds, and the plugs timed out after about
24 seconds. (The relay was probably still at room temperature
inside where the thermistors are.)
The manual has relevant jobs:
- 15-705 Operation of preglow system
- 15-708 Installing preglow time relay with modified ventilation
- 15-710 Checking preglow system
The first one is actually the most interesting. The manual implies
that at freezing the required preglow is about 7 seconds, which
seems short to me. For now I've told Jill to wait at least until the
seat belt light has extinguished, or for a slow count of 20.
Here is an approximation of the glow time/temperature chart from 15-705,
for quick reference:
Temp (°C) | (°F) | Time (sec)
|
---|
–30 | –22 | 27
|
–20 | –4 | 17
|
–10 | 14 | 10
|
0 | 32 | 7
|
10 | 50 | 4
|
20 | 68 | 3
|
30 | 86 | 2
|
Monday, January 23, 2012
Disaster! This morning was very icy on the hill, and as I'd had a
fair bit of trouble descending I resolved to call Jill from work and
suggest that she not go anywhere until it'd warmed up, or cooled off,
or whatever. Too late! By the time I got to work she was calling me,
telling me that she'd spun out on the hill and slid off the road,
knocking over the stop sign at the bottom of the hill and bashing in
the driver's door.
Crap.
I drove back home to look at it, and it appears that if she had
managed to miss the sign there would have been no damage at all. As
it is, the door is pretty much destroyed. It completely took out the
handle, so she has to get in on the passenger side. As befits a
Mercedes, once inside she can get out normally, and slam the door
shut. There's a small crease in the rocker under the door, but it's
minor and can be disregarded, I see no other body damage. The key
cylinder of the wrecked handle looks intact, so I should be able to
swap it into a junkyard handle to keep the key the same.
Looks like I'm going to have to come up with a new door. I have
Smelly in the woods, but it has no handles nor any other hardware.
There's a 123 at the U-Pull,
I'll swing by and see what it's got. The car's going to look bad
(worse?) after repair, it's unlikely that the replacement will be the
right color.
Jill also apparently needs ice driving lessons, she was holding the
car in low gear to keep the speed down (good), but did not put the car
in neutral once it broke loose (bad). (She should have hit neutral
and recovered via steering, before pumping the brakes to slow down as
best she could.)
Tuesday, January 24, 2012
I went to the U-Pull, and found
the 123 was still there and had a decent door. It was a 1980 Euro
280E, so it had a cloth interior and crank windows, though it did have
power locks. The bottom trim piece had come off, but was still with
the car, the mirror glass was gone, and the door check was shot.
There is some rust setting up in the bottom, at the seal channel, so
there'll be some work to do there. Anyway, I removed the door, it
came off pretty easy, just the four bolts and the door check strap
pin. I cut the vacuum lines where they came through the hinge. About
$25, though I did find $1.06 in change in the car to offset the
expenses. (This included a $1 coin, which looks a lot like a souvenir
rather than money once the shine is off it! They seem to be
corrosion-prone.)
The same car also had a pair of Bosch Euro headlamps. The glass was
broken out of one and the reflectors were pretty degraded, and both
had broken-off mounting ears, but I grabbed them, and their vacuum
hoses, anyway.
There was a 1960 180 there, which is a homely little cuss, a 201, a
124 300D and a 140 S320. (All airbags were deployed.) Odd that there
was nothing from the 70's. The S320 looked interesting, this is the
first time I'd seen the double-pane window glass up close.
Wednesday, January 25, 2012
I went back to the U-Pull, and
tackled the 1987 300D (W124), and liberated its glow plug
relay and the high-current wire from the battery to the
relay. That was a pain and a half. I'd like to try
bolstering the existing GP wiring with it, we'll see.
Saturday, January 28, 2012
I started taking apart the replacement door, and the farther along I
went the less happy I got. It was in worse shape than I'd thought, the
whole bottom channel for the weatherstripping was rusted away, and
there was a lot of rust in the door bottom too. Looks like it started
under the weatherstrip itself, and worked its way in from there.
(Rather than plugged drain holes causing rust to start on the inside
and work out.) The window tracks were messed up, which made it bind on
the way up, which caused PO to use too much torque on the handle which
flexed the door's inner metal panel and cracked it over time. So I'm
looking at a serious amount of rust repair and some welding, all for a
door that's the wrong color anyway. Ick.
OTOH I could just wait for a better door to come along, if I could get
the bent door working better. (I'd planned on this possibility all
along, the door itself was cheap enough that if all I got out of it
was a handle and the piece of belt trim I'd still be happy.) Figuring
I had very little to lose I opened up the damaged door and removed the
remains of the ruined door handle, and started hammering the metal
back out. I used a chunk of maple firewood that tapered down to about
½"×1½" or so, yet had a mallet-sized big
end which I could hit. The thin tapered end reached through the holes
in the door's inner panel, allowing me to direct the force better than
a big chunk would. Being wood it's softer than metal and less likely
to poke dimples into the panel. I had my son hold the door while I
whacked away. I also used a big crowbar to pry and pound at the
crease lines in the metalwork (the ones that belong there). I used
various small crowbars of my acquaintance to hook through the door
handle holes and pull out, trying to restore the correct profile in
the area without doing too much further damage. That actually went
fairly well. I removed the bottom trim strip and found that most of
the damage at the bottom was to the strip itself, which is metal with
plastic molded around it. (The strip comes off with one 8mm nut at
the trailing edge, behind a snap-in plastic cap, and a hook at the
front. I had to break it loose from the plastic retaining clips along
the middle and then pull backwards to release the front hook.) I
think I'll be able to restore the strip to usability on the anvil.
(The replacement door's strip was pried off, breaking off both the
hook and the retaining screw.) At this point the door opened and
closed well again, you could use a finger to grab the latch release
eye and pull the door open. The inner lock mechanism worked fine. It
no longer scraped at the front as it opened. Pretty good for a first
cut at the problem, I thought.
With this it was time to address the door handle itself. The
replacement, naturally, had no key and its weather door was long-gone.
But it was all there. The original was shattered into pieces, but its
key cylinder was untouched. (The actuating rod was bent, however.) I
found a bent siding trim nail in the metal recycling bin that looked
to be about the same diameter as the roll pin that holds the actuating
rod mechanism to the lock cylinder. I straightened that and had my
son hold the handle against a makeshift anvil while I drove the roll
pin out. (I had to straighten the nail a few times along the way.)
Once the pin was out the lock cylinder pulled straight out of the
handle. (Make sure the key is in the cylinder while you do this, and
don't lose the lock's torsion spring as it comes loose! If you remove
the key you could lose all the spring-loaded lock wafers, or at least
mix them all up and no longer be able to operate the lock.) I then
cleaned the lock guts with brake cleaner, removing the dirt and grime.
I then re-lubricated the lock wafers with spray graphite lock lube.
We then took apart the replacement handle the same way. Its lock was
full of dirt and grunge, the missing weather door had obviously been
necessary.
I tried to straighten the bent operating rod, but it was pot metal and
broke, no surprise. The replacement had a differently-shaped end
where it engaged the latch, but seemed to work OK nonetheless. I put
the good handle back together with the original lock cylinder and the
replacement's operating rod, we reversed the anvil/roll pin operation.
Once it was together the key operated as it should, and I slipped the
handle into position. It worked! I then tightened the three screws.
At this point the door was fully operational, but still could use some
more cosmetic shaping of the metal, and the trim pieces repaired and
replaced.
Sunday, January 29, 2012
I got out my as-yet-unused Harbor Freight body kit (hammers and
dollies) and tried to do some more straightening. I think there was
at most moderate success, but it was worth trying. The main problem
is access. I did remove the handle and straighten things out around
there a bit.
I was going to touch up the paint, I'd found an old blue rattle can.
I was going to spray in the cap and dab it on to the bare spots, but
the can seemed flat. I stupidly decided the propellant was gone and
punched a hole in the side to stick a brush into, and the can promptly
liberated most of its contents onto us, and the car—the bulk of
it on the door. Oops! We spent a fun time with turpentine removing
it from the glass, the trim, and ourselves. I left it on the paint,
it did mostly cover the door after all. I was able to find a
little left in the can to use the brush on, for the inside and the
weatherseal channel. I had to use a green can to do the scrapes on
the inside of the door where I had worked on it. That can, too, had
trouble—once it started spraying it wouldn't stop.
Both cans ended up in the garbage. I then straightened the bottom
trim piece out with a couple of hammers. At least it was more or less
straight, though the attachment channel was wrecked in one spot. I
figured out how it went back on on the car, you slide the hook into
the front hole, hook it over the tops of the plastic buttons and snap
it down over them while working the bolt into the rear hole. It
didn't mate perfectly, due to the remaining damage and the inability
to clip over the button in the bent area of the channel, but it's not
bad. Between the two doors' trim strips I found enough red snap-in
trim buttons to get the replacement belt trim back in place. That
masked the damage a lot, it being there and reasonable looking.
(While I was in the area I re-attached the fender belt trim too, it
had started coming loose. I tried pushing its depressed area out a
bit from the wheel well, I'm hoping that'll help.)
I started to put the door back together, but the window didn't work.
Stuck at the top of the track. Seems like the track might have gotten
a tiny pinch in it, because once you can get the window down an inch
or so it works fine. We were tired and hungry, though, so we stopped
for the day.
Monday, January 30, 2012
I worked on the window, and I didn't have much luck. The window also
binds against the side-impact bar, and doesn't want to fit into the
weatherseal at the top. Things are all out of whack, but I needed to
get it back together so Jill could drive it. The window is marginally
more movable now, at least, and should hold for awhile. I really need
to find a good replacement door. I then put the door back
together, that was uneventful, and cleaned up the area. I suppose the
car does look better than it did, and it certainly works better, but
it doesn't look all that good to me.
Sunday, February 5, 2012
The driver's door had a bit of a wind leak and the upper corner of the
window frame didn't look like it was fully flush, so I opened the door
and rolled down the window and whanged away on the window frame with a
rubber mallet. This bent the frame inwards some, which cured the
problem. (This is quite nerve-wracking to see done, but it's the
approved way!) Slapping down a stop sign no doubt shifted things a
bit.
Tuesday, February 7, 2012
The muffler fell off on a speed bump today. It'd been cracked at the
pipe, probably from when it went into the ditch, and finally let loose
today. I put it into the trunk. At least the turbocharger is itself
a nearly-adequate muffler and there's a center resonator, the car
doesn't sound too bad this way.
Wednesday, February 8, 2012
I checked the fluids, and it needed power steering fluid, a pint (at
least) of ATF, and a quart (at least) of engine oil. Thirsty girl! I
looked at the muffler and it looked like it broke off at the joint
where I'd (gas) welded it on in the first place. That weld was very
poor, and didn't penetrate properly. I thought it'd go back on just
fine after cleaning it up, and this time I'll use the wire-feed.
Saturday, February 11, 2012
Welding day! I backed the car outside and up onto ramps, wire-brushed
and ground the muffler end clean(er), and dropped the pipe from the
car. I started brushing the pipe clean and found that there were some
erosion holes along the top outside bend near the broken joint, so I
had to clean that up more, find a scrap piece of muffler pipe, cut a
patch for this area, and weld it on. (The rest of the pipe looked
great.) That took a fair bit of time, so once I had it welded on I
broke for breakfast.
I hung the muffler and pipe back in place, first using the handheld
bandsaw to align the joint better, and tack welded the joint along the
bottom, then I dropped it all back down from the car to weld over the
top, then hung it back up permanently and finished the job. I used
my $50 Hobart gasless wire-feed welder,
it's portable. The job was not made more pleasant by the light
drizzle that was falling the whole time.
Jill drove off later, and said that it was back to normal.
Friday, February 17, 2012
Jill reported that the right low headlight was out. Turned out to be
a corroded fuse. She also said that the right washer nozzle wasn't
working, and I found that was because the fitting had cracked and
popped off. I put a collar of heat-shrink tubing around it and used
the butane torch to shrink it, which holds it in place. Onwards to
Enumclaw! (Skiing trip.)
...Turns out the monovalve insert appears to be malfunctioning, we had
plenty of heat until we got well on the freeway. (At speed, once it
starts modulating the heater core temperature, the heat began fading.
If you stopped the heat came back. Classic.) It would wait
until we're on a road trip to exhibit these problems!
Tuesday, February 21, 2012
I removed the monovalve insert before our return trip, and it is
indeed torn. There are considerable signs of water leakage inside the
monovalve housing. I shook out the water in the plunger and put it
back together, hoping that removing the waterlogging would help get us
home.
...It did, sort of. But it is definitely in need of replacement! We
left the heat on MAX, on low fan, and modulated the cabin temperature
via a window. (If you let the monovalve cycle it tended to get stuck
'off'.)
Friday, March 16, 2012
Coupla little things, Jill stopped by work today and I cycled the
window switches until the LR window would go back up. I also re-set
the spring in the glovebox latch so that it would close again. Just
some of those little chores.
In the evening I changed the oil. (Finally! Another 7kmi change,
nothing to be too proud of.)
Saturday, March 17, 2012
On our skiing trip (local, up Mt. Spokane) the RR door check finally
decided to lock up. I tried to finesse it closed, but it wasn't
having any. I finally just forced the door shut, destroying the door
check and rendering the door unusable. Crap.
Thursday, March 29, 2012
The Chicken Wagon is sick. Jill said it had not been wanting to go
forwards yesterday, and she'd already put in a half quart of ATF, so I
checked the level again and was very low. I put in another half quart
and it would move, so I brought another quart with me. I was able to
check the level once I got to work and it seemed quite low, so I put
in another quart. Even with plenty of fluid it doesn't want to go
into first gear, though reverse is just fine. It also stutters
sometimes going into other gears. Methinks it's perhaps on its last
legs, this is fairly sudden. It won't downshift into third, and
sometimes it goes neutral-y on steep downhills. There's obviously a
leak somewhere, but is it possible that whatever is leaking is causing
this problem? Or did Jill try to drive it too much with not enough
fluid (due to the leak) and ruin the clutches? It didn't behave well
on my way home from work, and I checked the fluid level formally when
I got home. A tetch high, even, so it's not slipping due to a lack.
We're down to our last working cars, something has got to change.
I did a quick survey, and it is possible that this could be the
infamous B2 piston failure, though the symptoms don't line up 100%.
(Worse would be a B2 band failure.) The inability to get moving at
first, especially on a hill, but normal freeway driving does
match up though.
Wednesday, February 6, 2013
I put the battery on charge, it was pretty thirsty.
Saturday, April 20, 2013
I put the battery on charge, again.
Friday, May 5, 2017
The battery turned up dead this year. Jill states that she wants this
car running as a backup, so today I bought another one. $119 at Home
Depot, of all places.
Wednesday, August 15, 2018
We've decided to just take the car in to get the B2 piston
(transmission) fixed, I clearly don't have time to do the job.
Fernando has retired, but Silver Star Automotive knows the car model
and the job. This morning I put the new battery in the car,
after killing all the wasps living in it, and it started right up. It
goes into reverse, but not forward, so that's a fairly definite sign
of the B2 problem.
Wednesday, August 22, 2018
Daniel and I took the car to the shop. We got it started early this
morning, when traffic is next to nonexistent, and towed it out to the
road. We unhooked, and I started coasting down the hill. Once I was
up to speed the transmission would engage, confirming that it was a B2
piston problem. I drove it all the way to the shop, running every
stop sign and timing the lights so that I didn't have to stop. Not
100% legal, but I was being very careful, following Rule #1, and we
were always ready to revert to using the tow rope if a stop was
necessary. It helped that most of the trip was freeway, under very
light early morning traffic conditions; Daniel followed me in. I
rolled to a stop across the street from the shop, after which it would
not move again, and went inside to take care of business. That done,
I dropped Daniel off at school and went about my day. Fairly smooth
operation, I thought.
Wednesday, August 29, 2018
Picked up the car, $818.92, and it was indeed the B2 piston. The car
drove home normally, whereupon it got parked again. I disconnected
the battery.
Tuesday, September 5, 2023
There's been an interest in this car, which I think I could let go of
for the right price. Ten years in storage is long enough.
I connected the battery, which I'd charged sporadically over the
years, and the car started right up, even though the battery was weak
and could barely turn the engine over. I brought it up into the yard
and washed it, leaving it to idle during. Once clean (enough) I moved
it over to the parking pad and put it on charge while I vacuumed and
got it ready for (potential) sale.
Oddly, the gas cap is missing. It must have been stolen, perhaps when
it was on the street at the shop.
Friday, September 8, 2023
I stopped by the U-Pull, and
picked up a gas cap from a W126 380SE. We'll call it $5.68, counting
the $2 entry fee.
Saturday, September 9, 2023
Showed the car to a potential buyer. He wasn't scared off by my
$3,200 ask, at least. (These particular cars have appreciated
a lot in the last couple of years.)
Sunday, October 29, 2023
Put it in storage, and put a Battery MINDer on it. The car needs
brake service, and it had real battery trouble getting started.
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